IR 05000155/1987026

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Forwards Safety Insp Rept 50-155/87-26 on 871016-1214.No Violations Noted.Record Copy
ML20195K143
Person / Time
Site: Big Rock Point File:Consumers Energy icon.png
Issue date: 01/25/1988
From: Guldemond W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Buckman F
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
References
NUDOCS 8802020098
Download: ML20195K143 (2)


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Docket No. 50-155 Consumers Power Company ATTH: Dr. F.W. Buckman

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Senior Vice President Energy Supply 212 West Michigan Avenue Jackson, MI 49201 Gentlemen:

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This refers to the routine safety inspection conducted by Mr. Stephen Guthrie of this office on October 16, 1987 - December 14, 1987, of activities at Big

Rock Point Nuclear Plant authorized by NRC Operating License No. OPR-6 and to i

the discussion of our findings with Mr. C. R. Abel at the conclusion of the inspection.

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The enclosed copy of our inspection report identifies areas examined during the inspection. Within these areas, the inspection consisted of a selective examination of procedures and representative records, observations, and interviews with personnel.

No violations of NRC requirements were identified during the course of this inspection.

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In accordance with 10 CFR 2.790 of the Commission's regulations, a copy of this letter and the enclosed inspection report will be placed in the NRC Public Document Room.

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We will gladly discuss any questiens you have concerning this inspection.

Sincerely, l

Original signed by I. N. Jackiw/for

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W. G. Guldemond, Chief r

Reactor Project Branch 2

Enclosure:

Inspection Report

No. 50-155/87026(ORP)

See Attached Distribution

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Consumers Power Company

Distribution

REGION III==

Report No. 50-155/87026(DRP)

Docket No. 50-155

License No. OPR-6

Licensee:

Consumers Power Company

212 West Michigan Avenue

Jackson, MI 49201

Facility Name: Big Rock Point Nuclear Plant

Inspection At: Charlevoix, Michigan

Inspection Conducted: October 16, 1987 - December 14, 1987

Inspector:

S. Guthrie

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Approved By:

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P jects 5 ction 2C

Date

Inspection Summary

Inspection on October 16, 1987 - December 14, 1987 (Report No. 50-155/84-17(ORP))

Areas Inspected:

Routine, unannounced inspection conducted by the Senior

Resident Inspector of Operational Safety, Maintenance Operation, Surveillance

Operation, Reactor Trips, IE Bulletins, Management Meetings, Licensee Event

Report Followup, and Security.

Results: Of the nine areas inspected, no violations or deviations were

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identified.

No significant safety items were identified.

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DETAILS

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1.

Persons Contacted

T. Elward, Plant Superintendent

  • G. Petitjean, Planning and Administrative Services Superintendent
  • G. Withrow, Engineering Maintenance Superintendent
  • R. Alexander, Technical Engineer

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  • R. Abel, Production and Plant Performance Superintendent

L. Monshor, Quality Assurance Superintendent

D. Staton, Shift Supervisor

W. Trubilowicz, Operations Supervisor

  • J. Beer, Chemistry / Health Physics Superintendent

D. Kelly, Maintenance Supervisor

D. Ball, Maintenance Supervisor

W. Blosh, Maintenance Engineer

M. Acker, Senior Engineer

J. Toskey, General Engineer

L. Darrah, Shift Supervisor

J. Ho,an, Shift Supervisor

R. Scheels, Shift Supervisor

J. Boss, Reactor Engineer

The inspector also contacted other licensee personnel in the Operations,

Maintenance, Radiation Protection and Technical Departments.

  • Denotes those present at exit interview.

2.

Operational Safety Verification

The inspector observed control room operations, reviewed applicable legs

and conducted discussions with control room operators during the

inspection period. The inspector verified the operability of selected

emergency systems, reviewed tagout records and verified proper return to

service of affected components. Tours of the containment sphere and

turbine building were conducted to observe plant equipment conditions,

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including potential fire hazards, fluid leaks, and excessive vibrations

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and to verify that maintenance requests had been initiated for equipment

in need of maintenance. The inspector by observation and direct interview

verified that the physical security plan was being implemented in

accordance with the station security plan.

The inspector observed plant housekeeping / cleanliness conditions and

verified implementation of radiation protection controls.

During the

inspection period, the inspector walked down the accessible portions of

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the Liquid Poison, Emergency Condenser, Reactor Depressurization, Post

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Incident, Core Spray and Containment Spray systems to verify operability,

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The inspector also witnessed portions of the radioactive waste system

controls associated with radwaste shipments and barreling.

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a.

On November 9 the licensee commenced a normal shutdown of the

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reactor to enter a scheduled outage of estimated four days duration

to repair Reactor Depressurization System (RDS) depressurization

valve top assemblies and repack RDS isolation valves. The facility

had operated for several weeks at approximately 0.6 gpm unidentified

leak rate, below the administrative limit of 0.8 requiring power

reduction and corrective measures.

Normal values for unidentified

leakage are approximately 0.3 gpm.

The unit was returned to service November 14 following a normal

startup.

Leak rate calculations performed at normal reactor

pressure and temperature following startup indicated RDS repairs had

been ineffective in reducing the unidentified leak rate. Unidentified

leak rate, which did not include that portion of RDS leakage which

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could be collected in specially constructed collection rigs mounted

on the RDS tail pipes, increased from 0.642 gpm on November 14

to 0.752 on November 20. During the shutdown a reactor scram

occurred. The event is discussed in Section 5 of this report,

b.

On November 22 following replacement of RDS depressurization valve

top assemblies on trains A and C, a startup was commenced. During

approach to criticality double notching was observed during withdrawal

on three different control rod drives and all drives were then fully

inserted in the reactor.

During normal rod drive withdrawal a relay

interrupts the withdrawal signal after a prescribed time interval,

thus limiting rod movement to one notch.

In this instance operators

observed the rod traveling two notches before settling into a new

position. An earlier instance of double notching on withdrawal

occurred during the November 14 startup but could not be duplicated

for investigation. The licensee investigated rod drive timing

relays and determined the timing relays were set within

specifications. During trouble shooting two additional drives

were observed double notching.

The licensee experimented with different reactor recirculation

pump discharge valve positions, and during testing identified

three additional double notching drives.

Testing results indicated

that because the rod drive water discharges to the suction of

recirculation pump No. 2, fully opening the pumps discharge valves

reduced the back pressure on the rod drive system, permitting faster

rod drive water flow and resultant faster rod travel time.

For

those drives with rate set valves adjusted to permit relatively fast

rod travel time of approximately 25 seconds, the increased rod drive

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flow rate caused the drive to travel past the first notch before the

timing relay could interrupt the operation.

The licensee retested

all drives and adjusted rate set valves as indicated by test results

conducted with recirculation pumps at full flow with the discharge

valve fully open. Normally, rod drive timing and any required

adjustments are performed during refueling outages with the reactor

head removed and recirculating pumps idle.

The licensee undertook

an evaluation of procedures controlling rod drive operation and

testing to determine the effects of testing at plant conditions not

representative of those seen at power operation.

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Rod drive diagnostic testing revealed two drives which exceeded

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Technical Specifications 5.2.2 (a)(IV).

The specification limits

the speed of control rod drives withdrawal to 23 seconds minimum

for continuous travel over the full length of the stroke.

Drive B-1 timing was 22.6 seconds and drive D-2 was found to be

21.7 seconds.

The increased flow of control rod drive water as

described above was the apparent explanation.

The reactor physic.s

package for the current cycle calculates that a free fall rod

withdrawal, which withdraws the rod from full in to full out in

0.60 seconds, does not exceed the maximum allowable deposited

enthalpy specified by the fuel vendor.

Because the 21.7 second

withdrawal time of drive D-1 is well within the limiting criteria

for the rod free fall accident, the licensee concluded no fuel

damage would have resulted had the drive been fully withdrawn in a

continuous motion.

During normal operation rods are withdrawn one

notch at a time.

The licensee adjusted both drives.

Drive B-1 was

adjusted to 30.5 seconds and drive D-2 was reset to 29.0 seconds as

tested with recirculation pumps at full flow with discharge valves

fully open.

Reactor startup was commenced at 1:00 a.m. November 23,

but was interrupted by a reactor scram at 2:47 a.m.

That scram is

described in Section 5.b of this report.

The reactor was

successfully restarted following repairs to nuclear instrumentation.

During the period November 23-25 the inspector interviewed operators

on several shifts to verify each operator was fully versed in the

observed control rod malfunction, the identified cause, and corrective

action.

The inspector determined that operators performing startup

activities, while aware of instances of double notching of control

rods, were in some instances not aware of the effect of recirculation

pump discharge valve position on rod travel times.

The licensee,

when informed by the inspector, immediately placed a requirement in

the Daily Orders for operators to review the Deficiency Report

describing the event and its resolution.

The inspector noted that during the several startups and shutdowns

and scrams occurring during the period November 9-23, operators

consistently performed the evolutions and required responses in

accordance with procedural requirements and without operator error

or lapses in administrative control.

c.

On December 2 the inspector observed portions of the reactor shutdown

initiated in response to indications of steam leakage in the pipe

tunnel.

Immediately upon receipt of control room alarms from dew

cells located in the pipe tunnel and visual verification of steam

visible from the turbine deck operators commenced power reduction

to permit pipe tunnel entry for inspection.

Area radiation monitors

and sustained elevated offgas release rates were not observed because

of the prompt power reduction.

Inspection revealed through-the-wall

erosion in the shell of the low pressure side of the high pressure

feed heater.

Reactor power was further reduced to permit

nondestructive testing and repair of the defect. The reactor was

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maintained above 212 F and the shutdown cooling system was in

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operation during the maintenance period. Testing and corrective

maintenance is described in Section 3 of this report.

Upon completion of repair activity the reactor reached criticality

at 5:13 a.m. December 7 and the turbine was synchronized at 10:27 a.m.

During startup activities daily water chemistry sampling required by

Technical Specifications was delayed approximately two hours when'

calibration of feedwater instrumentation resulted in prohibition

of containment access.

No violations or deviations were identified in this area.

3.

Monthly Maintenance Observation

Station maintenance activities of safety related systems and components

listed below were observed / reviewed to ascertain that they were conducted

in accordance with approved procedures, regulatory guides and industry

codes or standards and in conformance with technical specifications.

The following items were considered during this review:

the limiting

conditions for operation were met while components or systems were

removed from service; approvals were obtained prior to initiating the

work; activities were accomplished using approved procedures and were

inspected as applicable; functional testing and/or calibrations were

performed prior to returning components or systems to service; quality

control records were maintained; activities were accomplished by

qualified personnel; parts and materials used were properly certified;

radiological controls were implemented; and, fire prevention controls

were implemented.

Work requests were reviewed to determine status of outstanding jobs and

to assure that priority is assigned to safety related equipment maintenance

which may affect system performance,

a.

On October 28 during a routine tour the inspector identified steam

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rising from the top assembly of B RDS depressurization valve,

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Investigation revealed steam escaping from a stud used to bolt

the top assembly to the body of the valve.

The licensee, as part

of repair activities on RDS valves during the outage commencing

November 9, performed cleaning and nondestructive testing of the

mating surfaces between the two valve components.

Leakage at the

stud was not observed following repairs.

b.

On November 9 and 10 the inspector observed disassembly and

inspection of RDS depressurization valves A and B following top

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assembly removal.

Based on direct observation and discussion with

licensee personnel the inspector determined that the seat had

visible cracks, the disc was visibly worn from being used as a

lapping tool during previous repairs, and discolorations in both

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disc and seat showed evidence of steam leakage. Original valve

design calls for seat angle to differ from disc angle, but long term

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use of the disc to lap the seat had resulted in nearly the same

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angle for both disc and seat.

The inspector questioned the use of

a stellite disc to lap a stellite seat and was informed by the

licensee that a cast iron lapping tool would be fabricated for

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future use. The inspector identified to the licensee a visiblo flat

spot or depression on the face of the B yalve's disc, but subsequent

blue checks during reassembly showed it to be outside the seating

area.

The inspector verified that the licensee had devised and implemented

an acceptable system for verifying correct reconnection of

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electrical leads on both valve coils as discussed in Section 4.a of

Report No. 155/87023.

c.

On November 10 the inspector observed testing of steam drum relief

valve serial Number A-5.

The single stage spring loaded relief

valve was removed from service for testing to satisfy a commitment

made by the licensee to verify the operability of steam drum relief

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valves following repeated occurrences of disc to seat adhesion that

resulted in as-found set points approximately 200 psi above

specification.

Incidents of unacceptable relief valve performance

and licensee corrective actions are detailed in Section 4.a of

Report No. 155/87011.

Valve No. A-5, one of six installed on the steam drum as

primary plant overpressure protection, has a specified setpoint

of 1535 psig +/- 15 psig. Testing was performed using compressed

nitrogen and at ambient temperature in accordance with Surveillance

TR-28 Testing of Steam Drum Relief Valves. As-found lift pressure

was 1484.6 psig, 50.4 psig below set point and 35.4 psig below

tolerance. A second test established repeatability at 1488.1 psig.

The adhesion of disc to seat which resulted in elevated lift

pressures during tests earlier in 1987 was not in evidence.

During the test the inspector questioned the procedural requirement

of Surveillance TR-28 to reposition the nozzle blow down ring from

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position 18 to position 2 prior to the as-found test.

The technical

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justification of the long standing practice could not be established

by the licensee.

The licensee maintained that the valve manufacturer

concurred with the adjustment. The inspector provided the licensee

with data from LER 83-74 (valves failed to meet "as found" acceptance

criteria) describing the Palisades Plant's experience with main steam

relief valve as-found setpoints above the specified limit. The

licensee attributed the palisades malfunction to adjustments made to

each valve's blowdown ring prior to as-found testing.

The Palisades

procedure was revised to eliminate the requirement for blowdown ring

adjustment.

To address the inspector's concern the licensee on November 11

performed two additional lift tests on Valve No. A-5 in an effort to

demonstrate that blowdown ring position has no effect on set point.

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The first lift was made with the blowdown ring at position 2 and

results were consistent witn the tests performed November 10.

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second test was conducted with the blowdown ring at its normally

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installed position number 18 and resulted in no appreciable

difference in lift points. The inspector questioned the validity of

any engineering judgements made on the basis of these additional

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lift because (1) the tests did not determine the as-found condition

of the valve, (2) seat leakage through the valve's disc and seat was

observed at a pressure well below the lift point, indicating the

repeated testing had prevented reestablishment of the disc to seat

seal typical of the as-found valve condition, and (3) the valve body

had cooled significantly from the previous day's testing.

On November 11 the Plant Review Committee convened to assess the

safety significance of the low setpoint found on valve A-5.

The PRC

concluded that the 1484.6 psig setpoint would not impede operation

of the emergency condenser, which operates at 100 psig above reactor

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pressure of 1335 psig and approximately 100 psig below steam drum

relief valve setpoints. The liquid poison system, which operates on

siphon effect was expected to operate normally. A relief valve with

a low setpoint thit might stick in the open position represents a

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loss of coolant accident that is an analyzed accident condition

against which the plant is protected. Applicable industry codes do

not address setpoint test results below the setpoint. As a

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conservative measure to verify the disc to seat adhesion phenomenon

was not in evidence the licensee elected to remove and test a second

steam drum relief.

Valve No. A-4 was tested using Surveillance TR-28

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with the blowdown ring in position 2.

The valve has a specified

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lift point of 1585 +/- 15 psig and lifted on the as-found test at

1581.9 psig.

A review by the inspector and Region III concluded that the disc to

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seat adhesion was not in evidence and that the low relief valve

setpoint did not impose an undue safety hazard while installed in

the plant. The testing of at least one additional relief valve

during the upcoming refueling outage in approximately 90' days will

be observed to determine if the low setpoint on valve A-5 was an

isolated incident or is represeritative of a programmatic deficiency

in the licensee's testing or setpoint calibration methodology. The

licensee committed to resolve the apparent conflict between Palisades

and Big Rock procedures that address position of the blowdown ring

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and its effect on valve setpoint.

The licensee is considered to

have met all commitments made to the staff concerning relief valve

testing arising from the concerns over disc to seat adhesion and

resultant high relief valve setpoints.

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d.

The HP feed heater is a single pass U tube heat exchanger with high

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pressure feed water on the tube side and low pressure extraction

steam on the shell side.

Extraction steam is drawn off the turbine

and at full power is approximately 185 psig.

The heat exchanger is

constructed with an internal steam deflector to prevent direct

impingement of steam on the U-tubes. The licensee performed

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nondestructive testing and constructed ultrasound maps of the

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heat exchanger's shell in both of the locations where the internal

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deflector would cause the steam to erode the shell's interior

surface.

Dye penetrant testing was performed in the area of

the erosion to verify the defect had not developed into a

structural crack.

The' turbulence resulting from the deflected

steam eroded the shell side metal from the inside, reducing it from

a nominal 0.562 inch thickness to as little as 0.047 - 0.097 inches

in the area adjacent to the defect.

The licensee welded the eroded area and constructed a patch from

0.25 inch steel rolled to the contour of the 30 inch diameter of the

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heat exchanger's shell.

The patch was sized to cover the areas on

both sides of the shell where ultrasound tests indicated wall

thinning, and was welded directly to the shell material. Attempts

were made to inspect the heater's interior for corrosion and

structural damage using a baroscope, but the restrictive contours of

the internal deflector prevented access. Wall thicknesses were

verified in the area of the only other deflector in the HP feed

heater and were also verified in the areas of possible erosion on

the low and intermediate pressure feed heaters. The licensee

expects to perform major repairs to the HP feed heater and

extraction line during the 1988 refueling outage.

Prior to startup December 7 the licensee unsuccessfully attempted to

hydrostatically pressure test the heat exchanger's shell side.

Several leaking valves prevented reaching test pressure. Visual

inspections of the repaired area were conducted during startup. A

humidity indicator with remote read out and a chart recorder was

installed in the area of the repairs to detect minor leakage.

The

licensee was sensitive to the need for limited personnel access

to the heat exchanger, which is located in the locked pipe tunnel

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not normally accessible during operation except for weekly

inspections.

No violations or deviations were identified in this area.

4.

Surveillance Observation

a.

On November 13 the inspector observed performance of

Surveillance TV-07, Control Rod Drive Scram Test from Notch 23.

The surveillance, which is performed prior to startup to verify

the ability of each control rod to scram from the full out position,

was successfully completed in accordance with procedural requirements.

b.

On November 13 the inspector observed from the control room the

performance of Surveillance T90-12, Reactor Depressurization System

(RDS) Valve Test.

The surveillance involves pressurization of

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portions of RDS piping to normal plant pressure (1335 psig) with

compressed nitrogen and actuation of the RDS depressurization valve

from the control room. A strip recorder verifies depressurization

of the test pressure when the valve is actuated.

The test was

successfully completed in accordance with procedural requirements.,

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c.

The inspector on November 17 reviewed the licensee's preparations

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for cold weather.

The inspector observed preparations which had

been completed and documented on the licensee's cold weather check

off sheet in the screen house, diesel generator room, sphere

ventilation shed and turbine building.

The inspector reviewed

maintenance orders issued to repair inoperable air louvers in the

turbine room,

d.

On November 25 the inspector observed performance of monthly

surveillance T30-22, ECCS Valve Test.

The surveillance verifies the

operability of four core spray valves.

The test was performed in

accordance with procedural requirements.

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5.

Reactor Trips

a.

On November 9, approximately three hours into a normal shutdown and

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with the reactor subcritical at approximately 15 x 10-3 per cent

power, the reactor tripped on a spurious upscale /downscale signal.

The trip occurred during downscaling of the three picoammeter

channels. With picoammeter No. I downscale with a downscale alarm

inserted, channel No. 3 was downscaled. A spurious high flux signal

caused the trip signal.

The susceptability of reactor trips from

spurious upscale /downscale signals with their origin in picoammeter

circuitry is a long known operating characteristic of the facility

associated with electrical noise at very low power levels. All

partially withdrawn control rods inserted fully and all systems

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functioned normally.

The licensee made the required notifications.

b.

On November 23 at 2:47 a.m. the reactor tripped during approach to

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criticality. With the reactor slightly subcritical operators

observed fluctuations in intermediate range channel 5 period

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indications ranging from +30 seconds to -100 seconds.

The second

intermediate range channel displayed no such fluctuation, and with

reactor power sufficient to register in the lower ranges of power

range instrumentation, operators observed no power level oscillations.

While ender observation by operators the reactor tripped on short

period. All systems functioned normally and the required

notifications were completed.

Cause of tne erratic indication was

determined to be electronic failure of channel 5 nuclear

instrumentation. The circuitry was replaced and tested and restart

commenced at approximately 1:00 p.m. November 23.

No violations or deviations were identified in this area.

6.

Management Meeting

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On October 21 the licensee participated in a management meeting with

members of the Region III staff in Glen Ellyn. During the meeting the

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licensee discussed the implementation of the trial Enhanced Performance

Incentive Program implemented approximately 18 months ago to provide

reduced site Quality Assurance department involvement with selected site

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departments who have demonstrated exemplary performance in meeting

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quality assurance requirements.

The licensee reviewed the program

philosophy and requirements, described the audits, surveillances, and

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inspections performed during the trial period, and proposed the

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formalizedcontinuationoftheprogramthroughachangeintheTopical

Report (CPC-2A). The staff concurred in the licensee s plan to continue

the program for the one site department now participating pending review

of the proposed CPC-ZA changes.

The licensee presently has no additional

candidates for the reduced involvement program.

7.

Licensee Event Reports Followup

Through direct observations, discussions with licensee personnel, and

review of records, the following event reports were reviewed to determine

that reportability requirements were fulfilled, immediate corrective

action was accomplished, and corrective action to prevent recurrence had

been accomplished in accordance with technical specifications.

By letter dated November 12 the licensee submitted Licensee Security

Event Report (BRP-87-01.5), Vital Area Barrier Breach, required by

10 CFR73.71(c). Contents of the report contain safeguards information

exempt from public disclosure in accordance with 10 CFR73.21(c). The

event is the subject of Inspection Report No. 155/87021(DRSS) and was

discussed with the licensee at an enforcement conference in Region III

on October 21, 1987.

The LER is considered closed.

By letter dated November 13 the licensee submitted Revision 3 to

LER 87-003, Inoperable Primary System Safety Valves. The LER was

submitted as an informational update to report the results of safety

valve testing conducted November 10-11. The update documented that test

results showed no evidence of disc to seat adhesion that earlier had

resulted in lif t points above specification. These elevated lift points

were the subject of the original LER submittal. A detailed description

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of the November 10-11 testing is presented in Section 4.c of this report.

The LER and Revision 3 are considered closed.

By letter dated December 1 the licensee submitted LER 87-011, Reactor

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Trip-Spurious Upscale /Downscale trip. The reactor trip occurred

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November 9 during a shutdown to perform RAS top assembly replacement.

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The event is described in Section 6.a of this report.

The LER is

considered closed.

8.

Security

a.

On December 8 the inspector observed a site employee enter the site

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with a sheathed knife normally used in outdoor sports. The inspector

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questioned the need to bring into the protected area a device which

was not a work related tool and which could be perceived as a weapon.

Interviews with several security officers revealed an inconsistency

among officers regarding the admissibility of knives of that

description. The licensee elected to prohibit the knife's entry

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and, at the ir.spector's request, committed to develop a prohibited

items list and provida clear instructions to security officers on

what items are prohibited from the site,

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b.

On December 9 the inspector observed through the window in the door

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to the Central Alarm Station (CAS) the security supervisor on watch

to have the appearance of inattentiveness.

Specifically, the interior

lights had been switched off, the supervisor _was in a fully reclined

position in his chair -with his feet up on the panel, and for a period

of several seconds his eyes were observed to be closed. The inspector

informed licensee management.

The supervisor was interviewed by the

licensee and counselled on the importance of professional conduct

and the appearance of attentiveness at all times. The licensee

committed to develop and implement a policy which clearly conveys to

security personnel staffing alarm stations expectations for

appropriate behavior to ensure attentiveness while on duty.

9.

Bulletins

As required by I.E.Bulletin 87-02, Fastener Testing to Determine

Conformance With Applicable Material Specifications, the inspector

participated with the licensee in the selection of 20 samples of safety

and non-safety related fasteners from current stock.

Nuts were included

for all fasteners selected.

The inspector noted that because the

licensee's procurement practices result in nearly all fasteners being

purchased as safety grade stock, only seven of the ten required non-safety

samples available on site. Using guidance from the Staff's Tethnical

contact, the inspector requested that the licensee obtain an additional

three samples of safety grade fasteners to satisfy the requirement

for 20 samples.

10.

Exit Interview

The inspector met with licensee representatives (denoted in Paragraph 1)

throughout the month and at the conclusion of the inspection period and

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summarized the scope and findings of the inspection activities.

The

licensee acknowledged these findings.

The inspectcr also discussed the

likely informational content of the inspection report with regard to

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documents or processes reviewed by the inspector during the inspection.

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The licensee did not identify any such documents or processes as

proprietary.

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