05000285/LER-1997-001, :on 970122,main Steam Outside of Design Basis Occurred Due to an Error in Safety Valve Analysis.Guidance Has Been Provided to Operating Staff to Ensure That Design Basis Maintained

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:on 970122,main Steam Outside of Design Basis Occurred Due to an Error in Safety Valve Analysis.Guidance Has Been Provided to Operating Staff to Ensure That Design Basis Maintained
ML20134Q280
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 02/21/1997
From: Gambhir S, Robert Lewis
OMAHA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-97-001, LER-97-1, LIC-97-0022, LIC-97-22, NUDOCS 9702260367
Download: ML20134Q280 (6)


LER-1997-001, on 970122,main Steam Outside of Design Basis Occurred Due to an Error in Safety Valve Analysis.Guidance Has Been Provided to Operating Staff to Ensure That Design Basis Maintained
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(ii)

10 CFR 50.73(a)(2)(iv), System Actuation

10 CFR 50.73(a)(2)(v), Loss of Safety Function
2851997001R00 - NRC Website

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Omaha PublicPowerDistrict

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444 Soutt; 16th StreetMall Omaha NE68102-2247 February 21, 1997 LIC-97-0022 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Station P1-137 Washington, DC 20555 Reference: Docket No. 50-285

Subject:

Licensee Event Report 97-001 Revision 0 for the Fort Calhoun Station j

Please find attached Licensee Event Report 97-001 Revision 0 dated February 21, 1997. This report is being submitted pursuant to 10 CFR 50.73(a)(2)(ii)(B). If you should have any questions, please contact me.

Sincerely,

)} Y S. K. Gambhir Division Manager Engineering & Operations Support EPM / epm t

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Winston and Strawn L. J. Callan, NRC Regional Administrator, Region IV L. R. Wharton, NRC Project Manager W. C. Walker, NRC Senior Resident Inspector INP0 Records Center 9702260367 970221 PDR ADOCK 05000285 S

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1 NRC FOR2 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED (sY OMB NO. 3150-0104 (4M 3

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Fort Calhoun Station Unit No.1 05000285 10F 5 s

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Main Steam Outside of Design Basis Due to an Error in Safety Valve Analysis I

f EVENT DATE(5)

LER NUMBER (6)

REPORT DATE(7)

OTHEl(FACILITIES INVOLWD(8) sE FACluTY NAME DOcKE1 #duteER MONTH DAY YEAR YEAR MONTH DAY YEAR g

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FACluTY NAME DOCKET NURSER

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01 22 97 97 001 00 02 21 97 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANTTO THE REQUIREMENTS OF 10 CFRS (Check one or more)(11)

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MODE (9) 20.2201(b) 20.2203(a)(2Xv) 50.73(a)(2)(i) 50.73(a)(2Xviii) i POWER 20.2203(a)(1) 20.2203(a)(3)(i)

X 50.73(a)(2)(ii) 50.73(aX2)(x)

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LEVEL (10) 100 20 2203(ax2)m 20 2203(ax3xu) 50 73(ex2)(iii) 73 71 l

i 20.2203(aX2)(ii) 20.2203(a)(4) 50.73(a)(2)(iv)

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20.2203(aX2Xin) 50.36(c)(1) 50.73(a)(2)(v)

Specifyin Abstract below orin NRC Forrn 366A 1

j 20.2203(aX2)(iv) 50.36(cX2) 50.73(aX2XvH)

LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NURSER (include Area Code)

Randel E. Lewis, Principal Engineer (402)533-6508 i

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COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

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SYSTEM COMPONENT MANUFACTURER

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DATE (16)

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ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewntten knes) (16) i Following the report by Millstone Unit 2 of a problem with the calculation of Main Steam Safety Valve (MSSV) setpoints on September 3, 1996, Fort Calhoun Station (FCS)d began an investigation to determine if similar issues a) plied. It has been determine i

i that on only one occasion, over the life of the plant, lave the number of inoperable l

MSSVs exceeded the design basis as recalculated due to this incident. The design basis was recalculated when it was discovered that the pressure drop to the MSSVs was not i

being taken into account.

The root cause of this event was an inadequate vendor review of a CESEC code modeling.

When the code modeling was originally developed, the analysis methodology should have accounted for piping pressure losses associated with flow. CESEC does not have the capability for directly modeling pressure drop in the piping. Therefore, the potential existed for pressure to exceed the code allowed during a single Main Steam (MS)

I j

isolation valve closure event.

i OPPD has performed the necessary analysis to update the design basis of the plant to 4

account for the error discovered and reported in this LER. GuidanLe has been provided l

to the operating staff to ensure that the design basis is maintained. A revision to the L

FCS Technical Specifications will be submitted to appropriately reflect the new design basis.

3 NRC FORM 366 (446) i J

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lU.S. NUCLEAR REGULATORY CoMMISSloN l

teel)

I LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACluTY NAME (1)

DbCKET LER NUMBER :6)

PAGE (3)

Fort Calhoun Station Unit No. 1 05000285 2OF5 97

- 001 -

00 l

TEXT pr more space as regenrad, sese adcatonat copes of NRC form 306A)(17)

BACKGROUND I

The Fort Calhoun Station (FCS) uses two steam generators (SGs) to supply steam to a single turbine. The Main Steam (MS) system is protected from over-pressure by ten safety valves, five on each of the two MS headers. The MS Safety Valves (MSSVs) are located in Room 81 just outside of the containment, about 100 piping feet from the SGs.

EVENT DESCRIPTION

On September 3, 1996, Millstone Unit 2 reported that the pressure drop between their SGs and MSSVs had not been taken into account in determining the safety valve setpoints. They indicated that the SG pressure resulting from one of the Design Basis Accidents (DBAs) would exceed 110 percent of American Society of Mechanical Engineers (ASME) design pressure for the system. Omission of the pressure drop effects the loss of load, loss of feedwater and loss of coolant accident (LOCA) analyses, and creates a potential for MSSV chatter. Omaha Public Power District (0 PPD) management determined

)

that the issue should be reviewed for applicability to FCS. An Engineering Assistance i

Request (EAR)96-153 was initiated to investigate this issue. The EAR was assigned to Design Engineering to determine if similar issues existed at FCS.

Calculation FC 06627 was performed to determine the pressure drop between the SGs and MSSVs for conditions of maximum design flow through the MSSVs coincident with MS Isolation Valve (MSIV) closure without a reactor trip. The calculated pressure drop is 35 pounds per square inch (psi) at maximum steam flow.

OPPD conducted a review to determine if problems similar to those reported by Millstone and subsequently elaborated upon by Asea Brown Boveri/ Combustion Engineering (ABB/CE), formerly known as Combustion Engineering (CE) existed at FCS. OPPD reviewed the FCS and Millstone Unit 2 MSSV configuration and their implications on FCS MSSV operation. A review of FCS MSSV design basis, disclosed one calculation related to i

valve setpoints. Calculation FC 05586 Rev. O, determined the minimum and maximum MSSV setpoints allowed by code, without consideration of inlet pressure drop. When the calculated pressure drop was considered in the response to EAR 96-153, it was concluded that the FCS MSSV configuration is not susceptible to the valve chattering reported by Millstone.

While updating the appropriate plant calculations with the previously mentioned data, the engineer compared his data with the pressure drop assumed in the plant accident analyses and discovered that the pressure drop between the SGs and MSSVs was also not accounted for in those analyses. Omission of the pressure drop, as previously noted, could adversely affect certain LOCA and non-LOCA safety analyses where the MSSVs are w

NRC FORM 344A (4-H)

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'U.S. NUCLEAR REGULATORY CoMMISSloN p*si LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET LER NUMBER E6)

PAGE (3)

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Fort Calhoun Station Unit No.1 05000285 3 or 5 97

- 001 -

00 TEKT (bt more space a requend, use adthhonalcrtues of NRC Form 366A)(11) activated.

On January 14, 1997, engineering completed the calculation associated with the 1

EAR 96-153 and concluded that pressure drops occurring between the SG and the inlet to the MSSVs was not accounted for in the appropriate Updated Safety Analysis Report (USAR) Chapter 14 (Safety Analysis) analyses. On January 15, 1997, a Condition Report (CR) was issued to document above findings and initiate the necessary corrective actions to resolve the deficiency.

CE had performed the initial LOCA and non-LOCA thermal hydraulic safety analyses for FCS. The non-LOCA analyses consist of the loss of load and loss of feedwater DBAs. The loss of load analysis was performed by CE until 1983 when OPPD started performing the analysis in-house. The CESEC (Combustion Engineering System Excursion Code) code is utilized to perform this analysis. The CESEC code does not have the capability to directly account for pressure drops in piping upstream or downstream of the MSSV. The I

piping losses can be accounted for within the CESEC code by adjusting other parameters, such as valve opening area and valve setpoints.

)

On January 17, 1997, ABB-CE issued a 10 CFR 21 notification that a reportable defect exists which is applicable to all safety analyses for nuclear power plants for which ABB-CE was the nuclear steam supply system vendor. The specific concern involves the piping losses between the SG and the MSSVs while the MSSVs are open. The CE part 21 notification stated that omission of the piping loss from calculations may adversely affect certain LOCA and non-LOCA safety analyses where the MSSVs are activated. The ASME code requirement states, in part, that "..in determining the setting pressures and discharge capacities required to comply with these rules, full account shall be taken of the pressure drop in both inlet and discharge side of the pressure relief devices at full discharge conditions. In addition back pressure arising from discharge of other devices through common discharge piping shall be considered..." This is the same issue that was independently discovered by 0 PPD and documented by the CR previously mentioned.

On January 22, 1997, this information was brought to the Plant Review Committee (PRC) for a reportability review. At 0850 Central Standard Time (CST), the PRC determined that this condition constituted a condition where the plant may have been outside of the plant design basis in the past. A one-hour non-emergency report was made to the NRC Operations Center pursuant to 10 CFR 50.72(b)(1)(ii)(B) on January 22, 1997, at 1005 Eastern Standard Time (EST). This report is being submitted pursuant to 10 CFR 50.73(a)(2)(ii)(B).

Technical Specification (TS) 2.1.6(3) states that "Whenever the reactor is in power operation, eight of the ten main steam safety valves shall be operable..." Subsequent NRC FORM 364A (446)

NRC FORJ 366A U.S. NUCLEAR REOULATORY COMMISSloN (445)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET LER NUMBER :6)

PAGE (3)

SEQUENTIAL REVISION g

Fort Calhoun Station Unit No. 1 05000285 4OF5 97

- 001 -

00 TEXT of noe space a requwed van edenhonalcopes of NRC Fonn 366N (17) analysis has determined that the design basis for the plant will support one inoperable MSSV on each of the two MS headers.

A comprehensive review was conducted to determine the status of all the MSSVs over the life of the plant. It was determined that on only one occasion over the life of the plant had more than one MSSV exceeded 103 percent of set pressure on the same MS header. LER 88-023 Revision 1 reported a condition where three MSSVs failed to lift within their required lift range during testing. MS-277 and MS-278 are connected to the same MS header. The revised design basis, which considers pressure drop, will not support any two steam safety valves being inoperable on the same MS header. The 1988 as found data for the valves was:

Specified As Found Lift Valve Set Pressure Pressure (psig)

(psig)

MS-275 1035 1045 MS-276 1025 1030 MS-277 1010 1140 MS-278 1000 1135 MS-279 1035

</= 1025 MS-280 1025 1020 MS-281 1010 1010 MS-282 1000 1125 MS-291 985 985 MS-292 985 990 Where psig is pounds per square inch gage. LER 88-023 Revision 1 reported that an analysis performed using the CE CESEC code indicated that even though three valves had been inoperable, the design basis of the plant was not effected. The analysis performed in 1988 did not account for the pressure drop discovered and reported in this LER. The conclusion of LER 88-023 Revision 1 that the design basis was not affected was incorrect. An evaluation using current data has been conducted. The results of this analysis are discussed below.

SAFETY SIGNIFICANCE

As indicated above, a comprehensive review of the plant history of MSSV operability has been conducted. While the plant TSs would have allowed two MSSVs on a single MS line to be inoperable, at only one time in the history of the plant has more than one valve in each MS line exceeded 103 percent of set pressure, m

NRC FORM 364A (445)

  • U.S. NUCLEAR REGULATORY COMMISSION

{446)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET LER NUMisER L6)

PAGE (3)

SEQUENTIAL REVISION g

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Fort Calhoun Station Unit No.1 05000285 5OF5 97

- 001 -

00 TEXT tof truwe space is reqwred. use edcahonal copes of NRC Form 366A)(47}

The limiting DBA, loss of feedwater, was evaluated with the MSSVs lifting at the as found values indicated by the 1988 test results. This evaluation indicated that the maximum pressure that would have been seen in a design basis loss of feedwater accident would be about 1099 psia, which is less than 110 percent of the design MS system pressure. The SGs have been hydrostatically tested to 125 percent of design pressure without incident as required by ASME code. No incidents of MS pressure unintentionally exceeding the design limit have been recorded.

These evaluations demonstrate that the error discovered and reported by this LER does not pose a significant safety concern.

CONCLUSION The root cause of this event was an inadequate vendor review of CESEC code modeling.

When the original code modeling was developed, the analysis methodology should have i

accounted for piping pressure losses associated with flow. CESEC does not have the capability for directly modeling pressure drop in the piping. Therefore, the potential l

existed for allowing pressure to exceed the ASME code limit during a single MSIV closure event.

l A contributing cause to this event is that CE performed transient analyses several times, but did not verify the input data regarding adjustment for piping loss. OPPD i

Engineering has performed loss of load and loss of feedwater analyses using the CESEC code since 1983 and the oversight was carried over from one revision to next revision.

CORRECTIVE ACTIONS

OPPD has performed the necessary analysis to update the design basis of the plant to account for the error discovered and reported in this LER. Guidance has been provided to the operating staff to ensure that the design basis is maintained.

OPPD will submit a revision to the FCS TSs to stipulate that no more than one MSSV may be inoperable on a MS line whenever the reactor is in power operation. The revision to TSs will be submitted by March 31, 1997.

PREVIOUS SIMILAR EVENTS

Other than the incident referenced above (LER 88-023), no other incidents have occurred at the FCS where MSSV setpoints have been affected by errors in vendor provided calculations.