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Category:Letter
MONTHYEARIR 05000259/20240032024-11-0404 November 2024 Integrated Inspection Report 05000259/2024003 and 05000260/2024003 and 05000296/2024003 CNL-24-043, Application for Subsequent Renewed Operating Licenses, Second Safety Supplement2024-11-0101 November 2024 Application for Subsequent Renewed Operating Licenses, Second Safety Supplement ML24305A1692024-10-31031 October 2024 Site Emergency Plan Implementing Procedure Revision 05000259/LER-2024-003, Valid Specified System Actuation Caused the Automatic Start of Emergency Diesel Generators2024-10-29029 October 2024 Valid Specified System Actuation Caused the Automatic Start of Emergency Diesel Generators 05000259/LER-2024-001-02, Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure2024-10-28028 October 2024 Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure ML24299A2632024-10-25025 October 2024 Response to Apparent Violation in NRC Inspection Report 05000260/2024090, EA-24-075 ML24289A1232024-10-24024 October 2024 Letter to James Barstow Re Environmental Scoping Summary Report for Browns Ferry CNL-24-074, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-10-23023 October 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24308A0042024-10-16016 October 2024 Ahc 24-1578 Environmental Review of the Browns Ferry Nuclear Plant, Units 1, 2 and 3 Subsequent License Renewal Application Limestone County CNL-24-077, Application for Subsequent Renewed Operating Licenses, Response to Request for Additional Information, Set 12024-10-0909 October 2024 Application for Subsequent Renewed Operating Licenses, Response to Request for Additional Information, Set 1 ML24270A2162024-09-27027 September 2024 Notice of Intentions Regarding Preliminary Finding from NRC Inspection Report 05000260/2024090, EA-24-075 CNL-24-060, Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description2024-09-24024 September 2024 Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description ML24262A1502024-09-24024 September 2024 Requalification Program Inspection - Browns Ferry Nuclear Plant ML24262A0602024-09-23023 September 2024 Summary of August 19, 2024, Meeting with Tennessee Valley Authority Regarding a Proposed Supplement to the Tennessee Valley Authority Nuclear Quality Assurance Plan ML24263A2952024-09-19019 September 2024 Site Emergency Plan Implementing Procedure Revision CNL-24-065, Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-09-18018 September 2024 Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions IR 05000260/20240902024-09-17017 September 2024 NRC Inspection Report 05000260/2024090 and Preliminary White Finding and Apparent Violation - 1 CNL-24-062, Cycle 16 Reload Analysis Report2024-09-16016 September 2024 Cycle 16 Reload Analysis Report ML24255A8862024-09-10010 September 2024 Core Operating Limits Report for Cycle 16 Operation, Revision 0 ML24239A3332024-09-0303 September 2024 Full Audit Plan IR 05000259/20244042024-09-0303 September 2024 Cyber Security Inspection Report 05000259/2024404 and 05000260-2024404 and 05000296/2024404-Cover Letter IR 05000259/20240052024-08-26026 August 2024 Updated Inspection Plan for Browns Ferry Nuclear Plant, Units 1, 2 and 3 - Report 05000259/2024005, 05000260/2024005 and 05000296/2024005 ML24225A1682024-08-16016 August 2024 – Notification of Inspection and Request IR 05000259/20244022024-08-0606 August 2024 Security Baseline Inspection Report 05000259/2024402 and 05000260/2024402 and 05000296/2024402 ML24219A0272024-08-0606 August 2024 Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations IR 05000259/20240022024-08-0202 August 2024 Brown Ferry Nuclear Plant – Integrated Inspection Report05000259/2024002 and 05000260/2024002 and 05000296/2024002 ML24199A0012024-07-22022 July 2024 Clarification and Correction to Exemption from Requirement of 10 CFR 37.11(c)(2) ML24172A1342024-07-15015 July 2024 Exemptions from 10 CFR 37.11(C)(2) (EPID L-2023-LLE-0024) - Letter ML24183A4142024-07-10010 July 2024 – License Renewal Regulatory Limited Scope Audit Regarding the Environmental Review of the License Renewal Application (EPID Number: L-2024-SLE-0000) (Docket Numbers: 50-259, 50-260, and 50-296) 05000296/LER-2024-003, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2024-07-0808 July 2024 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000259/LER-2024-001-01, Inoperability of Unit 3 Diesel Generator Due to Relay Failure2024-07-0303 July 2024 Inoperability of Unit 3 Diesel Generator Due to Relay Failure ML24184A1142024-07-0202 July 2024 Site Emergency Plan Implementing Procedure Revision ML24183A3842024-07-0101 July 2024 Registration of Use of Cask to Store Spent Fuel (MPC-364, -365) ML24179A0282024-06-26026 June 2024 Evaluation of Effects of Out-of-Limits Condition as Described in IWB-3720(a) 05000259/LER-2024-002, Reactor Scram Due to Generator Step-Up Transformer Failure2024-06-24024 June 2024 Reactor Scram Due to Generator Step-Up Transformer Failure ML24175A0042024-06-23023 June 2024 Interim Report of a Deviation or Failure to Comply Associated with a Valve in the Unit 3 High Pressure Coolant Injection System ML24176A1132024-06-23023 June 2024 American Society of Mechanical Engineers, Section XI, Fourth 10 Year Inspection Interval, Inservice Inspection, System Pressure Test, Containment Inspection, and Repair and Replacement Programs, Owner’S Activity Report Cycle 21 Oper ML24089A1152024-06-21021 June 2024 Transmittal Letter, Environmental Assessments and Findings of No Significant Impact Related to Exemption Requests from 10 CFR 37.11(c)(2) ML24155A0042024-06-18018 June 2024 Proposed Alternative to the Requirements of the ASME Code (Revised Alternative Request 0-ISI-47) ML24158A5312024-06-0606 June 2024 Registration of Use of Cask to Store Spent Fuel (MPC-361, -362, -363) ML24071A0292024-06-0505 June 2024 Subsequent License Renewal Application Enclosure 3 - Proprietary Determination Letter ML24068A2612024-06-0505 June 2024 SLRA Fluence Methodology Report - Proprietary Determination Letter IR 05000259/20244032024-05-22022 May 2024 – Security Baseline Report 05000259/2024403 and 05000260/2024403 and 05000296/2024403 05000260/LER-2024-002, High Pressure Coolant Injection Inoperable Due to Rupture Disc Failure and Resulting System Isolation2024-05-20020 May 2024 High Pressure Coolant Injection Inoperable Due to Rupture Disc Failure and Resulting System Isolation ML24141A0482024-05-17017 May 2024 EN 56958_1 Ametek Solidstate Controls, Inc ML24136A0702024-05-15015 May 2024 2023 Annual Radiological Environmental Operating Report IR 05000259/20240012024-05-14014 May 2024 Integrated Inspection Report 05000259/2024001, 05000260/2024001, and 05000296/2024001 CNL-24-040, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-05-0808 May 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24123A2012024-05-0202 May 2024 NRC Cybersecurity Baseline Inspection (NRC Inspection Report 05000259/2024404, 05000260-2024404, 05000296/2024404) and Request for Information ML24122A6852024-05-0101 May 2024 2023 Annual Radioactive Effluent Release Report and Offsite Dose Calculation Manual 2024-09-03
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000259/LER-2024-003, Valid Specified System Actuation Caused the Automatic Start of Emergency Diesel Generators2024-10-29029 October 2024 Valid Specified System Actuation Caused the Automatic Start of Emergency Diesel Generators 05000259/LER-2024-001-02, Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure2024-10-28028 October 2024 Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure 05000296/LER-2024-003, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2024-07-0808 July 2024 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000259/LER-2024-001-01, Inoperability of Unit 3 Diesel Generator Due to Relay Failure2024-07-0303 July 2024 Inoperability of Unit 3 Diesel Generator Due to Relay Failure 05000259/LER-2024-002, Reactor Scram Due to Generator Step-Up Transformer Failure2024-06-24024 June 2024 Reactor Scram Due to Generator Step-Up Transformer Failure 05000260/LER-2024-002, High Pressure Coolant Injection Inoperable Due to Rupture Disc Failure and Resulting System Isolation2024-05-20020 May 2024 High Pressure Coolant Injection Inoperable Due to Rupture Disc Failure and Resulting System Isolation 05000296/LER-2024-002, Breaker Trip Automatically Started an Emergency Diesel Generator2024-04-24024 April 2024 Breaker Trip Automatically Started an Emergency Diesel Generator 05000296/LER-2024-001, Primary Containment Isolation Valve Inoperable Due to Incorrect Motor Operated Valve Setup2024-04-22022 April 2024 Primary Containment Isolation Valve Inoperable Due to Incorrect Motor Operated Valve Setup 05000260/LER-2024-001-01, Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure2024-04-17017 April 2024 Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure 05000259/LER-2024-001, Inoperability of Unit 3 Diesel Generator Due to Relay Failure2024-04-11011 April 2024 Inoperability of Unit 3 Diesel Generator Due to Relay Failure 05000260/LER-2024-001, Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure2024-02-16016 February 2024 Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure 05000259/LER-2023-003, Standby Liquid Control Inoperable Due to Demineralized Water In-Leakage2024-01-29029 January 2024 Standby Liquid Control Inoperable Due to Demineralized Water In-Leakage 05000259/LER-2022-002-01, High Pressure Coolant Injection System Declared Inoperable Due to a Corroded Actuator2023-10-12012 October 2023 High Pressure Coolant Injection System Declared Inoperable Due to a Corroded Actuator 05000260/LER-2023-001-01, Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line Due to Fatigue Failure2023-09-18018 September 2023 Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line Due to Fatigue Failure 05000260/LER-2023-002, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2023-08-0404 August 2023 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000296/LER-2022-003-01, Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line Due to Fatigue Failure2023-07-31031 July 2023 Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line Due to Fatigue Failure 05000259/LER-2023-002, Full Reactor Scram Due to an Oscillation Power Range Monitor (OPRM) Confirmation Density Algorithm (CDA) Trip2023-07-17017 July 2023 Full Reactor Scram Due to an Oscillation Power Range Monitor (OPRM) Confirmation Density Algorithm (CDA) Trip 05000259/LER-2023-001-01, High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm2023-06-13013 June 2023 High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm 05000260/LER-2023-001, Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line2023-04-19019 April 2023 Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line 05000259/LER-2023-001, High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm2023-03-27027 March 2023 High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm 05000259/LER-1922-003, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2023-02-0606 February 2023 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000296/LER-2022-003, Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line2023-01-31031 January 2023 Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line 05000296/LER-2022-002, Both Standby Liquid Control Subsystems Inoperable Due to an Insufficient Boron Injection Rate2022-12-19019 December 2022 Both Standby Liquid Control Subsystems Inoperable Due to an Insufficient Boron Injection Rate 05000259/LER-2022-002, High Pressure Coolant Injection System Declared Inoperable Due to a Corroded Actuator2022-09-12012 September 2022 High Pressure Coolant Injection System Declared Inoperable Due to a Corroded Actuator 05000296/LER-2022-001, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2022-07-11011 July 2022 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000259/LER-2021-001-01, Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications Due to Failed Relay2022-07-0606 July 2022 Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications Due to Failed Relay 05000259/LER-2022-001, From Browns Ferry Nuclear Plant, Unit 1 Regarding Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line2022-03-16016 March 2022 From Browns Ferry Nuclear Plant, Unit 1 Regarding Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line 05000259/LER-2021-001, Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications Due to Failed Relay2021-11-22022 November 2021 Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications Due to Failed Relay ML20160A0232020-06-0404 June 2020 SR 2020-001-00 for Browns Ferry Nuclear Plant (Bfn),Inoperable Oscillating Power Range Monitor (OPRM) Instrumentation 05000296/LER-2017-0022017-12-29029 December 2017 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses, LER 17-002-00 for Browns Ferry Nuclear Plant, Unit 3 Regarding 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses 05000296/LER-2017-0012017-10-31031 October 2017 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications, LER 17-001-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications 05000260/LER-2017-0042017-07-0707 July 2017 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 17-004-00 for Browns Ferry, Unit 2, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000260/LER-2017-0032017-05-30030 May 2017 Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting, LER 17-003-00 for Browns Ferry Nuclear Plant, Unit 2 Regarding Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting 05000259/LER-2017-0022017-04-27027 April 2017 Unauthorized Firearm Introduced into the Protected Area, LER 17-002-00 for Browns Ferry, Unit 1, Regarding Unauthorized Firearm Introduced into the Protected Area 05000260/LER-2017-0022017-04-24024 April 2017 Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications, LER 17-002-00 for Browns Ferry, Unit 2, Regarding Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications 05000260/LER-2017-0012017-04-14014 April 2017 High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse, LER 17-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse 05000259/LER-2016-0022016-09-19019 September 2016 High Pressure Coolant Injection Safety System Functional Failure due to Inoperability of Primary Containment Isolation Valve, LER 16-002-00 for Browns Ferry, Unit 1, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to Inoperability of Primary Containment Isolation Valve 05000260/LER-2016-0022016-09-13013 September 2016 High Pressure Coolant Injection System Failure Due To Stuck Contactor, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 2, Regarding High Pressure Coolant Injection System Failure Due To Stuck Contactor 05000260/LER-2016-0012016-08-16016 August 2016 High Pressure Coolant Injection Safety System Functional Failure due to a Blown Fuse and a Failed Relay, LER 16-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse and a Failed Relay 05000296/LER-2016-0062016-08-0505 August 2016 1 OF 8, LER 16-006-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding High Pressure Coolant Injection System Found to be Inoperable During Testing 05000259/LER-2016-0012016-06-21021 June 2016 Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves, LER 16-001-00 for Browns Ferry, Unit 1, Regarding Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves 05000296/LER-2016-0052016-06-17017 June 2016 Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits, LER 16-005-00 for Browns Ferry, Unit 3, Regarding Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits 05000296/LER-2016-0042016-06-0606 June 2016 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 16-004-00 for Browns Ferry, Unit 3, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000296/LER-2016-0032016-04-25025 April 2016 Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements, LER 16-003-00 for Browns Ferry Nuclear Plant Unit 3 Regarding Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements 05000296/LER-2016-0022016-04-22022 April 2016 Improperly Installed Switch Results in Condition Prohibited by Technical Specifications, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Improperly Installed Switch Results in Condition Prohibited by Technical Specifications 05000296/LER-2016-0012016-03-21021 March 2016 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure, LER 16-001-00 for Browns Ferry, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure 05000260/LER-2015-0022016-03-17017 March 2016 High Pressure Coolant Injection System Inoperable due to Manual Isolation of Steam Leak I, LER 15-002-01 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection System Inoperable Due to Manual Isolation of Steam Leak ML1108400352011-03-22022 March 2011 Letter Re Licensee Event Report Which Occurred on December 22, 2010, Concerning Low Pressure Coolant Injection Operability, TVA Expects to Submit a Revised LER by April 15, 2011 ML1015505752010-04-0707 April 2010 Event Notification for Browns Ferry on Spill of Water Containing Tritium ML1015505632008-01-10010 January 2008 Event Notification for Browns Ferry on Offsite Notification - Spill of Water Containing Tritium 2024-07-08
[Table view] |
text
Post Office Box 2000, Decatur, Alabama 35609-2000
September 18, 2023 10 CFR 50.73
ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001
Browns Ferry Nuclear Plant, Unit 2 Renewed Facility Operating License No. DPR-52 NRC Docket No. 50-260
Subject: Licensee Event Report 50-260/2023-001-01
References: 1. Non-Emergency Event Notification 56371 - Degraded Condition
- 2. Letter from TVA to NRC, Licensee Event Report 50-260/2023-001-00, dated April 19, 2023 (ML23109A362)
The enclosed Licensee Event Report provides details of a pressure boundary leak on Browns Ferry Nuclear Plant, Unit 2. The Tennessee Valley Authority is submitting this report in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 50.73(a)(2)(i)(B), as any operation or condition which was prohibited by the plants Technical Specifications; and 10 CFR 50.73(a)(2)(ii)(A), as any event or condition that resulted in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.
There are no new regulatory commitments contained in this letter. Should you have any questions concerning this submittal, please contact David J. Renn, Nuclear Site Licensing Manager, at (256) 729-2636.
Respectfully,
Manu SivaramanMSi Site Vice President
Enclosure: Licensee Event Report 50-260/20 23-001 Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line Due to Fatigue Failure
cc (w/ Enclosure):
U.S. Nuclear Regulatory Commission Page 2 September 18, 2023
NRC Regional Administrator - Region II NRC Senior Resident Inspector - Browns Ferry Nuclear Plant NRC Project Manager - Browns Ferry Nuclear Plant ENCLOSURE
Browns Ferry Nuclear Plant Unit 2
Licensee Event Report 50-260/2023-001-01
Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line Due to Fatigue Failure
See Enclosed
Abstract
On February 17, 2023, during a drywell entry for leak identification, Browns Ferry Nuclear Plant (BFN) personnel discovered a cracked weld on the 2A Recirculation Pump discharge isolation valve drain line. On February 18, 2023, at 0439 Central Standard Time (CST), it was determined that this drain line was classified as American Society of Mechanical Engineers Code Class I piping and constitutes part of the BFN, Unit 2 Reactor Coolant System (RCS) pressure boundary. On February 18, 2023, at 1025 CST, eight-hour Event Notification 56371 was made to the NRC. On March 19, 2023, work was completed to remove and replace the drain line.
The root cause of this event was that small bore piping was not analyzed for vulnerability of fatigue failure due to operational or resonance vibration. Corrective actions are to implement changes that will result in bounded life cycles for all levels of vibrational stress that the piping will experience; and to implement additional actions, for Unit 2 systems where failure of small bore branch piping would cause a unit shutdown or loss of RCS boundary, to modify the operating ranges of the system and/or the piping assembly. TVA has concluded that sufficient systems were available to provide the required safety functions needed to protect the health and safety of the public.
I. Plant Operating Conditions before the Event
At the time of discovery, Browns Ferry Nuclear Plant (BFN) Unit 2 was in Mode 4 at approximately zero percent power.
II. Description of Event
A. Event Summary
On February 17, 2023, during a drywell entry for leak identification, BFN personnel di scovered a cracked weld on the 2A Recirculation Pump [AD] discharge isolation valve [ISV] drain line
[PSF]. On February 18, 2023, at 0439 Central Standard Time (CST), it was determined that this drain line was classified as American Society of Mechanical Engineers (ASME) Code Class I piping and constitutes part of the BFN, Unit 2 Reactor Coolant System (RCS) pr essure boundary. Operations personnel maintained BFN, Unit 2 in Mode 4 or 5 until the le ak was repaired. On February 18, 2023, at 1025 CST, eight-hour Event Notification 56371 was made to the NRC. On March 19, 2023, work was completed to remove and replace the drain line.
The TVA is submitting this report in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 50.73(a)(2)(i)(B), as any operation or condition which was proh ibited by the plants Technical Specifications (TS); and 10 CFR 50.73(a)(2)(ii)(A), as any even t or condition that resulted in the condition of the nuclear power plant, including its prin cipal safety barriers, being seriously degraded.
B. Status of structures, components, or systems that were inoperable at the start of the event and that contributed to the event
There were no structures, systems, or components (SSCs) whose inoperability cont ributed to this event.
C. Dates and approximate times of occurrences
Date Time (CST) Occurrence February 18, 2023 0439 Determined that leaking piping was ASME Code Class I.
February 18, 2023 1025 Made eight-hour EN 56371 to NRC.
March 14, 2023 1611 Completed WO 123487635 to repair leaking drain line.
March 19, 2023 2342 Declared BFN Unit 2 RCS structural integrity operable
D. Manufacturer and model number of each component that failed during the event
There were no failed components related to this event.
E. Other systems or secondary functions affected
No other systems or secondary functions were affected.
F. Method of discovery of each component or system failure or procedural error
During the planned outage on BFN Unit 2, personnel entered the drywell for leak identification and discovered a cracked weld on the 2A Recirc pump discharge isolation valve drain line. An engineering evaluation determined this line to be ASME Code Class I Piping.
G. The failure mode, mechanism, and effect of each failed component
Testing performed by Westinghouse determined that, for a previous similar event on BFN Unit 1, the pipe failed due to vibration induced high cycle fatigue originating at the outside diameter of the pipe where the valve and socket welds overlap. A Significant Issue Gap Analysis (SIGA) concluded that the piping involved in this event most likely failed by the same mechanism.
H. Operator actions
There were no operator actions related to this event.
I. Automatically and manually initiated safety system responses
There were no automatic or manual safety system responses during this event.
III. Cause of the event
The root cause of this event was that small bore piping was not specifically analyzed for vulnerability of fatigue failure due to operational or resonance vibration. During original plant design, there was not an accurate method for modeling or collecting vibration data in order to evaluate the effects on small bore piping. When data collection became available, this branch line was erroneously excluded from further evaluation.
Additionally, the following contributing cause was identified for this event:
During evaluations performed during Extended Power Uprate (EPU), the small bore piping was considered rigid in the seismic calculation, which are typically limited to frequencies below 35 Hz, and therefore did not need to be modeled separately from the large bore piping. That assessment was carried into the vibration acceptance calculation, and then into the vibration analysis report as the basis for acceptability of the measured vibration. This resulted in small bore piping not being evaluated independently from the large bore piping during EPU testing. When modeled independently with an accurate fatigue stress input, bounded vibration cycles no longer apply.
The design calculation failed to identify that the stress caused by flow induced resonance vibration at Recirculation System [AD] Pump speeds between 1500 and 1600 rpm was sufficient to exceed the endurance limit for the failed pipe assembly.
A. Cause of each component or system failure or personnel error
There were no component failures, system failures, or personnel errors associated with this event.
B. Cause(s) and circumstances for each human performance related root cause
There were no human performance related root causes associated with this event.
IV. Analysis of the event
The Radioactive Material Barrier is the systems, structures, or equipment that, together, physically prevent the uncontrolled release of radioactive materials. One of these is the Nuclear System Process Barrier, made up of a Primary Barrier and a Secondary Barrier, which includes the systems of vessels, pipes, pumps, tubes, and similar process equipment that contain the steam, water, gases, and radioactive materials coming from, going to, or in communication with the reactor core. The Primary Barrier, also known as the Reactor Coolant Pressure Boundary, consists of the reactor vessel and attached piping out to and including the second isolation valve in each attached pipe. A leak in the Pressure Boundary is therefore a degradation of one of the nuclear power plants principal safety barriers.
BFN, Unit 2 TS Limiting Condition for Operation (LCO) 3.4.4, RCS Operational Leakage, requires that there be no pressure boundary leakage while in Modes 1, 2, or 3. TS LCO 3.4.4 Condition C requires, when any pressure boundary leakage exists, that the unit be in Mode 3 within twelve hours, and Mode 4 within thirty-six hours. A Past Operability Evaluation (POE) determined that this condition is likely to have existed since November 13, 2022, when an increase in unidentified drywell leakage from the RCS was detected. Pressure boundary leakage likely existed from this time until February 17, 2023, when BFN, Unit 2 was placed in Mode 4.
V. Assessment of Safety Consequences
The POE for this event determined that the safety significance was low because, per Calculation MDQ0999950033 Rev. 3, Exclusion Criteria for ISI Scope, the normal reactor coolant makeup systems, Reactor Core Isolation Cooling, Feedwater, and Control Rod Drive, have adequate capacity to makeup reactor coolant in the worst-case scenario of a small break Loss of Coolant Accident (LOCA). Additionally, Calculation NDQ0074880118 Rev.8, Evaluation of LPCI Flow to RPV with Failed Open Min Flow Bypass Valve shows that the Low Pressure Coolant Injection (LPCI) mode of the Residual Heat Removal (RHR) system can still meet the required LPCI flow to the RPV in the worse-case scenario of a small break LOCA for the duration of its mission time.
During this time the High Pressure Coolant Injection system [BJ], both loops of the Core Spray system (CS) [BG], and all Automatic Depressurization System valves remained operable when required, aside from periods of planned maintenance and testing, and were available to provide coolant flow to the core during an emergency.
Based on the above, the TVA has concluded that sufficient systems were available to provide the required safety functions needed to protect the health and safety of the public.
A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event
There were no systems or components other than the RCS Pressure Boundary that failed during the event.
B. For events that occurred when the reactor was shut down, availability of systems or components needed to shutdown the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident
During the period concurrent with this event where BFN, Unit 2 was in Mode 4 or Mode 5, all systems or components required to shutdown the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident in Mode 4 or Mode 5 remained operable, aside from periods of planned maintenance and testing.
C. For failure that rendered a train of a safety system inoperable, estimate of the elapsed time from discovery of the failure until the train was returned to service
This event did not result in the inoperability of any safety system train.
VI. Corrective Actions
Corrective Actions are being managed by the TVAs corrective action program under Condition Reports (CRs) 1836572 and 1747875.
A. Immediate Corrective Actions
The immediate corrective action for this event was to repair the valves drain line under Work Order 123487635.
B. Corrective Actions to Prevent Recurrence or to reduce the probability of similar events occurring in the future
- 1. Implement an Engineering Change Package (ECP) for the test line that will result in bounded life cycles for all levels of stress that the piping assembly will experience.
- 2. Implement additional actions for Unit 2 systems containing small bore branch piping that would cause a unit shutdown or loss of RCS boundary if it failed, to either modify operating ranges of the system or modify the piping assembly or both if the natural frequency of the piping assembly is within the operating vibration band of the piping assembly or if the operating vibration level exceeds the acceptable vibration level.
VII. Previous Similar Events at the Same Site
There are two similar events which have occurred at BFN within the last two years:
- 1. On January 15, 2022, at 2320 CST, during a drywell entry for leak identification, BFN Engineering personnel discovered a through-wall piping leak on a test line upstream of the RHR and Shutdown Cooling DC test shut-off valve. This test line is classified as ASME Code Class 1 piping and constitutes part of the BFN, Unit 1 RCS pressure boundary.
Operations personnel declared the BFN, Unit 1 system LPCI Loop I inoperable and maintained BFN, Unit 1 in Mode 4 or 5 until the leak was repaired. On January 16, 2022, at 0541 CST, eight-hour EN 55706 was made to the NRC. The test line was cut and capped pending permanent repairs, and on January 20, 2022, at 1520 CST, BFN, Unit 1 LPCI Loop I was declared operable.
This event was reported to the NRC under Licensee Event Report (LER) 50-259/2022-001 Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line.
- 2. On December 2, 2022, at 2330 CST, during a drywell entry for leak identification, BFN Engineering personnel discovered a through-wall piping leak on a test line between the two RHR Shutdown Cooling test line isolation valves. On December 3, 2022, at 1000 CST, it was determined that this test line was classified as ASME Code Class 1 piping and constitutes part of the BFN, Unit 3 RCS pressure boundary. Operations personnel maintained BFN, Unit 3 in Mode 4 or 5 until the leak was repaired. On December 3, 2022, at 1205 CST, eight-hour Event Notification56257 was made to the NRC. The test line was cut and capped pending permanent repairs.
This event was reported to the NRC under LER 50-296/2022-003 Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line
The root cause of both of these events was small bore piping which was not specifically analyzed for fatigue failure vulnerability due to operational or resonance vibration. The corrective action for both of these events is to implement ECPs for small bore piping with vulnerability to fatigue failure due to exceeding the endurance limit due to operational vibration.
VIII. Additional Information
There is no additional information.
IX. Commitments
There are no new commitments.
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05000260/LER-2023-001-01, Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line Due to Fatigue Failure | Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line Due to Fatigue Failure | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000259/LER-2023-001-01, High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm | High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000260/LER-2023-001, Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line | Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000259/LER-2023-001, High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm | High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000260/LER-2023-002, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints | Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000259/LER-2023-002, Full Reactor Scram Due to an Oscillation Power Range Monitor (OPRM) Confirmation Density Algorithm (CDA) Trip | Full Reactor Scram Due to an Oscillation Power Range Monitor (OPRM) Confirmation Density Algorithm (CDA) Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000259/LER-2023-003, Standby Liquid Control Inoperable Due to Demineralized Water In-Leakage | Standby Liquid Control Inoperable Due to Demineralized Water In-Leakage | 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
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