IR 05000285/1979009
| ML19208B183 | |
| Person / Time | |
|---|---|
| Site: | Fort Calhoun |
| Issue date: | 07/31/1979 |
| From: | Kelley D, Westerman T NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML19208B178 | List: |
| References | |
| 50-285-79-09, 50-285-79-9, NUDOCS 7909190197 | |
| Download: ML19208B183 (5) | |
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U. S. NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT
REGION IV
Report No. 50-285/79-09 Docket No. 50-285 License No. DPR-40 Licensee:
Omaha Public Power District 1623 Harney Street Omaha, Nebraska 68102 Facility Name: Fort Calhoun Station - Unit 1 Inspection At: Fort Calhoun Station, Blair, Nebraska Inspection Conducted: July 17-20, 1979 Inspector:
nO, k,L jfe30/79 D. L. Kelley," Reatce 1bspector /Dat6 Reviewed by: 7, f, b P-7/- 7 9 T. F. h'esterman, Chief, Reactor Projects Date Section Inspection Summary Inspection on July 17-20, 1979 (Report No. 50-285/79-09) Areas Inspected: Routine, unannounced inspection of maintenance activities, plant operation; and plant conditions observed during a plant tour. The inspection consisted of 24 hours on-site by one hTC inspector.
Results: Of the three (3) areas inspected, no apparent items of noncompliance or deviations were identified.
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DETAILS 1.
Persons Contacted
- R. L. Andrews, Manager, Fort Calhoun Station W. G. Gates, Supervisor, Operations G. R. Peterson, Supervisor, I&C and Electrical Field Maintenance
- Dentoes those attending the exit meeting.
The inspector also talked with and interviewed other liccasee employees during the inspection. These included reactor operators and office personnel.
2.
Plant Operations a.
Shift Log and Operating Records The inspector reviewed the following logs and records: Shift Supervisor's Log, April 1 - June 30, 1979 -, Control Room Operator's Log, April 1 - June 30, 1979 Auxiliary Building Log, April 1 - June 30, 1979 Jumper Log, April 1 - June 30, 1979 Night Order Book, April 1 - June 30, 1979 Surveillance Log, April 1 - June 30, 1979 The logs and records were reviewed to verify conformance to plant procedures, Technical Specification reporting requirements and Limiting Conditions for Operations (LCO).
The inspector noted that some of the signatures, QA stamps or initials were missing from a few procedures and logs. Further inquiry verified that the steps in the procedures and reviews of logs had, in fact, been completed. The inspector discussed this with the licensee.
The inspector was unable to determine whether this was an isolated case or the beginning of a trend. The licensee agreed to review the matter and to take the necessary steps to prevent the matter from becoming a serious problem. This item will remain unresolved pending the results of the review by the licensen (79-09-2a).
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Plant Tour At various times during the inspection, the inspector observed plant operations in the control room including shift change.
Control room manning and equipment status were found to be in accordance with Technical Specification requirements. The inspector toured accessible areas of the auxiliary building, and made the following observations: General cleanliness was satisfactory.
. No excessive fluid leaks or piping vibrations were observed.
. No fire hazzards were observed.
. Seismic restraints and pipe hangers appear to be in satisfacory . condition.
Control room operators were knowledgeable in annunciator status.
. Selected valves were observed to be in the required positions.
. Selected equipment status tags were verified correct.
. No items o'f noncompliance or deviations were identified.
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Reactor Start-up During the second quarter of tais year Ft. Calhoun experienced a reactor trip caused by testinf; the fire protection system and inadvertently wetting a pressare switch which tripped the turbine.
All system responded as required. The inspector reviewed "Startup No. 75 following Reactor Trip due to Loss of Load."
The start-up package consisted of the following: OP-1, R10, March 16,1978, " Check List for Start-up or Trip Recovery" . ST-RPS-2, R3, April 30, 1979, " Wide Range Logarithmic Channels" . ST-RPS-9, R4, April 30, 1979, " Turbine Loss of Load Channels" . ST-RPS-10, R4, April 30, 1979, " Manual Trip Channels" . OI-RPS-1, R2, April 29,1979, " Normal Operation" . OP-7, R15, December 22, 1979, " Reactor Start-up" . (hl"} <- ,S b b '
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The inspector ccncluded that the trip recovery and start-up were accomplished in accordance with Technical Specification requirements and approved procedures.
No items of noncompliance or deviations were identified.
3.
Maintenance Activities The inspector reviewed maintenance activities performed on safety-related systems during the past 12 months. The safety-related activities were associated with the following areas: Reactivity Control and Reactor Distribution . Instrumentation . Reactor Coolant System . Emergency Core Cooling System . Containment Systems . Plant and E,lectrical Power Systems . Within the above areas the maintenance activities were reviewed to determine: Administrative approvals were obtained as needed . Approved procedures were used to accomplish the work . The work was performed using proper fire prevention provisions as applicable . kRequired inspection were performed . Required Test or Calibration activities were performed . Qualified personnel performed the work . Quality Control activities were performed and recorded as required.
. The Maintenance Orders reviewed were: M.0. 21279, December 12, 1978, " Clutch Replacement on CEDM-31" . M.0.18440, March 23,1978, " Replacement of RTD in Pressurize. Vapor Space" . M.0. 20954, November 29, 1978, " Adjust or Replace Seals (PCV-742 C&D)" . . [3G , t, !- . a s (.
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M.0. 21734, February 6,1979, " Disassembly of Reactor Coolant Pump . Seal" M.0. 20184, October 2,1978, " Replace Timer SI-2B on Sequencer 52-2" . M.0. 20813, November 18, 1978, " Repair Leaking End Bell on HX-AC-IA" . M.0. 18122, February 27, 1978, " Free up Purge Pump VA-80B" . M.0.1138, June 28,1979, " Repair Trip Arm on Breaker 1AD1" . No items of noncompliance or deviations were identified.
4.
Unresolved Items Unresolved items are those items for which further information is required to determine whether the items are acceptable items, items of noncompliance or deviations.
Unresolved items are discussed in paragraph 2a.
5.
Exit Interview The inspector met with Mr. R. L. Andrews on July 20, 1979 and suramarized the scope and findings of the inspection.
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