05000368/FIN-2014004-02
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Finding | |
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Title | Failure to Establish Preventative Maintenance on Unit 2 Main Steam Isolation Valves |
Description | Inspectors documented a Green self-revealing non-cited violation of Technical Specification 6.4.1.a for the licensees failure to establish procedures recommended by Regulatory Guide 1.33, Revision 2, Appendix A, Section 9, February 1978. Specifically, the licensee failed to establish preventative maintenance procedures for valve internal inspection and testing of the Unit 2 main steam isolation valves. On December 23, 2013, the train A main steam isolation valve (2CV-1010-1) was declared Inoperable due to the valve sticking at fifteen percent open on multiple stroke attempts. The licensees cause evaluation identified that mechanical binding and corrosion of the valve internals were results of a lack of preventive maintenance. The licensee repaired the 2CV-1010-1 valve and performed subsequent testing to demonstrate Operability. The issue was documented in Condition Report CR-ANO-2-2013-02502. The inspectors determined that the failure to establish preventative maintenance procedures for valve internal inspection and testing of the Unit 2 main steam isolation valves was a performance deficiency. The performance deficiency is more than minor because it was associated with the procedure quality attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences, and is therefore a finding. Specifically, the lack of preventative maintenance adversely affected the reliability of the main steam isolation valve 2CV-1010-1 to close within the time assumed in the accident analysis. Using Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings at Power, Exhibit 2, the inspectors determined the finding to be of very low safety significance (Green) because the finding did not represent the loss of a system safety function and did not represent an actual loss of safety function of at least one train for greater than its technical specification allowed outage time. The finding was determined to have a cross-cutting aspect in the area of problem identification and resolution, in that the licensee failed to thoroughly evaluate issues to ensure that resolutions address causes commensurate with their safety significance. Specifically, during a previous stroke test of the 2CV-1010-1 valve in 2011, the licensee identified that the valve experienced a sluggish or jerky motion and took longer than normal to open. The licensee entered this issue into the corrective action program but did not fully evaluate and troubleshoot the condition adverse to quality to ensure resolution of the cause. |
Site: | Arkansas Nuclear |
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Report | IR 05000368/2014004 Section 1R19 |
Date counted | Sep 30, 2014 (2014Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71111.19 |
Inspectors (proximate) | A Fairbanks B Larson B Tindell J Melfi J Watkins K Clayton M Hayes M Young R Kopriva R Lantz R Latta T Farina |
Violation of: | Technical Specification - Procedures Technical Specification |
CCA | P.2, Evaluation |
INPO aspect | PI.2 |
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Finding - Arkansas Nuclear - IR 05000368/2014004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Arkansas Nuclear) @ 2014Q3
Self-Identified List (Arkansas Nuclear)
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