IR 05000259/1979046

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IE Insp Repts 50-259/79-46,50-260/79-46 & 50-296/79-46 on 791127-1207.No Noncompliance Noted.Major Areas Inspected: Plant Operations,Plant Tours,Ros,Refueling,Maint,Physical Protection & Radiation Area Controls
ML18024B380
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 01/17/1980
From: Dance H, Sullivan R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18024B379 List:
References
50-259-79-46, 50-260-79-46, 50-296-79-46, NUDOCS 8003050360
Download: ML18024B380 (8)


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UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTAST., N.W., SUITE 3100 ATLANTA,GEORGIA 30303 Report Nos. 50-259/79-46, 50-260/79-46 and 50-296/79-46 Licensee:

Tennessee Valley Authority 500A Chestnut Street Tower II Chattanooga, Tennessee 37401 Facility Name:

Browns Ferry Nuclear Plant Docket Nos.

50-259, 50-260, 50-296 License Nos.

DPPR-33, DPR-52, and DPR-68 Inspection at Browns Ferry Site near Athens

, Alabama Inspected by:

R. F ~

ullivan So D te Signed Approved by:

H.

C. Dance, Sec ion Chi f, R NS Branch te gned

~

SUHMARY Inspection on November 27 - December 7,

1979 Areas 'Inspected This routine inspection involved 45 resident inspector-hours in the areas of plant operations, plant tours, reportable occurrences, refueling, maintenance, plant physical protection, training and radiation area controls.

Results Of the eight areas inspected no items of noncompliance or deviations were identified.

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DETAIIS Persons Contacted Licensee Employees H. L. Abercrombie, Plant Superintendent J. L. Harness, Assistant Plant Superintendent J.

B. Studdard, Operations Supervisor R. Hunkapillar, Assistant Operations Supervisor J.

A. Teague, Maintenance Supervisor, Electrical M. A. Haney, Maintenance Supervisor, Mechanical J.

R. Pittman, Maintenance Supervisor, Instruments R.

G. Metke, Results Section Supervisor G. T. Jones, Outage Director J. E. Swindell, Assistant Outage Director R. T. Smith, QA Supervisor T. H. Childers, Mechanical Engineer, Outage S.

G. Bugg, Plant Health Physicist A. L. Burnett, Shift Engineer B. E. Baggett, Shift Engineer R. E. Jackson, Captain, Public Safety J.

D. Glover, Shift Engineer R. R. Smallwood, Shift Engineer R. Cole, QA Site Representative, Office of Power Other licensee employees contacted included Licensed Senior Reactor Operators and Reactor Operators, auxiliary operators, craftsmen, technicians, public safety officers, QA personnel and engineering personnel.

Management Interviews Licensee Action on.Previous Inspection Findings Not inspected.

Unresolved Items No unresolved items were identified during this inspection.

Plant Operations The inspector kept informed on a daily basis of the overall plant status and any significant safety matters related to plant operations.

Daily discussions were held with plant management and various members of the plant operations staff.

Frequent visits were made to the shift engineers'ffice and control rooms to review current reactor operating status and activities.

Special visits were made to other locations in the plant to observe activities and to verify system or component statu Selected portions of the daily journals and other operating records were reviewed on at least a weekly basis during the report period.

The inspector made general plant tours on November 30 and December 3, 1979.

Selected areas in the turbine building, reactor buildings and outside areas were visited.

Observations included witnessing work activities in progress, status of operating and standby safety systems, valve positions, snubber condition, instrument readings and recordings, annunciator alarms, house-keeping, radiation area controls and vital area controls.

Informal

'discussions were held with operators and other personnel about work activities and equipment status.

Some of the specific activities observed were:

a.

Unit 2 control room operations following a reactor trip due to a flux spike on November 29, 1979.

Recording charts and log entries were reviewed and discussion held with control room operations personnel.

b.

Unit 2 control room operations involving return to power operations on November 30 1979.

c.

Unit 3 instrumentation readings during the hydrostatic test of the primary system on November 30, 1979.

d.

Portions of the Unit 3 startup from the refueling outage ending on December 6,

1979.

Included were low level power operations from cold conditions to operating conditions.

e.

Shift turnover in the Unit 2 control room on November 29 and 30, 1979.

No items of noncompliance or deviations were identified by the inspector in

,the above areas.

6.

Reportable Occurence Review The below listed licensee event reports were reviewed to determine if the information provided met NRC reporting requirements.

The determination included adequacy of event description and corrective action taken or planned, existence of potential generic problems and the relative safety significance of each event.

LER No.

259/7829 R-1 259/7927 259/7928 Date 11/13/79 11/7/79 ll/15/79 Event Cable raceway outside diesel generator building settled Trip of HPCI turbine HPCI valve failed to open during test

259/7930 11/21/79 Torus hydrogen sensor out of calibration 260/7915 R1 ll/27/79 HPCI overspeed trip set improperly 260/7923 11/30/79 Torus hydrogen sensor out of calibration Corrective action on the above items was determined to be adequate.

The inspector's questions were satisfactorily answered.

7.

Special Operator Training The inspector reviewed with the Training Coordinator the content of the special training provided to licensed operators for Unit 3, prior to startup from the recent refueling outage.

The training covered modifications to the LPCI system, the new accoustical monitoring system in the main steam relief valves and modifications to the controls on certain primary containment isolation valves.

All affected licensed personnel received the subject training prior to December 6,

1979.

8.

Plant Physical Protection During the course of routine inspection activities, the inspector made observations of certain plant physical protection activites.

These included personnel badging, personnel search and escort, vehicle search and escort, vital area access control and physical barriers.

No items of noncompliance or deviations were note I 0