05000285/LER-2013-005, Regarding Control Room HVAC Modification Not Properly Evaluated

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Regarding Control Room HVAC Modification Not Properly Evaluated
ML13120A059
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 04/29/2013
From: Cortopassi L
Omaha Public Power District
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LIC-13-0051 LER 13-005-00
Download: ML13120A059 (6)


LER-2013-005, Regarding Control Room HVAC Modification Not Properly Evaluated
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
2852013005R00 - NRC Website

text

LlC-13-0051 April 29, 2013 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001 Reference: Docket No. 50-285

Subject:

Licensee Event Report 2013-005, Revision 0, for the Fort Calhoun Station Please find attached Licensee Event Report 2013-005, Revision 0, dated April 29, 2013.

This report is being submitted pursuant to 10 CFR 50.73(a)(2)(v)(D) and 10 CFR 50.73(a}(2)(vii)(D). There are no new commitments being made in this letter.

If you should have any questions, please contact Terrence W. Simpkin, Manager, Site Regulatory Assurance, at (402) 533-6263.

ouis P. Cortopassi Site Vice President and CNO LPC/epm/rjr Attachment c:

A. T. Howell, NRC Regional Administrator, Region IV J. M. Sebrosky, NRC Project Manager L. E. Wilkins, NRC Project Manager J. C. Kirkland, NRC Senior Resident Inspector Employment with Equal Opportunity

NRC FORM 366 (10-2010)

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (10-2010)

LICENSEE EVENT REPORT (LER)

(See reverse for required number of digits/characters for each block)

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013

, the NRC may not conduct or sp onsor, and a person is not required to respond to, th e

information collection.

1. FACILITY NAME Fort Calhoun Station
2. DOCKET NUMBER 05000285
3. PAGE 1 OF 5
4. TITLE Control Room HVAC Modification Not Properly Evaluated
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL NUMBER REV NO.

MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 05000 2

27 2013 2013 005 -

0 04 29 2013 FACILITY NAME DOCKET NUMBER 05000

9. OPERATING MODE 5
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 20.2201(b) 20.2203(a)(3)(i) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii) 20.2201(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(2)(i) 50.36(c)(1)(i)(A) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A) 20.2203(a)(2)(ii) 50.36(c)(1)(ii)(A) 50.73(a)(2)(iv)(A) 50.73(a)(2)(x) 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(v)(A) 73.71(a)(4) 20.2203(a)(2)(iv) 50.46(a)(3)(ii) 50.73(a)(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(C)

OTHER 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(v)(D)

Specify in Abstract below or in LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET This report is being submitted pursuant to 10 CFR 50.73(a)(2)(v)(D): Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident, and 10 CFR 5073(a)(2)(vii)(D): Any event where a single cause or condition caused two independent trains or channels to become inoperable in a single system designed to mitigate the consequences of an accident.

CONCLUSION A causal analysis is in progress. The results of the analysis will be published in a supplement to this LER.

CORRECTIVE ACTIONS

A causal analysis is in progress. The results of the analysis will be published in a supplement to this LER.

SAFETY SIGNIFICANCE

A causal analysis is in progress. The results of the analysis will be published in a supplement to this LER.

SAFETY SYSTEM FUNCTIONAL FAILURE A causal analysis is in progress. The results of the analysis will be published in a supplement to this LER.

PREVIOUS EVENTS A causal analysis is in progress. The results of the analysis will be published in a supplement to this LER.