01-14-2005 | 465D, the first-off low side root isolation valve for the Point Beach Nuclear Plant Unit 2 "A" steam generator steam line flow transmitter. The leak location could not be isolated from the main steam line. The affected portion of the main steam line is credited as a closed system boundary for containment penetration P-1, the "A" main steam line penetration. Accordingly, Technical Specification (TS) Condition 3.6.3.C, which is applicable to penetration flow paths with only one containment isolation valve and a closed system, was entered and Required Action C.1 was initiated. The required action for this condition is to isolate the affected penetration flow path with a completion time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The repair of the leak would require a shutdown and cooldown of Unit 2 and could not be accomplished within that 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> time frame; therefore, a reactor shutdown and cooldown was promptly initiated. This was considered to be a TS required shutdown and was reported in accordance with 10 CFR 50.72.(b)(2)(i). Unit 2 entered Mode 5 on November 21, 2004, and the valve body leak was repaired. Unit 2 returned to full power operation on November 25, 2004. The cause of the leak was determined to be either a material defect in the valve body or an improper welding process, which provided a stress riser that failed due to cyclic loading. An assessment of the safety significance of this event concluded that the impact of this event on the health and safety of the public was not significant. |
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FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Event Description: On November 19, 2004, the Point Beach Nuclear Plant (PBNP), Unit 2, was operating at full power. A Unit 2 containment [EIIS System Code: NH] entry was conducted on that date by Nuclear Management Company, LLC (NMC) personnel. The purpose of that entry was to inspect the unit in an attempt to identify the source of a suspected secondary system steam leak inside the containment. The possibility of a fluid leak in containment had been initially detected earlier in October 2004, based on having to pump the Unit 2 containment "A" sump [EllS Component Code: DRN] (volume of approximately 44 gallons) as often as once per day (CAP 60247). A sample of the sump on October 27, 2004, indicated that the leakage did not appear to be primary coolant, service water, or component cooling water, but was consistent with condensation. An earlier containment entry on November 8, 2004, was not successful in identifying the source of the leakage.
During the containment inspection on November 19, 2004, operations personnel located a source of sump "A" leakage when a pinhole leak was found on the body of valve 2MS-465D [EIIS "A" steam generator [EIIS Component Code: SG] steam line flow transmitter [EIIS Component Code: FT], 2FT-465. The inspection also revealed a packing leak on valve 2MS-465B, which is the second-off high side root isolation of 2FT-465.
Due to the leak location on the valve body of 2MS-465D, NMC determined that the leakage could not be isolated from the "A" steam generator main steam [EIIS System Code: SB] line. For containment isolation considerations, the main steam system is considered to be a closed system inside containment. Since the leak could not be isolated from the containment penetration [EIIS Component Code: PEN] for the "A" main steam line, the main steam system inside containment was no longer considered to be a closed system and was declared out of service at 15:44 (all times are CST) on November 19, 2004.
Technical Specification LCO 3.6.3 states that "Each containment isolation valve shall be operable." The modes of applicability for this LCO are 1 through 4. Technical Specification Action Condition (TSAC) 3.6.3.0 is specifically applicable to penetration flow paths having only one containment isolation valves and a closed system. TSAC 3.6.3.0 was entered for "One or more penetration flow paths with one containment isolation valve inoperable". Since the Unit 2 "A" main steam line inside containment was declared out of service and was no longer considered to be a closed system, Required Action C.1 was applicable. This action directs that the affected penetration flow path be isolated with a completion time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Since the repair or replacement of the 2MS-465D valve would require a shutdown and cooldown of PBNP Unit 2, NMC concluded that the 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> completion time for required action 3.6.3.C.1 could not be met.
TSAC 3.6.3.D would then be applicable and directs that the unit be shut down to Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 5 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> of the 72-hour completion time of required action 3.6.3.C.1.
FACILITY NAME (1)� DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) At 16:22, a Unit 2 load reduction was initiated in accordance with plant procedures from power operations to hot standby. This normal reactor shutdown was considered to be a Technical Specification required shutdown. At 18:01 a four-hour Emergency Notification System report was made to the NRC in accordance with 10 CFR 50.72(b)(2)(i) (EN 41212). The NRC senior resident inspector had been notified at 15:54 on November 19, 2004, of the planned shutdown.
The shutdown was completed with no significant problems noted. Unit 2 entered Mode 3 at 21:10 on November 19, 2004, and Mode 5 at 09:22 on November 21, 2004.
Following the repair of valve 2MS-465D (See discussion under Corrective Action) Unit 2 was returned to service. Unit 2 entered Mode 1 at 09:07 on November 24, 2004, and full power was achieved for Unit 2 at 07:00 on November 25, 2004.
Safety Significance:
An assessment of the safety significance for the containment pressure boundary leak was performed shortly after identification of the steam leak on 2MS-465D. Prior to discovery of the steam leak, the containment sump "A", which has a volume of about 40 gallons, was being pumped less than once per day. Assuming that the condensation in the sump was coming from the steam leak alone, the leakage from the valve body hole was assumed to be bounded by approximately 40 gallons of water per day. Using a factor of 1,000 to account for the steam volume being added to containment (1,000:1 expansion ratio for water boiling at atmospheric pressure), this equates to approximately.40,000 gallons per day of steam leakage or about 5,350 cubic feet per day. This leakage was occurring with a differential pressure of approximately 800 psid.
Under accident conditions, the design pressure of the containment building (60 psid) is not exceeded in a loss of coolant accident (LOCA), and therefore presents an upper limit on the potential leakage through the closed system containment boundary into the main steam system.
To adjust the flow rate for comparing this lower differential pressure to the higher differential pressure of the observed leakage, the square-root relationship was used to give an adjustment factor of 0.274. Multiplying the leakage by this factor gives an estimated potential steam leakage through the closed system inside containment boundary following a design basis accident of 1,460 cubic feet per day.
Using the containment net free volume 970,000 cubic feet, the estimated leakage would equate to 0.15%/day containment leakage. This is less than the FSAR containment design limit of 0.4%/day and our currently committed administrative limit of 0.2%/day. Based on this assessment, the leakage through the valve wall was bounded by the existing accident analyses.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) POINT BEACH NUCLEAR PLANT UNIT 2 05000301 YEAR I� SEQUENTIAL� INUMBER Under a LOCA scenario, the steam generators remain at a much higher pressure than the containment pressure until well into the event. Therefore, leakage from containment out into the main steam (MS) system would be significantly delayed and not occur at the onset of the accident.
Additionally, the MS system is not directly vented to the environment at that point in the accident scenario. Any steam releases at that time would be via steam dumps or safety valves. Steam dumps and safety valves are not effective or used with steam pressures below 60 psig, and residual heat removal [ENS System Code: BP] is used to remove decay heat at these low pressures (even in the event of a LOCA). In aggregate, the increase in risk of a radiological release due to the leak was deemed minimal. Accordingly, the potential impact of this event on the health and safety of the public and the plant staff was considered to be insignificant.
NMC further concludes that the through-wall steam leak, which prompted this Technical Specification required shutdown, did not constitute a loss of any system, structure or component safety function; therefore, the degradation of this containment closed system boundary did not constitute a safety system functional failure.
Cause:
A review of the component history of the valve revealed that the instrumentation line off the main steam header including the two isolation valves and condensing pot had previously been identified as a location of vibration (CR 97-2440). This main steam flow instrument line was not supported as were all other similar main steam flow indication lines. An evaluation of the vibration had been performed and the fatigue stress determined to be acceptable. Although fatigue failure was initially suspected, the defect on 2MS-465D valve was in the valve body in the heat affected zone of the weld. A dye penetrant test (PT) revealed a horse-shoe shaped indication in the valve body at the socket weld location suggesting that this failure was the result of a manufacturing defect in the valve body and not a fatigue failure. Excavation of the indication during repair resulted in removal of the weld and valve body in the socket location down to the pipe material. After the horse-shoe shaped indication was removed, another PT exam did not reveal any additional circumferential cracking, which would be expected if fatigue was the mode of failure. The horse shoe shape of the PT examinations indicates the existence of a possible stress riser due to a material defect either from the valve body or the welding process used during original installation.
The manufacturing defect was likely opened by the stress of repeated transients. Had the defect not been present, a failure would not be expected. Because of the repair technique used, destructive testing and material examination for further analysis of the failure was not possible.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Corrective Action:
Repairs were made to the affected area by excavation and welding the affected area. PT examinations of the surface were conducted during the grinding to ensure that the flaw had been completely removed. The affected area was then repaired by laying in new weld material. A PT of the final weld was performed and documented as satisfactory. A final successful leak check of the weld was completed with the unit at normal operating temperature and pressure. The packing leak on valve 2MS-465B was also corrected.
The other accessible welds on the main steam header instrumentation lines for Unit 2 were PT examined. No other weld defects were noted. In addition, all the welds on the 2FT-465 instrumentation line were examined with no additional indication identified. NMC is also evaluating a modification to provide a support for the existing condensing pot similar to the supports provided on the other main steam flow instrument lines.
Previous Similar Events:
A review of recent LERs (past three years) identified two events which involved a reactor shutdown required by the Technical Specifications and one event involving a defect in a pressure boundary:
LER NUMBER Title 301/2002-001-00 Completion of Unit 2 Shutdown Required by TS LCO 3.5.2 Action B.1 301/2003-002-00 Reactor Shutdown Required Due To Technical Specification TSAC 3.1.6.B.2 Not Met 266/2004-001-00 Reactor Vessel Upper Head CRDM Penetration 26 Flaw Indications
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05000348/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2004-001 | Inadvertent Actuation of ECCS and EDGs While in Refueling Mode | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2004-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2004-001 | Failure To Comply With Technical Specification 3 .7 .5 .1, Control Room Emergency Ventilation System | | 05000301/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000313/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000285/LER-2004-001 | Failure To Perform A Leakage Test Due To Lack Of Understanding of Penetration Design | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000271/LER-2004-001 | Main Steam Isolation Valve Leakage Exceeds a Technical Specification Leakage Rate Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2004-001 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000318/LER-2004-001 | . Reactor Trip Due to Low Steam Generator Water Level After Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000289/LER-2004-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-001 | | | 05000247/LER-2004-001 | Manual Reactor Trip Due to Oscillating Feedwater Flow and Steam Generator Level with Flow Perturbations Caused by a Degraded Feed Water Regulating Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000244/LER-2004-001 | Gaps in the Control Room Emergency Zone Boundary | | 05000255/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000461/LER-2004-001 | Clinton Power Station 05000461 1 OF 4 | | 05000414/LER-2004-001 | relPowere Vice President A Duke Energy Company Duke Power Catawba Nuclear Station 4800 Concord Rd. / CNO1VP York, SC 29745-9635 803 831 4251 803 831 3221 fax November 9, 2004
U. S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, DC 20555-0001
SUBJECT: Duke Energy Corporation
Catawba Nuclear Station Unit 2
Docket No. 50-414
Licensee Event Report 414/04-001 Revision 0
Reactor Coolant System Pressure Boundary Leakage
Due to Small Cracks Found in Steam Generator
Channel Head Bowl Drain Line on 2C & 2D Steam
Generators
Attached please find Licensee Event Report 414/04-001
Revision 0, entitled "Reactor Coolant System Pressure
Boundary Leakage Due to Small Cracks Found in.Steam
Generator Channel Head Bowl Drain Line on 2C & 2D Steam
Generators."
This Licensee Event Report does not contain any regulatory
commitments. Questions regarding this Licensee Event Report
should be directed to R. D. Hart at (803) 831-3622.
Sincerely,
Dhiaa Jamil
Attachment
www.dukepower.corn 00- U.S. Nuclear Reguldhory Commission
November 9, 2004
Page 2
XC: W.D. Travers
U.S. Nuclear Regulatory Commission
Regional Administrator, Region II
Atlanta Federal Center
61 Forsyth St., SW, Suite 23T85
Atlanta, GA 30303
E.F. Guthrie
Senior Resident Inspector (CNS)
U.S. Nuclear Regulatory Commission
Catawba Nuclear Station
S.E. Peters (addressee only)
NRC Project Manager (CNS)
U.S. Nuclear Regulatory Commission
One White Flint North, Mail Stop 10-B3
11555 Rockville Pike
Rockville, MD 20852-2738
NRC FORM 366� U.S. NUCLEAR REGULATORY APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004)� COMMISSION Estimated burden per response to comply with this mandatory collection request 50
hours. Reported lessons learned are Incorporated Into the licensing process and fed back
to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy
Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, WashinMon, DC 2055
LICENSEE EN/ENT REPORT (LER) 0001, or by Internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104). Office of Management(See reverse for required number of and Budget, Washington, DC 20503. If a means used to impose an Information col ectiond( inverse �for each block) does not display a currently valid OMB control number, the NRC may not conduct or sponsor. and a person Is not required to respond o. the Information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 050- 00414 1 OF�6 4. TITLE Reactor Coolant System Pressure Boundary Leakage Due to Small Cracks Found in
Steam Generator Channel Head Bowl Drain Line on 2C & 2D Steam Generators | | 05000368/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2004-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2004-001 | Gas Accumulation in Centrifugal Charging Pump Suction Piping | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000395/LER-2004-001 | Reactor Trip Due to Valve Failure During Forced Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000390/LER-2004-001 | Automatic Reactor Trip Due to a Invalid Turbine Trip Signal (P-4) | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2004-001 | Auxiliary Feedwater System in prohibited condition due to inadequate procedure. | | 05000454/LER-2004-001 | Exelent
Exelon Generation Company, LLCRwww.exeloncorp.com NuclearByron Station 4450 North German Church Road Byron, IL 61010-9794 October 17, 2004 LTR: BYRON 2004-0111 File: 2.01.0700 United States Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Subject:RLicensee Event Report (LER) 454-2004-001-00, "Reactor Containment Fan Coolers Flow Rates Below Technical Specification Requirements Due to Inaccurate Flow Indication" Byron Station, Unit 1
Facility Operating License No. NPF-37
NRC Docket No. STN 50-454
Enclosed is an LER involving the August 17, 2004, event involving low flow conditions discovered in Unit 1 Reactor Containment Fan Coolers for a time period longer than allowed by the Technical Specifications. This event is reportable to the NRC in accordance with 10CFR 50.73 (a)(2)(i)(B), as a condition prohibited by Technical Specifications. Should you have any questions concerning this matter, please contact Mr. William Grundmann, Regulatory Assurance. Manager, at (815) 234-5441, extension 2800. Respectfully, Stephen E. Kuczynski Site Vice President Byron Nuclear Generating Station Attachment LER 454-2004-001-00 cc:RRegional Administrator, Region III, NRC NRC Senior Resident Inspector— Byron Station NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7.2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T.6 E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail toLICENSEE EVENT REPORT (LER) *I@ nrc.gov, and to the Desk Officer, Office of Informabon and Regulatory Affairs, NEOB:10202 (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose information collection does not display a currently valid OMB control number, the NRC may not _ conduct or sponsor, and a person is not required to respond to, the information collection. 1 rand ITV NAUP o natuerr An warn q par= . Byron Station, Unit 1 0500454 1 OF 5 4. Reactor Containment Fan Coolers Flow Rates Below Technical Specifications Requirements Due to Inaccurate Flow Indication | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2004-001 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000336/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2004-002 | Dresden Nuclear Power Station Unit 2 05000237 1 of 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000244/LER-2004-002 | Consolidated Rod Storage Canister Placed in Incorrect Storage Location | | 05000530/LER-2004-002 | Main Turbine Control System Malfunction Results in Automatic Reactor Trip on Low DNBR | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000305/LER-2004-002 | | | 05000247/LER-2004-002 | Manual Reactor Trip Due to Decreasing 23 Steam Generator Level Caused by Feedwater Regulating Valve Closure Due to a De-energized Solenoid Operated Valve from Wiring Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000414/LER-2004-002 | Manual Reactor Trip Initiated Due to Control Rods from Shutdown Bank D Dropping into the Core | | 05000251/LER-2004-002 | AAA | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv)(b) | 05000397/LER-2004-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000346/LER-2004-002 | Reactor Trip During Reactor Trip Breaker Testing Due To Fuse Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2004-002 | Emergency Diesel Generator Start and Load Due to Momentary Fault on Incoming Feed | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000269/LER-2004-002 | eif Powere RON A. JONES Vice President A Duke Energy Company Oconee Nuclear Site Duke Power ONO1VP / 7800 Rochester Highway Seneca, SC 29672 864 885 3158 864 885 3564 fax September 9, 2004
U.S. Nuclear Regulatory Commission
Document Control Desk
Washington, D.C. 20555
Subject: Oconee Nuclear Station
Docket Nos. 50-269,-270, -287
Licensee Event Report 269/2004-02, Revision 1
Problem Investigation Process No.: 0-04-2808
Gentlemen:
Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached
is Licensee Event Report 269/2004-02, Revision 1, regarding
a Main Steam Line Break mitigation design/analysis
deficiency which could result in the main and startup
feedwater control valves being technically inoperable for
mitigation of some steam line break scenarios.
This report is being submitted to supplement Revision 0
submitted July 6, 2004. At that time the root cause
investigation and an analysis of the consequences of
potentially exceeding the Environment Qualification (EQ)
envelope curve were still in progress.
This event is being reported in accordance with 10 CFR
50.73 (a)(2)(i)(B) as a condition prohibited by Technical
Specifications, 50.73(a)(2)(ii)(B) as an Unanalyzed
Condition, and 50.73(a)(2)(V)(D) as a potential loss of
safety function for Accident Mitigation. This event is
considered to be of no significance with respect to the
health and safety of the public.
www.dukepower.corn Document Control Desk
Date: September 9, 2004
Page 2
Attachment: Licensee Event Report 269/2004-02, Revision 1
cc: Mr. William D. Travers
Administrator, Region II
U.S. Nuclear Regulatory Commission
61 Forsyth Street, S. W., Suite 23T85
Atlanta, GA 30303
Mr. L. N. Olshan
Project Manager
U.S. Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Washington, D.C. 20555
Mr. M. C. Shannon
NRC Senior Resident Inspector
Oconee Nuclear Station
INPO (via E-mail)
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7-2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T-6 E6), U.S. Nuclear Regulatory Commission, Washington. DCLICENSEE EVENT REPORT (LER) 20555-0001, or by Internet e-mail to bpi @nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management and(See reverse for required number of Budget, Washington, DC 20503. If a means used to impose information collection doesdigits/characters for each block) not display a currently valid OMB control number, the NRC may not conduct or sponsor, and,1 nnmnn lc not rent Owl to tocnnni-I to the intnrmatinn rntlentinn 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Oconee Nuclear Station, Unit 1 050-81 OF 0269 11 4. TITLE Main Steam Line Break Mitigation Design/Analysis Deficiency | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000313/LER-2004-002 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000271/LER-2004-002 | Special Nuclear Material Inventory Location Discrepancy | | 05000285/LER-2004-002 | Inoperable Diesel Generator for 28 Days Due to Blown Fuse During Shutdown | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2004-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000311/LER-2004-002 | Failure To Comply With Technical Specifications During Reactor Protection Instrument Calibration . | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2004-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-002 | | | 05000302/LER-2004-002 | Emergency Diesel Generator Inoperable Due To Fuel Oil Header Outlet Check Valve Leaking Past Seat | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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