Similar Documents at Salem |
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OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Statiori U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 90-033-00 October 23, 1990 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a) (2) (vii) (C).
This report is required within thirty (30) days of discovery.
MJP:pc Distribution
- ~10102'?0270 PDR A:OOO=::
The Energy People Sincerely yours, S. LaBruna General Manager -
Salem Operations re:12 95-2189 (10M) 12-89
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TITLE ICI Two channels made inoperable due to common equipment failure.
EVENT OATI (Ill LER. NUMBER Ill REPORT DATE (7)
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On 9/23/90, a.control Room Operator observed that the 1RllA/1R12A/lR12B Containment Radiation Monitoring System (RMS) pump operability indication was not illuminated.
Since it was questionable as to pump operability, the lRllA, 1R12A and 1R12B RMS channels were declared inoperable and Technical Specification Action Statements 3.4.6.1 and 3.9.9 were entered as per Technical Specification Table 3.3-6 Action 20 (i.e., lRllA inoperable) and Action 22 (i.e., 1R12A inoperable).
The 1Rl2B channel is not taken credit for in the accident analyses.
The lRllA and 1R12A channels provide. automatic isolation of the Containment Purge/Pressure -
Vacuum Relief System upon detection of high activity.
The root cause of this event has been attributed to an equipment/design concern.
Condensation had caused corrosion (rust) which seized the moving vanes of the positive displacement sampling pump.
Upon replacement of the sample pump, the lRllA and 1R12A monitors were declared operable and the appropriate Action Statement were exited.
An inspection program will be initiated to identify the mean time to sample pump failure.
The design of the Containment-1R11A/1R12A/1R12B RMS will be reviewed.
Appropriate design change(s) to address condensation concerns will be made as applicable.
The pump will be replaced with a more reliable pump.
In the interim, preventive maintenance every six (6) months will be performed until a *more reliable pump is approved for use.
In addition, the weekly inspe~tion program for the sample pump and associated equipment (e.g., filter paper motor) will be enhance~ to better predict the the next failure.
NRC Form 3111 (9-631
LICENSEE EVENT REPO~T (LE~) ~EXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272 LER NUMBER 90-033-00 PAGE 2 of*6
PLANT AND SYSTEM IDENTIFICATION
.Westinghouse
- - Pressurized Water Reactor Energy Industry Identification System (E!IS) codes are identified* in
. the text as {xxl IDENTIFICATION OF OCCURRENCE:
Two (2) channels in a
~ingle system made inoperaple due to common equipment failure Event Date:
9/23/90 Report Date:
10/23/90 This report was initiated by Incident Report No.90-714.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 Reactor Power 97% - Unit Load 1119 MWe DESCRIPTION OF OCCURRENCE:
On September 23, 1990 at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, a Control Room Operator observed that the 1R11A/1Rl2A/1R12B Containment Radiation Monitoring System (RMS) {!LI pump operability indication was not illuminated.
These three (3) RMS channels analyze a sample of Containment atmosphere provided by this single pump.
Since it was questionable as to pump operability, the lRllA, 1Rl2A and 1R12B RMS channels were declared inoperable and Technical Specification Action Statements 3.4.6.1 and 3.9.9 were entered as per Techriical Specification Table 3.3-6 Action 20 (i.e., lRllA inoperable) and Action 22 (i.e., 1Rl2A inoperable).
The 1Rl2B channel is not taken credit for in the accident analyses and therefore has no.applicable Technical *Specifi_cation.
Technical Specification Table 3.3-6 Action 20 'states:
"With the number of channels OPERABLE-less than required by the Minimum Channels OPERABLE. requirement, comply with the ACTION requirements of Specification 3.4.6.1."
Technical Specification Table 3.3-6 Actio~ 22 states:-
"With the number of channels OPERABLE less than required by the Minimum Channels OPERABLE requirement, comply with the ACTION requirements of Specification 3.9.9."
Technical Specification 3.4.6.1 states:
"The following Reactor Coolant System leakage detection systems shall be OPERABLE:
LICENSEE EVENT REPORT (LER)
T~XT CONTINUATION Salem Generating Station Unit 1
- DOCKET NUMBER 5000272 DESCRIPTION OF OCCURRENCE:
(cont'd)
LER NUMBER 90-033-00' PAGE 3 of 6 a.
The containment atmosphere particulate radioactivity monitoring system, b.
The conta1nment sump level monitoring system, and c.
Either the containment fan cooler condensate flow rate or the containment atmosphere gaseous radioactivity monitoring system.
Technical Specification Action Statement 3.4.6.1 states:
"With only two of the above required leakage detection systems OPERABLE, operation may continue for up to 30 days provided grab samples of *the containment atmosphere are. obtained and analyzed at least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> when the required gaseous and/or particulate radioactivity monitoring system i~ inoperable; otherwise, be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the fallowing 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />. ;,
Technical Specification 3.9.9 states:
"The. Containment Purge and Pressure-Vacuum Relief isolation system shall be OPERABLE."
Technical Specification Action Statement 3.9.9 states:
"With the Containment Purge and Pressure-Vacuum Relief isolation system inoperable, close each of.the Purge and Pressure-Vacuum Relief penetrations providing direct access frpm the containment atmosphere to the outside atmosphere.
The provision of Specification 3.0.3 are not applicable."
APPARENT CAUSE OF OCCURRENCE:
The root cause of this event is attributed to equipment/design concerns.
Investigation revealed that the sample pump was tripped due to failure of the lRllA channel's filter paper motor.
The paper motor is interlocked with the sample pump.
Instrument.power fuses were found blown due to a shorted filter paper motor.
After replacement of the paper motor and the associated fuses, the technician initiated a system operability check.
He observe.d that the lRllA RMS sample pump was not operating properly.
Subsequently the sample pump and belts were replaced.
The filter paper motor had apparently overloaded due to increased friction caused by condensation oxidizing the rotating surface of the "paper drive drum".
Inspection of the filter paper housing revealed
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
- . Salem Generating Station Unit 1 DOCKET NUMBER 5000272 APPARENT CAUSE OF OCCURRENCE:
(cont'd)
LER NUMBER 90-033-00 water accumulation (filter paper had swelled).
PAGE 4 of 6 Inspection of the sample pump revealed that the pump vanes*had seized due to corrosion (rust) attributed to condensation.
This is a positive displacement pump which uses graphite vanes.
A system walkdown (by the System Engineer) has revealed that the slope of the sample tubing is towards the pump.
Although the sample is drawn from Containment (130' El.) the sample pump and detectors*
are located outside Containment in the 78' Elevation Electrical Penetration Area.
The sample line Containment penetrati.on is located at 88' Elevation.
The Electrical Penetration Area is ~equired to be maintained between 60°F and 105°F.
Located directly above the radiation monitoring equipment skid (lRllA, 1R12A and 1R12_B) is a.vent which blows directly onto the skid.
Ventilation to the area is not heated
{outside air only).
Also, the filter paper housing and sample and discharge lines are not insulated or heat traced.
These factors contribute to the promotion of condensation.
This area is normally cooler than Containment; therefore, any hlimidity in the Containment air sample readily condenses in the sample line {and filter paper housing) outside Containment.
ANALYSIS OF OCCURRENCE:
The lRllA Containment Particulate Monitor monitor's the air particulate gamma radioactivity in the Containment atmosphere.
It is used as an aid_ in the identification of Reactor Coolant System (ABJ*
leakage in conjunction with the containment sump level monitoring system and either the containment fan cooler condensate flow rate or the containment atmosphere gaseous.( 2R12A) *
- radioactivity c.-moni taring system {as per Technical. Specification 3.4.6.* 1). _;,An alarm signal will cause the automatic isolation of the Co#ta~ii.inent Pressure/Purge Vacuum Relief System.
0
._::~~-.
The 1R12A Containment Noble Gas Monitor monitor's the noble_ gas activity in the Containment atmosphere to ensure *the gaseous releases through the plant vent or from containment purges.do.not *exceed Technical Specification 3.11.2.1 limits.
Ari*alarm siQ!lal will cause the automatic isolation of the Containment Pressure/Purge**- ~vacuum
- Relief System {an Engineered Safety Feature). **;.Iii' *Mode 6 (Refueling),
this monitors setpoint is reset to 2 times background in order to provide early isolation and indication of a fuel handling accident.
Air samples are pulled directly from the Containment atmosphere (130' Elevation) through a moving filter paper.
The filter paper continuously moves pas-t the lRllA detector, a scintillation type detector.
After the air sample passes through the moving filter
LICENSEE EVENT REPORT (LER} TEXT CONTINUATION Salem Generating Station Unit 1 ANALYSIS OF OCCURRENCE:
DOCKET NUMBER 5000272 (cont'd}
LER NUMBER
'90-033-00 PAGE 5 of 6 paper, it passes through a charcoal cartridge and is then mixed into a fixed shielded volume where it is viewed by the 1Rl2A monitor, a geiger-mueller detector.
The a1r sample is then returned to the Containment.
The 1Rl2B Containment Iodine Monitor monitors the charcoal cartridge for increases in Containment iodine activity.
The 1Rl2B monitor does not have any safety interlock functions.
Several area r'adiation monitors corroborate the lRllA and 1R12A *
.channels I indications.. The corroborating area radiation monitors do not have isolation capabilities, they only have alarm capability.
The requirements of the applicable Technical Specifications for inoperability of the lRllA and 1Rl2A monitors were complied with.
No Containment release*occurred during the time when the lRllA*and the 1Rl2A monitors were inoperable.
The corroborating area RMS channels did not indicate any significant increase in Containment atmosphere radioactive efflu~nts. Therefore, this event did not affect the health or safety of the public, however, since a single cause (erratic sample air flow} restilted in the lRllA and 1R12A monitors, each of which provide an ESF system actuation signal, to become inoperable this event is reportable in accordance with 10CFR 50.73 (a) (2) (vii).
CORRECTIVE ACTION
The sample pump, the filter paper.motor and the fuses :were replaced.
Subsequently, based upon adjustment of the sample flow and verification of* system operability, on September 26, 1990 at 1626 hours0.0188 days <br />0.452 hours <br />0.00269 weeks <br />6.18693e-4 months <br />,* the lRllA and 1Rl2A monitors were declared operable and the appropriate Technical Specifications were*.exited.
The design of the Containment 1R11A/1R12A/1R12B AtMS:-,will be reviewed.
Appropriate design change (s) t'o.. ~a<idreiiJs,;;c;ondensation *
- c::::e:
1:i :: ::e a::~:::i::b::~ pump's d~~y~:i::lication has been previously identified (reference LER 272/~9-010-00). *-The pump is scheduled to be replaced with a more reliable p11mp as part of the RMS Upgrade Project.
In the interim, based upon ~-a review of the failure history of the pump, preventive maintenance every six (6) months will be performed until a more reliable"p\\lmp is approved for use.
In addition, the weekly inspection program for the*sample pump and associated equipment (e.g., filter paper motor) will be enhanced to better predict the the next failure.
The failure history of the paper filter motor was reviewed.
Only one other failure (circa 1984) was identified.
The prior failure could not be shown to be related to the cause of this event.
LICENSEE EVENT REPORT (LER} TEXT CONTINUATION Salem Generating Station Unit 1 FAILURE DATA:
Air Sample Pump:
DOCKET NUMBER 5000272 LER NUMBER 90-033-00 PAGE 6 of 6 Manufacturer:
Conde Milking Machine Co.
MJP:pc SORC Mtg.90-145 Dry Air Rotary Positive Displacement Vacuum Pump Part :ft DA06CWOO General Manager -
Salem Operations
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| 05000272/LER-1990-001, :on 900106,containment purge/pressure-vacuum Relief Sys Isolation Signal Actuated as Result of Channel Spike on Particulate Radiation Monitor 1R11A.Caused by Dirty Pc Cards.Cards Cleaned & Connectors Checked |
- on 900106,containment purge/pressure-vacuum Relief Sys Isolation Signal Actuated as Result of Channel Spike on Particulate Radiation Monitor 1R11A.Caused by Dirty Pc Cards.Cards Cleaned & Connectors Checked
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-001-01, :on 900101,general Area Radiation Monitoring Sys Monitor Spiked Into Alarm Resulting in Second Automatic Switching of Control Room Ventilation.Caused by Design/ Equipment Concerns.Channel Reset |
- on 900101,general Area Radiation Monitoring Sys Monitor Spiked Into Alarm Resulting in Second Automatic Switching of Control Room Ventilation.Caused by Design/ Equipment Concerns.Channel Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-002-01, :on 900117 & 0201,containment Purge/Pressure Vacuum Relief Sys Isolation Signals Initiated Due to Failures of Radiation Monitor Channel 1R41.Caused by Design/ Equipment Problem.Control Modules Reseated |
- on 900117 & 0201,containment Purge/Pressure Vacuum Relief Sys Isolation Signals Initiated Due to Failures of Radiation Monitor Channel 1R41.Caused by Design/ Equipment Problem.Control Modules Reseated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-002, :on 900104,determined That ECCS Flow Balance Verification Surveillance Not Correctly Calculated After Last Refueling Outage on 881023.Caused by Personnel Error. Discretionary Enforcement Granted by NRC |
- on 900104,determined That ECCS Flow Balance Verification Surveillance Not Correctly Calculated After Last Refueling Outage on 881023.Caused by Personnel Error. Discretionary Enforcement Granted by NRC
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1990-003-01, :on 900122,plant Vent Radioactive Noble Gas Monitor 1R41C Spiked High,Causing Containment Purge/Pressure Vaccum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Detector.Channel Relay Repaired |
- on 900122,plant Vent Radioactive Noble Gas Monitor 1R41C Spiked High,Causing Containment Purge/Pressure Vaccum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Detector.Channel Relay Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-003, :on 900105,steam Generator 22 Blowdown Radiation Monitoring Sys Channel 2R19B Failed.Caused by Design/Equipment Concerns.Radiation Monitoring Sys Monitors & Modules Reseated |
- on 900105,steam Generator 22 Blowdown Radiation Monitoring Sys Channel 2R19B Failed.Caused by Design/Equipment Concerns.Radiation Monitoring Sys Monitors & Modules Reseated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-004-01, :on 900124,spurious Actuation Signal for Containment Purge/Pressure Vacuum Relief Sys Isolation Received.Probably Caused by Failed Radiation Monitoring Sys Channel.Sys Design Mods Underway |
- on 900124,spurious Actuation Signal for Containment Purge/Pressure Vacuum Relief Sys Isolation Received.Probably Caused by Failed Radiation Monitoring Sys Channel.Sys Design Mods Underway
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-004, :on 900112,plant Vent Noble Gas Monitor 2R41A Channel Failed Low,Resulting in Containment Purge/Pressure Vacuum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Monitor.Channel Module Adjusted |
- on 900112,plant Vent Noble Gas Monitor 2R41A Channel Failed Low,Resulting in Containment Purge/Pressure Vacuum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Monitor.Channel Module Adjusted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-005-01, :on 900220,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor Channel Began Intermittently Spiking High Resulting in Containment Purge.Caused by Design /Equipment Problem.Equipment Replaced |
- on 900220,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor Channel Began Intermittently Spiking High Resulting in Containment Purge.Caused by Design /Equipment Problem.Equipment Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-005, :on 900117,Tech Spec Action Statement 3.0.3 Entered Due to Inoperability of Two High Head ECCS Subsys. Caused by Leak from Welded Pipe Cap on Boron Injection Tank. Pipe-to-cap Socket Welded Joint Repaired |
- on 900117,Tech Spec Action Statement 3.0.3 Entered Due to Inoperability of Two High Head ECCS Subsys. Caused by Leak from Welded Pipe Cap on Boron Injection Tank. Pipe-to-cap Socket Welded Joint Repaired
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1990-006-01, :on 900302,ESF Actuation & Containment Ventilation Isolation Occurred.Caused by Design/Equipment Problem.Channel Backplane Replaced & Functional Test Completed |
- on 900302,ESF Actuation & Containment Ventilation Isolation Occurred.Caused by Design/Equipment Problem.Channel Backplane Replaced & Functional Test Completed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-006, :on 900117,control Room General Area Radiation Monitor Spiked High,Resulting in Switching Ventilation Sys to Emergency Mode of Operation.Caused by Damaged Pins on Channel Backplate & Modules.Pins Repaired |
- on 900117,control Room General Area Radiation Monitor Spiked High,Resulting in Switching Ventilation Sys to Emergency Mode of Operation.Caused by Damaged Pins on Channel Backplate & Modules.Pins Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-007-01, :on 900321,found Tech Spec Surveillance for Containment Spray Not Performed Historically.Root Cause of Event Attributed to Past Inadequate Administrative Controls. Administrative Procedure Revised |
- on 900321,found Tech Spec Surveillance for Containment Spray Not Performed Historically.Root Cause of Event Attributed to Past Inadequate Administrative Controls. Administrative Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-007, :on 900117,main Steam Line Isolation Signal Actuated During Surveillance for Pressure Transmitter, Causing Isolation Signal & ESF Actuations.Caused by Inadequate Procedure.Panel Labeling Corrected |
- on 900117,main Steam Line Isolation Signal Actuated During Surveillance for Pressure Transmitter, Causing Isolation Signal & ESF Actuations.Caused by Inadequate Procedure.Panel Labeling Corrected
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-008, :on 900120,plant Vent Noble Gas Monitor 2R41C Failed Low,Resulting in Closure Signal for Waste Gas Decay Tank Vent Control Valve 2WG41.Caused by Personnel Error. Operator Aid Will Be Posted on Panel |
- on 900120,plant Vent Noble Gas Monitor 2R41C Failed Low,Resulting in Closure Signal for Waste Gas Decay Tank Vent Control Valve 2WG41.Caused by Personnel Error. Operator Aid Will Be Posted on Panel
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-008-01, :on 900327,controlled Shutdown Commenced,Per Tech Spec Action Statement Due to Inoperability of Safeguards Equipment Controls Cabinet 1A.Caused by Equipment Failure.Spare Chassis Installed |
- on 900327,controlled Shutdown Commenced,Per Tech Spec Action Statement Due to Inoperability of Safeguards Equipment Controls Cabinet 1A.Caused by Equipment Failure.Spare Chassis Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000311/LER-1990-009, :on 900123,plant Vent Radioactive Iodine Monitor Channel Spiked High Resulting in Containment Purge/ pressure-vacuum Relief Sys Isolation Signal.Caused by Design & Equipment Problems.Scaler Test Jack Replaced |
- on 900123,plant Vent Radioactive Iodine Monitor Channel Spiked High Resulting in Containment Purge/ pressure-vacuum Relief Sys Isolation Signal.Caused by Design & Equipment Problems.Scaler Test Jack Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-009-01, :on 900328,main Steamline Isolation Signal Actuated During Performance of Channel I Main Steamline Flow Calibr.Caused by Inadequate Procedure.Main Steamline Flow Detector Calibr Procedure Revised |
- on 900328,main Steamline Isolation Signal Actuated During Performance of Channel I Main Steamline Flow Calibr.Caused by Inadequate Procedure.Main Steamline Flow Detector Calibr Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-010, :on 900216,containment Radioactive Iodine Monitor Radiation Monitoring Sys Channel Failed Low.Caused by Design/Equipment Concerns.Sys Design Mods Will Be Implemented to Eliminate ESF Actuation Signals |
- on 900216,containment Radioactive Iodine Monitor Radiation Monitoring Sys Channel Failed Low.Caused by Design/Equipment Concerns.Sys Design Mods Will Be Implemented to Eliminate ESF Actuation Signals
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-010-01, :on 900403,reactor Trip Signal Initiated Due to lo-lo Level in Steam Generator 12.Caused by Personnel Error. Event Reviewed by Operations Dept Mgt & Personnel Involved Held Accountable |
- on 900403,reactor Trip Signal Initiated Due to lo-lo Level in Steam Generator 12.Caused by Personnel Error. Event Reviewed by Operations Dept Mgt & Personnel Involved Held Accountable
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-011, :on 900301,containment Ventilation Isolation Signal (ESF) Occurred.Caused by Equipment Failure.Frayed Wire Repaired & Functional Surveillance Requirement Modified to Include Insp of Wire |
- on 900301,containment Ventilation Isolation Signal (ESF) Occurred.Caused by Equipment Failure.Frayed Wire Repaired & Functional Surveillance Requirement Modified to Include Insp of Wire
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-011-01, :on 900406,turbine Trip & Feedwater Isolation Actuation Occurred on Steam Generator 14 hi-hi Level. Caused by Equipment Failure.Valve Stem on Valve 12TB10 Polished & Adjusted |
- on 900406,turbine Trip & Feedwater Isolation Actuation Occurred on Steam Generator 14 hi-hi Level. Caused by Equipment Failure.Valve Stem on Valve 12TB10 Polished & Adjusted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-012, :on 900403,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor 2R41C Lost Power Resulting in Isolation in Containment purge/pressure-vacuum Relief Sys. Cause Not Determined |
- on 900403,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor 2R41C Lost Power Resulting in Isolation in Containment purge/pressure-vacuum Relief Sys. Cause Not Determined
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-012-01, :on 900409,reactor Trip on Steam Generator 12 lo-lo Level Occurred.Caused by Equipment Failure.Steam Generator 12 Governor Valve Linkage Repaired |
- on 900409,reactor Trip on Steam Generator 12 lo-lo Level Occurred.Caused by Equipment Failure.Steam Generator 12 Governor Valve Linkage Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-013, :on 900410,radiation Monitoring Sys Channel 1R12A Spiked Into Alarm,Resulting in ESF Actuation Signal. Caused by Failure of Electrical Signal Connectors &/Or Electronic Circuit Connections.Repairs Made |
- on 900410,radiation Monitoring Sys Channel 1R12A Spiked Into Alarm,Resulting in ESF Actuation Signal. Caused by Failure of Electrical Signal Connectors &/Or Electronic Circuit Connections.Repairs Made
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-013-01, :on 900416,discovered That Setpoint for 2R11A & 2R12A Monitors for Radiation Monitoring Sys Channels Not Changed During Last Refueling Outage.Caused by Inadequate Administrative Control.Procedure Revised |
- on 900416,discovered That Setpoint for 2R11A & 2R12A Monitors for Radiation Monitoring Sys Channels Not Changed During Last Refueling Outage.Caused by Inadequate Administrative Control.Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1990-014, :on 900419,ESF Actuation Signal for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40 |
- on 900419,ESF Actuation Signal for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(b)(2)(ii) | | 05000272/LER-1990-014-01, :on 900409,determined That Last Calculated Safety Injection Pump Flow Rate for Pumps 12 & 21 Greater than 650 Gpm.Caused by Personnel Error & Procedural Deficiencies.New Orifice Plates Installed |
- on 900409,determined That Last Calculated Safety Injection Pump Flow Rate for Pumps 12 & 21 Greater than 650 Gpm.Caused by Personnel Error & Procedural Deficiencies.New Orifice Plates Installed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-015, :on 900415,ESF Signal Actuation for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40 |
- on 900415,ESF Signal Actuation for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-015-01, :on 900430,control Room Intake Radiation Monitor 1R1B Alarm Circuitry Failed,Resulting in Switching Control Room Ventilation from Normal to Accident Mode. Caused by Short in Bulb.Bulbs Replaced |
- on 900430,control Room Intake Radiation Monitor 1R1B Alarm Circuitry Failed,Resulting in Switching Control Room Ventilation from Normal to Accident Mode. Caused by Short in Bulb.Bulbs Replaced
| | | 05000272/LER-1990-016-01, :on 900419,determined That Six Fast Closure Turbine Bldg Svc Water Sys Isolation Valves Could Not Be Counted on to Function During Design Base Event.Caused by Inadequate Design |
- on 900419,determined That Six Fast Closure Turbine Bldg Svc Water Sys Isolation Valves Could Not Be Counted on to Function During Design Base Event.Caused by Inadequate Design
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000311/LER-1990-016, :on 900420,discovered That Containment Pressure Relief Conducted W/Associated Radiation Monitoring Sys Channels Inoperable.Caused by Inoperability of Control Room Pump Low Flow Alarm.Procedures Revised |
- on 900420,discovered That Containment Pressure Relief Conducted W/Associated Radiation Monitoring Sys Channels Inoperable.Caused by Inoperability of Control Room Pump Low Flow Alarm.Procedures Revised
| 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1990-017-01, :on 900507,high Head Safety Injection Pumps Failed to Meet Seismic Criteria.Caused by Equipment Mfg Failure to Complete Required Welding.Intermediate Head Safety Injection Pumps Design Reviewed |
- on 900507,high Head Safety Injection Pumps Failed to Meet Seismic Criteria.Caused by Equipment Mfg Failure to Complete Required Welding.Intermediate Head Safety Injection Pumps Design Reviewed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000311/LER-1990-017, :on 900501,inadvertent Manual Safety Injection Occurred Due to Personnel Error.Technician Made Assumption Re Wiring Changes Performed.Train B Wiring Corrected & Deficiency Rept Initiated |
- on 900501,inadvertent Manual Safety Injection Occurred Due to Personnel Error.Technician Made Assumption Re Wiring Changes Performed.Train B Wiring Corrected & Deficiency Rept Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-018, :on 900528,control Room Air Intake Radiation Monitoring Sys Monitor Alarm Circuitry Failed & on 900701, Channel 1R1B Failed Resulting in Actuation of ESF Function. Caused by Spurious High Channel Spike |
- on 900528,control Room Air Intake Radiation Monitoring Sys Monitor Alarm Circuitry Failed & on 900701, Channel 1R1B Failed Resulting in Actuation of ESF Function. Caused by Spurious High Channel Spike
| | | 05000272/LER-1990-018-01, :on 900528,ESF Actuation Involving Control Room Ventilation Switch Occurred.Caused by Spurious High Channel Spike.Channel Functional Test Successfully Completed on 900611 |
- on 900528,ESF Actuation Involving Control Room Ventilation Switch Occurred.Caused by Spurious High Channel Spike.Channel Functional Test Successfully Completed on 900611
| 10 CFR 50.73(a)(2) | | 05000311/LER-1990-018, :on 900511,containment Purge/Pressure Vacuum Relief Sys Actuated.Caused by Design/Equipment Failures. Lighting Transformer 2HL Replaced |
- on 900511,containment Purge/Pressure Vacuum Relief Sys Actuated.Caused by Design/Equipment Failures. Lighting Transformer 2HL Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-019-01, :on 900603,main Steam Line Isolation Actuation Occurred & Bistables for Low Steam Line Pressure Logic Tripped.Caused by Equipment/Design Concerns W/Sensing Lines. Design Mods Re Flow Instrumentation Underway |
- on 900603,main Steam Line Isolation Actuation Occurred & Bistables for Low Steam Line Pressure Logic Tripped.Caused by Equipment/Design Concerns W/Sensing Lines. Design Mods Re Flow Instrumentation Underway
| 10 CFR 50.73(a)(2) | | 05000311/LER-1990-019, :on 900511,ESF Actuation Occurred When Radioactive Noble Gas Monitor 2R12A RMS Channel Spiked High. Caused by Equipment/Design Failures.Several Sys Design Mods Will Eliminate Spurious Actuation |
- on 900511,ESF Actuation Occurred When Radioactive Noble Gas Monitor 2R12A RMS Channel Spiked High. Caused by Equipment/Design Failures.Several Sys Design Mods Will Eliminate Spurious Actuation
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-020-01, :on 900608,identified That maint-I&C Procedures for Setting Intermediate Range Excore Nuclear Instrumentation Sys Permissive P-6 Not Correct.Caused by Inadequate Procedure Control |
- on 900608,identified That maint-I&C Procedures for Setting Intermediate Range Excore Nuclear Instrumentation Sys Permissive P-6 Not Correct.Caused by Inadequate Procedure Control
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-020, :on 900512,containment purge/pressure-vacuum Relief Sys Isolation Signal Received from Radiation Monitoring Sys.Caused by Equipment Design Concerns. Uninterruptible Power Supply Installed |
- on 900512,containment purge/pressure-vacuum Relief Sys Isolation Signal Received from Radiation Monitoring Sys.Caused by Equipment Design Concerns. Uninterruptible Power Supply Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-021, :on 900515,radiation Monitoring Sys Channel 2R12A Failed Resulting in ESF Signal Actuation for Containment Purge/Pressure Vacuum Relief Sys Isolation. Caused by Equipment/Design Concerns |
- on 900515,radiation Monitoring Sys Channel 2R12A Failed Resulting in ESF Signal Actuation for Containment Purge/Pressure Vacuum Relief Sys Isolation. Caused by Equipment/Design Concerns
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-021-01, :on 900717,discovered That Work Order Not Issued to Perform Revised Procedure 1IC-16.1.008.Caused by Personnel Error.Event Reviewed by Technical Department Mgt Appropriate Personnel |
- on 900717,discovered That Work Order Not Issued to Perform Revised Procedure 1IC-16.1.008.Caused by Personnel Error.Event Reviewed by Technical Department Mgt Appropriate Personnel
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1990-022-01, :on 900717,observed That Relief Valve 1SJ167 Was Leaking Past Seat as Result of Investigation to Determine Cause of Decreasing Level in Accumulators.Caused by Equipment Failure.Valve Repaired on 900722 |
- on 900717,observed That Relief Valve 1SJ167 Was Leaking Past Seat as Result of Investigation to Determine Cause of Decreasing Level in Accumulators.Caused by Equipment Failure.Valve Repaired on 900722
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-022, :on 900522,radiation Monitoring Sys Channel 2R12A Failed Low.Probably Caused by Equipment/Design Concerns.Anticipates That Several Sys Design Mods Will Eliminate Spurious ESF Actuation Signals |
- on 900522,radiation Monitoring Sys Channel 2R12A Failed Low.Probably Caused by Equipment/Design Concerns.Anticipates That Several Sys Design Mods Will Eliminate Spurious ESF Actuation Signals
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-023, :on 900516,4 Kv Vital Bus Deenergized During 2A Safeguard Equipment Control 18-month Surveillance.Caused by Personnel Error.Personnel Reprimanded & Procedure M3U Revised |
- on 900516,4 Kv Vital Bus Deenergized During 2A Safeguard Equipment Control 18-month Surveillance.Caused by Personnel Error.Personnel Reprimanded & Procedure M3U Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-023-01, :on 900725,discovered That Surveillance of Svc Water Sys Check Valves Not Completed Per Inservice Testing Program Manual Requirements.Caused by Inadequate Administrative Controls.Program Modified |
- on 900725,discovered That Surveillance of Svc Water Sys Check Valves Not Completed Per Inservice Testing Program Manual Requirements.Caused by Inadequate Administrative Controls.Program Modified
| 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1990-024, :on 900521,T-handle Instrument Isolation Valve Discovered Closed,Resulting in Isolation of Liquid Radwaste Effluent Line Monitor 2R18.Caused by Personnel Error.Valve Added to Tagging Request Info Sys Data Base |
- on 900521,T-handle Instrument Isolation Valve Discovered Closed,Resulting in Isolation of Liquid Radwaste Effluent Line Monitor 2R18.Caused by Personnel Error.Valve Added to Tagging Request Info Sys Data Base
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000272/LER-1990-024-01, :on 900728,discovered That Interlock Functions for P-10 & P-12 Permissives Not Fully Tested Per Tech Spec Surveillance 4.3.1.1.2.Caused by Inadequate Administrative Controls.Procedures Revised to Address Testing |
- on 900728,discovered That Interlock Functions for P-10 & P-12 Permissives Not Fully Tested Per Tech Spec Surveillance 4.3.1.1.2.Caused by Inadequate Administrative Controls.Procedures Revised to Address Testing
| | | 05000272/LER-1990-025-01, :on 900806,control Room Air Intake Radiation Sys Monitor Alarm Circuitry Spiked High Resulting in Automatic Switching of Ventilation to Accident Mode of Operation.Addl Spikes Occurred on 900807 & 08 |
- on 900806,control Room Air Intake Radiation Sys Monitor Alarm Circuitry Spiked High Resulting in Automatic Switching of Ventilation to Accident Mode of Operation.Addl Spikes Occurred on 900807 & 08
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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