05000498/FIN-2014008-01
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Finding | |
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Title | Inadequate Loop Flow Test |
Description | The team identified a non-cited violation of Technical Specification 6.8.1.d for the failure to implement and maintain written procedures for fire protection program implementation. Specifically, the licensee failed to have procedures for and to flow test the portions of the underground piping that supplied water to the diesel generator buildings since the initial startup test. The licensee initiated actions to perform the flow testing within two months and entered the deficiency into their corrective action program as Condition Report 14-17098. The failure to conduct flow testing of the entire underground fire protection piping loop was a performance deficiency. This performance deficiency was more than minor because it was associated with the protection against external factors attribute (fire) and adversely affected the mitigating systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to performance test the underground fire protection piping loops supplying the emergency diesel generator buildings for both units did not demonstrate the continued capability to deliver adequate flow and pressure to the fire suppression systems supplying those buildings. The team evaluated the finding using Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process, because it affected fire protection defense-in-depth strategies involving fire water supply. Using Appendix F, the team determined that the finding screened to very low safety significance. Specifically, the finding did not prevent the reactor from achieving safe shutdown since only one safe shutdown train would be affected at a time. Since these underground fire protection piping loops had not been flow tested since initial installation and nothing caused the licensee to reevaluate the test, the team determined that this failure did not reflect current performance. |
Site: | South Texas |
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Report | IR 05000498/2014008 Section 1R05 |
Date counted | Sep 30, 2014 (2014Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.05 |
Inspectors (proximate) | B Correll B Larson G Pick G Werner N Hernandez S Alferink |
Violation of: | Technical Specification - Procedures Technical Specification |
INPO aspect | |
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Finding - South Texas - IR 05000498/2014008 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (South Texas) @ 2014Q3
Self-Identified List (South Texas)
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