05000499/FIN-2014007-01
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Finding | |
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| Title | Failure to Accurately Document Completion of a Maintenance Activity |
| Description | The inspectors identified a violation of 10 CFR 50.9; 10 CFR 50, Appendix B, Criterion XVII; and Technical Specification 6.8.1.a, for failure to accurately document completion of a maintenance activity. Specifically, on November 7, 2011, a maintenance supervisor documented that a work order step to hot torque the Unit 2 pressurizer spray valve hold down bolts had been performed, when this activity was never completed. The NRCs investigation determined that this falsification was deliberate violation that impacted the NRCs ability to perform its regulatory function, so this violation is being cited in accordance with the NRC Enforcement Policy (EA-13-213). This issue was entered into the licensees corrective action program under Condition Report 14-4633. The individual who falsified the document was subject to administrative action in accordance with the licensees program, and licensee management reinforced the need to ensure accurate quality records with workers. The failure to accurately document completion of a maintenance activity was a performance deficiency. The performance deficiency was more than minor, therefore, a finding, because it affected the initiating events cornerstone, and adversely affected the cornerstone objective of limiting the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Using the Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Section A, LOCA Initiators, the inspectors determined that the finding was of very low safety significance (Green) because the performance deficiency did not result in an actual degradation of the reactor coolant pressure boundary. In addition, this finding was evaluated under traditional enforcement due to the conclusion that it was a deliberate violation that impacted the NRCs ability to perform its regulatory function, and was determined to be a Severity Level IV violation. The finding was not assigned a cross-cutting aspect because it was not representative of current licensee performance in that the violation occurred more than 2 years ago. |
| Site: | South Texas |
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| Report | IR 05000499/2014007 Section 4OA2 |
| Date counted | Mar 31, 2014 (2014Q1) |
| Type: | Violation: Green |
| cornerstone | Initiating Events |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71152 |
| Inspectors (proximate) | G Guerra N Hernandez N O'Keefe A Sanchez B Correll D Proulxd Proulxn O'Keefe |
| Violation of: | Technical Specification 10 CFR 50 Appendix B Criterion XVII, Quality Assurance Records |
| INPO aspect | |
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Finding - South Texas - IR 05000499/2014007 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (South Texas) @ 2014Q1
Self-Identified List (South Texas)
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