11-30-2016 | On 10/1/2016 at 0512 CDT with Unit 1 at 99 percent power the plant experienced a turbine trip and automatic reactor trip as a result of inadvertent closure of the 1 A Steam Generator Main Steam Isolation Valve ( MSIV).
This caused a rapid pressure reduction in the remaining two Steam Generators' steam lines, resulting in a Safety Injection (SI). The 1 A MSIV closure was caused by failure of its test solenoid in conjunction with other air system leakage, which vented air pressure from the 1A MSIV actuator. An inadequate technical justification allowed the improper deactivation of the preventive maintenance (PM) task of the test solenoid valve in 2004. Decision making by control room personnel not to strictly adhere to an Annunciator Response Procedure was a contributing cause to the reactor trip being automatic versus manual, and led to the SI.
Following the reactor trip and SI the 1 A MSIV test solenoid was replaced and check valves on the 1 A MSIV steam line were tested and replaced. The technical justifications of a sample of previously extended or deleted PMs strategies will be reviewed and corrected. The PM for the Unit 1 solenoid will be reinstated.
Procedure use and adherence standards have been reinforced with Operations personnel, simulator just-in- time training was conducted for all crews, and further causal analysis is planned to investigate operations fundamental performance gaps. This event is reportable per 10 CFR 50.73(a)(2)(iv)(A) due to actuation of the reactor protection system, Emergency Core Cooling System ( ECCS) injection into the Reactor Coolant System, and automatic actuation of the AFW system. |
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Category:Letter
MONTHYEARNL-24-0364, Notification of Deferral of Baffle Former Bolt Inspections from Farley 1R33 to 1R342024-10-31031 October 2024 Notification of Deferral of Baffle Former Bolt Inspections from Farley 1R33 to 1R34 NL-24-0392, Response to Requests for Additional Information Related to Proposed Alternative GEN-ISI-AL T-2024-0022024-10-28028 October 2024 Response to Requests for Additional Information Related to Proposed Alternative GEN-ISI-AL T-2024-002 NL-24-0396, Response to Request for Additional Information Related to Relief Request to Defer Charging Pump and Mini-Flow Isolation Valve Inservice Testing2024-10-25025 October 2024 Response to Request for Additional Information Related to Relief Request to Defer Charging Pump and Mini-Flow Isolation Valve Inservice Testing NL-24-0384, Request for Alternative RR-PR-04 for Inservice Testing of the 2A, 2B, and 2C Charging Pumps and Mini-Flow Isolation Valves2024-10-18018 October 2024 Request for Alternative RR-PR-04 for Inservice Testing of the 2A, 2B, and 2C Charging Pumps and Mini-Flow Isolation Valves NL-24-0320, License Amendment Request Proposing a New Set of Fission Gas Gap Release Fractions for High Burnup Fuel Rods That Exceed the Linear Heat Generation Rate Limit Detailed in Regulatory Guide 1.183, Table 3,.2024-09-27027 September 2024 License Amendment Request Proposing a New Set of Fission Gas Gap Release Fractions for High Burnup Fuel Rods That Exceed the Linear Heat Generation Rate Limit Detailed in Regulatory Guide 1.183, Table 3,. NL-24-0349, Units 1 and 2 - 10 CFR 26.719(c)(1) 30-Day Report Blind Performance Test Results Inconsistent with Sample Provided2024-09-20020 September 2024 Units 1 and 2 - 10 CFR 26.719(c)(1) 30-Day Report Blind Performance Test Results Inconsistent with Sample Provided NL-24-0341, Response to Request for Additional Information Related to the Application to Revise Technical Specifications Regarding Change to Containment Spray Nozzle Test Frequency2024-09-10010 September 2024 Response to Request for Additional Information Related to the Application to Revise Technical Specifications Regarding Change to Containment Spray Nozzle Test Frequency IR 05000348/20244012024-09-10010 September 2024 Security Baseline Inspection Report 05000348-2024401 and 05000364-2024401 ML24247A1102024-09-0505 September 2024 Corporate Notification Letter Aka 210-day Letter NUREG Rev 12 NL-24-0340, Unit 1 - Inservice Inspection Program Owners Activity Report (OAR-1) for Outage 1 R322024-09-0404 September 2024 Unit 1 - Inservice Inspection Program Owners Activity Report (OAR-1) for Outage 1 R32 NL-24-0259, License Amendment Request to Revise Technical Specification 3.4.14, Reactor Coolant System Pressure Isolation Valve Leakage, Surveillance Requirement 3.4.14.3 Acceptance Criteria and Miscellaneous Obsolete Changes2024-09-0404 September 2024 License Amendment Request to Revise Technical Specification 3.4.14, Reactor Coolant System Pressure Isolation Valve Leakage, Surveillance Requirement 3.4.14.3 Acceptance Criteria and Miscellaneous Obsolete Changes ML24242A1332024-08-29029 August 2024 Issuance of Amendment Nos. 250 and 247, Regarding License Amendment Request to Revise Technical Specification 3.6.5, Containment Air Temperature, Actions (EPID L-2024-LLA-0098) - Non-Proprietary ML24233A0022024-08-27027 August 2024 Request for Withholding Information from Public Disclosure for Joseph M. Farley Nuclear Plant, Units 1 and 2, License Amendment Request Supplement to Change Technical Specification 3.6.5, Containment Air Temperature Actions ML24240A0812024-08-27027 August 2024 License Amendment Request to Change Technical Specification 3.6.5, Containment Air Temperature Actions - Revised Completion Time IR 05000348/20240052024-08-26026 August 2024 Updated Inspection Plan for Joseph M. Farley Nuclear Plant, Units 1 and 2 - Report 05000348/2024005 and 05000364/2024005 IR 05000348/20244022024-08-26026 August 2024 Information Request for the Cyber Security Baseline Inspection, Notification to Perform Inspection 05000348/2024402 and 05000364/2024402 ML24226B2112024-08-22022 August 2024 Regulatory Audit Summary in Support of License Amendment Requests to Revise Technical Specification 3.6.5, Containment Air Temperature, Actions NL-24-0321, License Amendment Request to Change Technical Specification 3.6.5, Containment Air Temperature Actions - Supplemental Information2024-08-16016 August 2024 License Amendment Request to Change Technical Specification 3.6.5, Containment Air Temperature Actions - Supplemental Information IR 05000348/20240022024-08-12012 August 2024 – Integrated Inspection Report 05000348-2024002 and 05000364-2024002 and Exercise of Enforcement Discretion ML24215A3772024-08-0707 August 2024 2024 Farley Requal Inspection Corporate Notification Letter ML24201A2032024-08-0101 August 2024 Request for Withholding Information from Public Disclosure for Joseph M. Farley Nuclear Plant, Units 1 and 2, License Amendment Request to Change Technical Specification 3.6.5, Containment Air Temperature Actions ML24200A1392024-07-25025 July 2024 Regulatory Audit in Support of Review of the License Amendment Request to Revise Technical Specification 3.6.5, Containment Air Temperature ML24199A2072024-07-24024 July 2024 TS 3-6-5 LAR - Individual Notice Transmittal Letter and NSHC - Rev 1 (1) - Letter NL-24-0261, 10 CFR 50.46 ECCS Evaluation Model Annual Report for 20232024-07-19019 July 2024 10 CFR 50.46 ECCS Evaluation Model Annual Report for 2023 NL-24-0281, License Amendment Request to Change Technical Specification 3.6.5, Containment Air Temperature Actions2024-07-18018 July 2024 License Amendment Request to Change Technical Specification 3.6.5, Containment Air Temperature Actions NL-24-0227, Proposed Inservice Inspection Alternative GEN-ISI-AL T-2024-03 for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1)2024-07-0303 July 2024 Proposed Inservice Inspection Alternative GEN-ISI-AL T-2024-03 for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1) ML24184A0452024-07-0202 July 2024 Notification of Inspection and Request for Information for NRC Problem Identification and Resolution Inspection ML24178A3762024-07-0101 July 2024 Nonacceptance of Requested Licensing Action License Amendment Request to Revise Technical Specification 3.6.5, Containment Air Temperature, Using Risk-Informed Process for Evaluations NL-24-0234, Application to Revise Technical Specifications to Adopt TSTF-589, Eliminate Automatic Diesel Generator Start During Shutdown2024-06-28028 June 2024 Application to Revise Technical Specifications to Adopt TSTF-589, Eliminate Automatic Diesel Generator Start During Shutdown NL-24-0230, License Amendment Request for Adoption of Technical Specifications Task Force (TSTF) Traveler TSTF-500, Revision 2, DC Electrical Rewrite – Update to TSTF-3602024-06-28028 June 2024 License Amendment Request for Adoption of Technical Specifications Task Force (TSTF) Traveler TSTF-500, Revision 2, DC Electrical Rewrite – Update to TSTF-360 NL-24-0143, Proposed Alternative to Use ASME Code Case N-752, Risk-Informed Categorization and Treatment for Repair/ Replacement Activities in2024-06-27027 June 2024 Proposed Alternative to Use ASME Code Case N-752, Risk-Informed Categorization and Treatment for Repair/ Replacement Activities in 05000348/LER-2024-002-01, Manual Reactor Trip Due to Loss of Power to the 2A 125 Volt DC Distribution Panel2024-06-19019 June 2024 Manual Reactor Trip Due to Loss of Power to the 2A 125 Volt DC Distribution Panel NL-24-0201, Proposed Inservice Inspection Alternative GEN-ISI-ALT-2024-002 for Steam Generator Welds in Accordance with 10 CFR 50.55a(z)(1)2024-06-18018 June 2024 Proposed Inservice Inspection Alternative GEN-ISI-ALT-2024-002 for Steam Generator Welds in Accordance with 10 CFR 50.55a(z)(1) 05000348/LER-2024-001, Pressurizer Safety Valve Lift Pressure Outside of Technical Specifications Limits Due to Setpoint Drift2024-06-17017 June 2024 Pressurizer Safety Valve Lift Pressure Outside of Technical Specifications Limits Due to Setpoint Drift NL-24-0238, RIPE License Amendment Request to Change Containment Air Temperature Actions, Supplemental Information2024-06-14014 June 2024 RIPE License Amendment Request to Change Containment Air Temperature Actions, Supplemental Information NL-24-0229, Notice of Intent to Pursue Subsequent License Renewal2024-06-0707 June 2024 Notice of Intent to Pursue Subsequent License Renewal ML24149A0492024-06-0404 June 2024 SNC Fleet - Regulatory Audit in Support of Review of the License Amendment Request to Revise TS 1.1, Use and Application Definitions, and Add New Technical Specification 5.5.21 and 5.5.17, Online Monitoring Program, ML24143A0412024-05-28028 May 2024 Supplemental Information Needed for Using the Risk-Informed Process for Evaluation for the LAR to Change Technical Specification 3.6.5, Containment Air Temperature, Actions NL-24-0202, SNC Response to Regulatory Issue Summary 2024-01: Preparation and Scheduling of Operator Licensing Examinations2024-05-24024 May 2024 SNC Response to Regulatory Issue Summary 2024-01: Preparation and Scheduling of Operator Licensing Examinations NL-24-0191, Annual Radiological Environmental Operating Reports for 20232024-05-10010 May 2024 Annual Radiological Environmental Operating Reports for 2023 NL-24-0064, Units 1 & 2 and Hatch Nuclear Plant - Units 1 & 2 License Amendment Request to Revise Technical Specification 1.1 and Add Online Monitoring Program to Technical Specification 5.52024-05-0303 May 2024 Units 1 & 2 and Hatch Nuclear Plant - Units 1 & 2 License Amendment Request to Revise Technical Specification 1.1 and Add Online Monitoring Program to Technical Specification 5.5 NL-24-0188, Cycle 33 Core Operating Limits Report2024-05-0101 May 2024 Cycle 33 Core Operating Limits Report NL-24-0165, Annual Non-Radiological Environmental Operating Reports and Annual Radioactive Effluent Release Reports for 20232024-04-25025 April 2024 Annual Non-Radiological Environmental Operating Reports and Annual Radioactive Effluent Release Reports for 2023 IR 05000348/20240012024-04-24024 April 2024 Integrated Inspection Report 05000348/2024001 and 05000364/2024001 NL-24-0137, RIPE License Amendment Request to Change Containment Air Temperature Actions2024-04-19019 April 2024 RIPE License Amendment Request to Change Containment Air Temperature Actions IR 05000348/20240102024-04-16016 April 2024 NRC Inspection Report 05000348/2024010 and 05000364/2024010 05000364/LER-2024-002, For Manual Reactor Trip Due to Loss of Power to the 2A 125 Volt DC Distribution Panel2024-04-15015 April 2024 For Manual Reactor Trip Due to Loss of Power to the 2A 125 Volt DC Distribution Panel IR 05000348/20240112024-04-12012 April 2024 Fire Protection Team Inspection Report 05000348/2024011 and 05000364/2024011 NL-24-0134, Renewed National Pollutant Discharge Elimination System (NPDES) Permit2024-04-12012 April 2024 Renewed National Pollutant Discharge Elimination System (NPDES) Permit NL-24-0088, Application to Revise Technical Specifications Regarding Change to Containment Spray Nozzle Test Frequency2024-04-0505 April 2024 Application to Revise Technical Specifications Regarding Change to Containment Spray Nozzle Test Frequency 2024-09-05
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000348/LER-2024-002-01, Manual Reactor Trip Due to Loss of Power to the 2A 125 Volt DC Distribution Panel2024-06-19019 June 2024 Manual Reactor Trip Due to Loss of Power to the 2A 125 Volt DC Distribution Panel 05000348/LER-2024-001, Pressurizer Safety Valve Lift Pressure Outside of Technical Specifications Limits Due to Setpoint Drift2024-06-17017 June 2024 Pressurizer Safety Valve Lift Pressure Outside of Technical Specifications Limits Due to Setpoint Drift 05000364/LER-2024-002, For Manual Reactor Trip Due to Loss of Power to the 2A 125 Volt DC Distribution Panel2024-04-15015 April 2024 For Manual Reactor Trip Due to Loss of Power to the 2A 125 Volt DC Distribution Panel 05000364/LER-2024-001, Manual Reactor Trip Due to Rising Steam Generator Levels2024-01-11011 January 2024 Manual Reactor Trip Due to Rising Steam Generator Levels 05000348/LER-2023-003, Emergency Diesel Generator (Eog) Lube Oil Pwnp Outlet Coupling Leak2023-12-0707 December 2023 Emergency Diesel Generator (Eog) Lube Oil Pwnp Outlet Coupling Leak 05000364/LER-2023-003, Pressurizer Code Safety Valve Lift Pressure Outside of Technical Specifications Limits2023-12-0707 December 2023 Pressurizer Code Safety Valve Lift Pressure Outside of Technical Specifications Limits 05000364/LER-2023-002, Main Steam Safety Valve Lift Pressure Outside of Technical Specifications Limits Due to Setpolnt Drift2023-11-30030 November 2023 Main Steam Safety Valve Lift Pressure Outside of Technical Specifications Limits Due to Setpolnt Drift 05000348/LER-2023-002, Residual Heat Removal Pump Inoperable for Longer than Allowed by Technical Specifications2023-11-29029 November 2023 Residual Heat Removal Pump Inoperable for Longer than Allowed by Technical Specifications 05000364/LER-2023-001, Pressurizer Code Safety Valve Lift Pressure Outside of Technical Specifications Limits2023-09-28028 September 2023 Pressurizer Code Safety Valve Lift Pressure Outside of Technical Specifications Limits 05000348/LER-2023-001, Automatic Reactor Trip Due to DC Ground on Turbine Trip Solenoid2023-03-30030 March 2023 Automatic Reactor Trip Due to DC Ground on Turbine Trip Solenoid 05000348/LER-2022-001, Outdated Relay Settings Resulted in an Automatic Reactor Trip After a Floor Tile Was Dropped in High Voltage Switch House2022-09-30030 September 2022 Outdated Relay Settings Resulted in an Automatic Reactor Trip After a Floor Tile Was Dropped in High Voltage Switch House 05000364/LER-2017-0052018-01-11011 January 2018 Power Range Nuclear Instrument Inoperable Due to Poor Connection of High Voltage Cable Connector, LER 17-005-00 for Joseph M. Farley Nuclear Plant, Unit 2, Regarding Power Range Nuclear Instrument Inoperable Due to Poor Connection of High Voltage Cable Connector 05000364/LER-2017-0042017-12-22022 December 2017 I OF 3, LER 17-004-00 for Joseph M. Farley Nuclear Plant, Unit 2 Regarding Turbine-Driven Auxiliary Feedwater Pump Steam Admission Valve Air Leak Resulted in a Condition Prohibited by Technical Specifications 05000364/LER-2017-0032017-12-20020 December 2017 Pressurizer Safety Valve Lift Pressure Outside of Technical Specifications Limits, LER 17-003-00 for Joseph M. Farley, Unit 2, Regarding Pressurizer Safety Valve Lift Pressure Outside of Technical Specifications Limits 05000364/LER-2017-0022017-12-19019 December 2017 Main Steam Safety Valve Lift Pressure Outside of Technical Specifications Limits, LER 17-002-00 for Joseph M. Farley, Unit 2, Regarding Main Steam Safety Valve Lift Pressure Outside of Technical Specifications Limits 05000364/LER-2017-0012017-08-21021 August 2017 2B Emergency Diesel Generator Rendered Inoperable Due to a Jacket Water Leak without Makeup Capability, LER 17-001-00 for Farley, Unit 2, Regarding 28 Emergency Diesel Generator Rendered Inoperable Due to a Jacket Water Leak without Makeup Capability 05000348/LER-2016-0072017-06-0707 June 2017 Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters, LER 16-007-01 for Joseph M. Farley, Unit 1, Regarding Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters 05000348/LER-2016-0092017-02-0202 February 2017 Tornado Missile Vulnerabilities Result in Condition Prohibited by Technical Specifications, LER 16-009-00 for Joseph M. Farley Nuclear Plant, Units 1 and 2 Regarding Tornado Missile Vulnerabilities Result in Condition Prohibited by Technical Specifications 05000348/LER-2016-0082017-01-23023 January 2017 Manual Reactor Trip Due to Generator Voltage Swings, LER 16-008-00 for Farley, Unit 1, Regarding Manual Reactor Trip Due to Generator Voltage Swings 05000348/LER-2016-0052016-12-28028 December 2016 Toxic Gas Event, LER 16-005-00 for Joseph M. Farley Nuclear Plant, Unit 1, Regarding Toxic Gas Event 05000348/LER-2016-0042016-12-19019 December 2016 Unapproved Environmental Qualification Material Caused Inoperability of One Containment Cooling Train, LER 16-004-00 for Joseph M. Farley Nuclear Plant, Unit 1, Regarding Unapproved Environmental Qualification Material Caused lnoperability of One Containment Cooling Train 05000348/LER-2016-0062016-12-19019 December 2016 Manual Reactor Trip due to Loss of Speed Control on 1A Steam Generator Feed Pump, LER 16-006-00 for Joseph M. Farley Nuclear Plant, Unit 1 Regarding Manual Reactor Trip due to Loss of Speed Control on 1A Steam Generator Feed Pump 05000348/LER-2016-0032016-12-12012 December 2016 Pressurizer Safety Valve Setpoint Pressure Outside of Technical Specification Tolerance Band, LER 16-003-00 for Farley, Unit 1, Regarding Pressurizer Safety Valve Setpoint Pressure Outside of Technical Specification Tolerance Band 05000348/LER-2016-0022016-11-30030 November 2016 Automatic Reactor Trip and Safety Injection Due to Closure of Main Steam Isolation Valve, LER 16-002-00 for Joseph M. Farley Nuclear Plant, Unit 1 Regarding Automatic Reactor Trip and Safety Injection Due to Closure of Main Steam Isolation Valve 05000348/LER-2016-0012016-06-0909 June 2016 Condition Prohibited by Technical Specifications Due to 600V Load Center Inoperable Longer than Allowed by Technical Specifications, LER 16-001-00 for Farley, Unit 1, Regarding Condition Prohibited by Technical Specifications Due to 600V Load Center Inoperable Longer than Allowed by Technical Specifications 05000364/LER-2015-0012016-01-13013 January 2016 Turbine Driven Auxiliary Feedwater Pump in a Condition Prohibited by Technical Specifications due ,to a Design Issue, LER 15-001-01 for Farley, Unit 2, Regarding Turbine Driven Auxiliary Feedwater Pump in a Condition Prohibited by Technical Specifications Due to a Design Issue NL-13-1525, Special Report 13-001-00 for Joseph M. Farley, Unit 2, Regarding Nonfunctional Radiation Monitor R-60B2013-07-26026 July 2013 Special Report 13-001-00 for Joseph M. Farley, Unit 2, Regarding Nonfunctional Radiation Monitor R-60B NL-11-2445, LER 11-S01-00 for Joseph M. Farley, Unit 1 Regarding Loss of Power to Security Systems2012-01-0909 January 2012 LER 11-S01-00 for Joseph M. Farley, Unit 1 Regarding Loss of Power to Security Systems NL-08-0756, Special Report 2008-002-00, Inoperable Radiation Monitor R-60B2008-05-0909 May 2008 Special Report 2008-002-00, Inoperable Radiation Monitor R-60B NL-08-0659, Special Report 2008-001-00, Inoperable Radiation Monitor R-29B2008-04-25025 April 2008 Special Report 2008-001-00, Inoperable Radiation Monitor R-29B NL-05-2234, Special Report No. 2005-001-00 for Joseph M. Farley Nuclear Plant - Unit 1 Re Inoperable Radiation Monitor R-60B2005-12-0606 December 2005 Special Report No. 2005-001-00 for Joseph M. Farley Nuclear Plant - Unit 1 Re Inoperable Radiation Monitor R-60B 2024-06-19
[Table view] |
Reported lessons learned are incorporated into the licensing process and fed back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Joseph M. Farley Nuclear Plant, Unit 1 05000- 348
A. PLANT AND SYSTEM IDENTIFICATION
Westinghouse - Pressurized Water Reactor
B. DESCRIPTION OF EVENT
On 10/1/2016 at 0512 CDT with Unit 1 at 99 percent power and coasting down in power for a planned refueling outage, the Control Room received dual indication for the 1 A Steam Generator (SG) Main Steam Isolation Valve (MSIV), a closed indication for the 1A MSIV test switch, and a Main Control Board (MCB) annunciator for main steam line isolation valve air pressure being low. Operations personnel implemented the Annunciator Response Procedure (ARP) for this annunciator and followed the first step, which was to attempt to recharge the accumulator by placing the switch for the 1 A MSIV to the 'open' position. Although the second step directed tripping the reactor if the alarm was in and dual indication was indicated, Operations instead dispatched licensed and non-licensed personnel into the plant to investigate the cause for the alarm. The normally closed test solenoid vent port was found to be releasing air. Operations initiated steps to isolate the leaking test solenoid valve; however, the leaking solenoid and check valves caused air pressure in the 1 A MSIV actuator to fall low enough to cause inadvertent 1 A MSIV closure. Actuation of the 1A MSIV turbine trip limit switch initiated a turbine trip and subsequent reactor trip.
The closure of the 1A MSIV caused a rapid pressure reduction in the remaining two Steam Generators' steam lines and resulted in actuation of a Safety Injection (SI). The Emergency Core Cooling System (ECCS) actuated and injected into the Reactor Coolant System (RCS). Auxiliary Feedwater (AFW) auto-started. All Control rods fully inserted and all equipment actuated as designed. The unit was stabilized in Mode 3 with decay heat removed through the condenser.
The test solenoid had last been replaced in 2003. The Preventive Maintenance (PM) task for this component was improperly deactivated in 2004 due to inadequate technical justification.
Decision making by control room personnel not to strictly adhere to the ARP was a contributing cause to the reactor trip being automatic versus manual, and led to the SI. Manual actuation of a reactor trip prior to the closure of the 1 A MSIV would have prevented the SI from occurring.
C. UNIT STATUS AT TIME OF EVENT
Unit 1, Mode 1, 99 percent power Unit 2, Mode 1, 100 percent power
D. CAUSE OF EVENT
The 1 A MSIV closure was caused by failure of its test solenoid in conjunction with other air system leakage, which vented the air pressure from the 1A MSIV actuator. An inadequate technical justification allowed the improper deactivation of the PM task of the test solenoid valve in 2004 and led to the component failure. Decision making by control room personnel not to strictly adhere to the ARP was a contributing cause to the reactor trip being automatic versus manual, and led to the SI.
Reported lessons learned are incorporated into the licensing process and ted back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer. Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office .of Manatiement and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Joseph M. Farley Nuclear Plant, Unit 1 05000- 348 2016 - 002 - 00
E. REPORTABILITY ANALYSIS AND SAFETY ASSESSMENT
This event is reportable per 10 CFR 50.73(a)(2)(iv)(A) due to actuation of the reactor protection system, actuation and injection of ECCS into the RCS, and automatic actuation of the AFW system.
The 1A MSIV closing caused steam flow in steam line A to decrease, and steam flow increased and steam pressure decreased in steam lines B and C. The rate of steam pressure decrease in steam lines B and C resulted in the initiation of the safety injection signal. All systems responded as required, including all control rods fully inserting into the core, AFW system auto-starting to supply the Steam Generators, and decay heat removal occurring through the condenser. This system response to the event was as designed for turbine trip, reactor trip, and SI actuation.
Because all systems responded as required and there were no actual adverse effects on the health and safety of the public, the safety significance of this event is considered very low.
F. CORRECTIVE ACTION
The 1A MSIV test solenoid was replaced. In addition, all of the test solenoids for all Unit 1 MSIVs were solenoid will be reinstated. The technical justifications of a sample of previously extended or deleted PM strategies will be reviewed and corrected. Prior to Unit 1 entering Mode 3 all Unit 1 MSIV test solenoid isolation valves were closed to prevent a loss of air through the test portion of the lines.
The Unit 2 main steam system was walked down for similar issues, and needed test solenoid replacements will be completed by the end of the next refueling outage. In addition, the Unit 2 MSIV test solenoid isolation valves were closed to prevent a loss of air through the test portion of the lines.
Procedure use and adherence standards have been reinforced with Operations personnel, simulator just- in-time training was conducted for all crews, and further causal analysis is planned to investigate operations fundamental performance gaps.
G. ADDITIONAL INFORMATION
1) Failed Components: Loop A test solenoid valve for the 1A MSIV 2) Previous Similar Events: None 3) Other system affected: None 4) Commitment Information: None 5) Energy Industry Identification System Code:
[JC]- Reactor Protection System [BA] -Auxiliary Feedwater [SB] - Main Steam System
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05000364/LER-2016-001 | Manual Reactor Trip due to High Steam Generator Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000348/LER-2016-001 | Condition Prohibited by Technical Specifications Due to 600V Load Center Inoperable Longer than Allowed by Technical Specifications LER 16-001-00 for Farley, Unit 1, Regarding Condition Prohibited by Technical Specifications Due to 600V Load Center Inoperable Longer than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2016-002 | Automatic Reactor Trip and Safety Injection Due to Closure of Main Steam Isolation Valve LER 16-002-00 for Joseph M. Farley Nuclear Plant, Unit 1 Regarding Automatic Reactor Trip and Safety Injection Due to Closure of Main Steam Isolation Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000348/LER-2016-003 | Pressurizer Safety Valve Setpoint Pressure Outside of Technical Specification Tolerance Band LER 16-003-00 for Farley, Unit 1, Regarding Pressurizer Safety Valve Setpoint Pressure Outside of Technical Specification Tolerance Band | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2016-004 | Unapproved Environmental Qualification Material Caused Inoperability of One Containment Cooling Train LER 16-004-00 for Joseph M. Farley Nuclear Plant, Unit 1, Regarding Unapproved Environmental Qualification Material Caused lnoperability of One Containment Cooling Train | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2016-005 | Toxic Gas Event LER 16-005-00 for Joseph M. Farley Nuclear Plant, Unit 1, Regarding Toxic Gas Event | 10 CFR 50.73(a)(2)(x) | 05000348/LER-2016-006 | Manual Reactor Trip due to Loss of Speed Control on 1A Steam Generator Feed Pump LER 16-006-00 for Joseph M. Farley Nuclear Plant, Unit 1 Regarding Manual Reactor Trip due to Loss of Speed Control on 1A Steam Generator Feed Pump | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000348/LER-2016-007 | Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters LER 16-007-01 for Joseph M. Farley, Unit 1, Regarding Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000348/LER-2016-008 | Manual Reactor Trip Due to Generator Voltage Swings LER 16-008-00 for Farley, Unit 1, Regarding Manual Reactor Trip Due to Generator Voltage Swings | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000348/LER-2016-009 | Tornado Missile Vulnerabilities Result in Condition Prohibited by Technical Specifications LER 16-009-00 for Joseph M. Farley Nuclear Plant, Units 1 and 2 Regarding Tornado Missile Vulnerabilities Result in Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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