05000285/LER-2013-013, Unqualified Components Used in Safety System Control Circuit

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Unqualified Components Used in Safety System Control Circuit
ML13337A451
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 12/02/2013
From: Cortopassi L
Omaha Public Power District
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LIC-13-0176 LER 13-013-00
Download: ML13337A451 (14)


LER-2013-013, Unqualified Components Used in Safety System Control Circuit
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function
2852013013R00 - NRC Website

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jjjjjjjj Omaha Public Power 0/slrlcl 444 South I rJh Street Mall Omaha, NE 68102-2247 LIC-13-0176 December 2, 2013 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001

Reference:

Docket No. 50-285

Subject:

Licensee Event Report 2013-013, Revision 0, for the Fort Calhoun Station Please find attached Licensee Event Report 2013-013, Revision 0. This report is being submitted pursuant to 10 CFR 50.73(a)(2)(i)(B). There are no new commitments being made in this letter.

If you should have any questions, please contact Terrence W. Simpkin, Manager, Site Regulatory Assurance, at (402) 533-6263.

Louis P. Cortopassi Site Vice President and CNO LPC/rjr Attachment c:

M. L. Dapas, NRC Regional Administrator, Region IV J. M. Sebrosky, NRC Senior Project Manager J. C. Kirkland, NRC Senior Resident Inspector L. E. Wilkins, NRC Project Manager Employment with Equal Opportunity

NRC FORM 366 (10-2010)

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (10-2010)

LICENSEE EVENT REPORT (LER)

(See reverse for required number of digits/characters for each block)

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

1. FACILITY NAME Fort Calhoun Station
2. DOCKET NUMBER 05000285
3. PAGE 1 OF 3
4. TITLE Unqualified Components used in Safety System Control Circuit
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL NUMBER REV NO.

MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 05000 10 18 2012 2013 013 -

0 12 2

2013 FACILITY NAME DOCKET NUMBER 05000

9. OPERATING MODE 5
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 20.2201(b) 20.2203(a)(3)(i) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii) 20.2201(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(2)(i) 50.36(c)(1)(i)(A) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A) 20.2203(a)(2)(ii) 50.36(c)(1)(ii)(A) 50.73(a)(2)(iv)(A) 50.73(a)(2)(x) 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(v)(A) 73.71(a)(4) 20.2203(a)(2)(iv) 50.46(a)(3)(ii) 50.73(a)(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(C)

OTHER 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(v)(D)

Specify in Abstract below or in LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET SAFETY SYSTEM FUNCTIONAL FAILURE This does not represent a safety system functional failure in accordance with NEI 99-02, Revision 6.

PREVIOUS EVENTS Engineering is reviewing this condition and the results of this review will be used to update this report.