05000302/LER-1983-053, Updated LER 83-053/03L-1:on 831109,safety-related Hydraulic Snubber MSH-252 Declared Inoperable When Lack of Oil Level Indication Noted in Sightglass.Caused by Loose jam-nut on Stationary End of Snubber,Allowing rotation.W/8401

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Updated LER 83-053/03L-1:on 831109,safety-related Hydraulic Snubber MSH-252 Declared Inoperable When Lack of Oil Level Indication Noted in Sightglass.Caused by Loose jam-nut on Stationary End of Snubber,Allowing rotation.W/840106 Ltr
ML20086G815
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 01/06/1984
From: Bufe J, Westafer G
FLORIDA POWER CORP.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
3F0184-07, 3F184-7, LER-83-053-03L, LER-83-53-3L, NUDOCS 8401120414
Download: ML20086G815 (3)


LER-2083-053, Updated LER 83-053/03L-1:on 831109,safety-related Hydraulic Snubber MSH-252 Declared Inoperable When Lack of Oil Level Indication Noted in Sightglass.Caused by Loose jam-nut on Stationary End of Snubber,Allowing rotation.W/840106 Ltr
Event date:
Report date:
3022083053R00 - NRC Website

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" Update Report - Previous Report Date December 12, 1983"

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" Update Report '- Previous Report Date December 22, 1983" SUPPLEMENTARY INFORMATION

. REPORT NO : 50-302/83-053/03L-1 FACILITY: Crystal River Unit 3 REPORT DATE: . January 6,1984 ,

DATE OF OCCURRENCE: November 9,1983 IDENTIFICATION OF OCCURRENCE:

' One ' safety-related hydraulle snubber, MSH-252, was inoperable on November 9, 1983, contrary to Technical Specification 3.7.9.1.

CONDITIONS PRIOR TO OCCURRENCE:

Mode 1,97% FP DESCRIPTION OF OCCURRENCE:

On November 9,1983, during routine visual inspection, the sightglass for snubber MSH-252 (Main Steam System) indicated no oil level. It was also observed that the snubber had rotated to another position. The snubber MSH-252, was declared inoperable at 1400 and maintenance was initiated.

ANALYSIS OF OCCURRENCE:

There was.no significant effect on public health and safety as a result of this

i. . occurrence since the probability of seismic events in the peninsula'of Florida is
. very low and considerable safety margin is maintained in piping stress analyses.

DESIGNATION OF APPARENT CAUSE:

This event was caused by a loose jam-nut on the stationary end of the snubber which allowed the snubber to rotate. As the snubber rotated, the fluid drained out.

. CORRECTIVE ACTION:

! MSH-232 was replaced with a spare snubber. Operability was restored on l November 10,1983 at 1800.

' Procedure MP-130, Pipe Snubber Maintenance, will be revised to ensure proper snubber orientation is maintained.

' FAILURE DATA:

This is the ninth occurrence reported under Technical Specification 3.7.9.1.

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,o January 6,1984 3F0184-07 Mr. James P. O'Reilly Regional Administrator, Region II Office of Inspection & Enforcement U.S. Nuclear Regulatory Commission ,

101 Marietta Street N.W., Suite 2900 Atlanta, GA 30303

Subject:

Crystal River Unit 3 Docket No. 50-302 Operating License No. DPR-72.

Licensee Event Report No.83-053, Revision 1 .

Dear Mr. O'Reilly:

Enclosed is Licensee Event Report No.83-053, Revision 1, and the attached supplementary information sheet, which are submitted in accordance with Technical Specification 6.9.1.9(b). This change corrects a typographical error in the component manufacturer code.

Should there be any questions, please contact this office.

Sincerely, o

G.R. Westafer Manager Nuclear Operations Licensing and Fuel Management DVH/feb Enclosure cc: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555

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}YII G ENERAL OFFICE 3201 Thirty fourth street south e P.O. Box 14042, St. Petersburg, Florida 33733 e 813-866-5151