IR 05000285/1979012

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IE Insp Rept 50-285/79-12 on 790821-24.No Noncompliance Noted.Major Areas Inspected:Qa Program & Housekeeping Cleanliness Program
ML19254D420
Person / Time
Site: Fort Calhoun 
Issue date: 09/05/1979
From: Dean S, Kelley D, Westerman T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML19254D412 List:
References
50-285-79-12, NUDOCS 7910250473
Download: ML19254D420 (4)


Text

U. S. NUCLEAR REGULATORY COTIISSION OFFICE OF INSPECTION AND ENFORCEMENT

REGION IV

Report No.

50-285/79-12 Docket No.

50-285 License No. DPR-40 Licensee:

Omaha Public Power District 1623 Harney Street Omaha, Nebraska 68102 Facility Name: Fort Calhoun Station - Unit 1 Inspection At: Fort Calhoun Station, Blair, Nebraska Inspection Conducted: August 21-24, 1979 de 9/t//79 Inspectors f

D. L. KeiTep. Jeac

>r-Inspector

' 'Da-d ac / e w,1 S. R. Dean, Reactor Inspector Date

'

Approved by:

7e f.

M M f/f/77 T. F. Westerman, Chief Date Reactor Projects Cection Inspection Summary Inspection on August 21-24, 1979 (Report No. 50-285/79-12)

Areas Inspected: Routine, unannounced inspection of the licensee's (1) Quality Assurance Program; (2) Housekeeping Cleanliness Program.

The inspection consisted of forty-eight (48) inspectors hours on-site by two (2) NRC inspectors.

Results: Of the two (2) areas inspected, no apparent items of noncompliance or deviations were identified.

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DETAILS SECTION 1.

Persons Contacted

  • R. L. Andrews, Manager, Fort Calhoun Station
  • K. J. Morris, Manager, Administrative Services
  • W. C. Jones, Section Manager, Operations
  • R. L. Jaworski, Acting Manager, Technical Services
  • F. A. Thurtell, Division Manager, Environmental and Regulatory Affairs W. G. Gates, Supervisor, Operations
  • Denotes those attending exit 'oterview.

The inspectors also talked with and interviewed other licensee employees during the inspection.

2.

Housekeeping / Cleanliness Program The inspector reviewed the licensee's Housekeeping / Cleanliness Program to ascertain that the following administrative controls have been established:

a.

Housekeeping

- Housekeeping Zones

- Housekeeping during work activities

- Excess equipment and material control

- Prompt removal of combustible material

- Implementation responsibility b.

Cleanliness

- Cleaning of safety-related components and systems

- Cleanliness classifications

- Material accountability in critical clean areas

- Cleaning requirements for primary system components

- Maintaining cleanliness of previously cleaned systems

- Implementation responr.ibility 1209

?72

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The inspector reviewed Administrative Procedure A-G-6, R3, 9/29/78,

" Housekeeping," to ascertain if the above listed items had been adequately addressed.

In addition to the above procedures, other procedures were reviewed during a previous inspection (79-11)

of the facility fire prevention / protection program.

No items of noncompliance or deviations were identified.

3.

Annual Review of QA Progrom The two QA Procedures listed below were revised since the last annual review. These procedures were reviewed as part of this inspection to verify conformance with the program described in 10 CFR 50, Appendix B, Technical Specifications, and the applicable codes, standards, and regulatory guides.

QAP REV Issue Date Title

.

1 8/7/78 Storage and Retention of QA Records

1 8/7/78 Adverse Conditions Reporting and Correction No items of noncompliance or deviation were identified.

4.

Unit Trip and Recovery At 3:40 p.m. on August 21, 1979, Fort Calhoun Station experienced a unit trip from approximately 100% power. The trip was initiated by the turbine Electro-Hydraulic Controller.

The inspectors arrived in the control room immediately after the trip and observed the actions of the operating staff. During this recovery period the inspectors also observed plant parameters indicated on meters, and strip chart recorders in addition to printouts on the sequence of events recorder and alarm types. The plant was placed in the Hot Standby condition.

Closer and more detailed review of strip charts and computer printout indicated that the unit did not undergo any unexpected or abnormal transient. The inspectors further verified that the plant was recovered and placed in the Hot Standby conditions as prescribed by approved procedures.

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5.

Plant Tour Durit s the course of the inspection the inspectors toured the accessible areas of the plant and made the following observations:

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General cleanliness was satisfactory.

No excessive fluid Icaks or piping vibrations were observed.

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No fire hazards were observed.

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Seismic restraints and pipe hangers appear to be in satis-factory condition.

No items of noncompliance or deviations were identified.

6.

Exit Interview The inspectors met with licensee representatives (denoted in paregraph 1) at the conclusion of the inspection on August 24,,

1979. The inspectors summarized the scope and results of the inspection.

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