07-28-2016 | On May 30, 2016, at 0930 PDT, with Unit 2 in Mode 4, "Hot Shutdown," licensed operators responding to a difference greater than 12 steps between digital rod position indication (DRPI) and demand position indication in the control room, manually opened the Reactor Trip Breakers in accordance with plant procedures. The plant operators stabilized the plant and technicians identified a failure of a control rod moveable gripper fuse. At 1611 PDT, plant operators made an 8-hour, nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A). Plant technicians replaced the fuse and plant operators confirmed proper operation by performance of surveillance testing.
The cause was attributed to Surveillance Test Procedure (STP) R-1C, "Digital Rod Position Indicator Functional Test," which did not explicitly specify actions to identify improper DRPI indications prior to exceeding a 12-step difference between rod demand and rod position indication.
Corrective actions to prevent recurrence include revision of STP R-1C to include guidance regarding verification of rod motion prior to exceeding 12 steps and operator training of the changes to the procedure.
This event did not adversely affect the health and safety of the public.
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 205550001, or by e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. |
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Category:Letter
MONTHYEARIR 05000275/20230042024-02-0909 February 2024 Integrated Inspection Report 05000275/2023004 and 05000323/2023004 ML24002B1802024-01-29029 January 2024 LRA Audit Plan DCL-24-010, Nuclear Material Transaction Report for New Fuel2024-01-29029 January 2024 Nuclear Material Transaction Report for New Fuel ML24018A0152024-01-29029 January 2024 License Renewal Application Review Schedule Letter ML24017A2492024-01-24024 January 2024 Letter to Neil Peyron, Chairman, Tule River Tribe, Re. Diablo Canyon ML24024A1752024-01-24024 January 2024 Letter to Tribal Council San Luis Obispo County Chumash Indians on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24003A8902024-01-24024 January 2024 Letter to P. Gerfen - Diablo Canyon Notice of Intent to Conduct Scoping and Prepare an Environmental Impact Statement ML24012A1582024-01-24024 January 2024 Letter to Hon. Violet Sage Walker, Chairwoman Northern Chumash Tribal Council on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24012A0062024-01-24024 January 2024 Achp Scoping Letter for Diablo Canyon License Renewal ML24012A0552024-01-24024 January 2024 Letter to J. Polanco, Shpo, on Request to Initiate Section 106 Consultation and Scooping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24024A1562024-01-24024 January 2024 Letter to Hon. Gabe Frausto, Coastal Band of Chumash Indians on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24024A1652024-01-24024 January 2024 Letter to Hon. Mona Olivas Tucker, Yak Tityu Tityu Yak Tilhini Northern Chumas Indians on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24024A1612024-01-24024 January 2024 Letter Hon. Gary Pierce, Salian Tribe of Monterey and San Luis Obispo Counties on Section 106 Consultation and Scoping Process for the Environmental Review of Diablo Canyon Nuclear Plant, Unit 1 and 2 License Renewal Application ML24012A0362024-01-24024 January 2024 Request to Initiate Section 106 Consultation and Scoping Process for the Environmental Review License Renewal Application DCL-24-009, Nuclear Material Transaction Report for New Fuel2024-01-17017 January 2024 Nuclear Material Transaction Report for New Fuel DCL-24-008, Schedule Considerations for Review of the DCPP License Renewal Application2024-01-17017 January 2024 Schedule Considerations for Review of the DCPP License Renewal Application DCL-24-004, Supplement to License Amendment Request 23-01 Revision to Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b2024-01-15015 January 2024 Supplement to License Amendment Request 23-01 Revision to Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b IR 05000275/20230112024-01-12012 January 2024 NRC License Renewal Phase 1 Inspection Report 05000275/2023011 DCL-23-129, Nuclear Material Transaction Report for New Fuel2023-12-27027 December 2023 Nuclear Material Transaction Report for New Fuel ML23326A0122023-12-21021 December 2023 12-21-23 Letter to the Honorable Byron Donalds from Chair Hanson Responds to Letter Regarding 2.206 Petition to Close Diablo Canyon Nuclear Power Plant, Unit 1 ML23341A0042023-12-19019 December 2023 LRA Acceptance Letter ML23352A2342023-12-18018 December 2023 Notification of Age-Related Degradation Inspection (05000275/2024014 and 05000323/2024014) and Request for Information DCL-23-122, Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-12-14014 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation DCL-23-128, Emergency Plan Update2023-12-13013 December 2023 Emergency Plan Update ML23355A0952023-12-0808 December 2023 License Renewal Application Online Reference Portal DCL-23-125, Core Operating Limits Report for Unit 1 Cycle 252023-12-0606 December 2023 Core Operating Limits Report for Unit 1 Cycle 25 ML23291A2702023-11-28028 November 2023 Letter to Nakia Zavalla, Shpo, the Santa Ynez Band of Chumash Indians; Re., Diablo Canyon ISFSI Initiating Section 106 Consultation ML23320A2442023-11-28028 November 2023 Letter to Kerri Vera, Director of Department of Environmental Protection, Tule River Tribe; Re., Diablo Canyon ISFSI Initiating Section 106 Consultation ML23325A1382023-11-27027 November 2023 ISFSI Tribal Letter to San Luis Obispo County Chumash Indians ML23325A1322023-11-27027 November 2023 ISFSI Tribal Letter to Salian Tribe of Montgomery, San Luis Obispo ML23325A1332023-11-27027 November 2023 ISFSI Tribal Letter to Yak Tityu Tityu Northern Chumash Indians ML23307A0062023-11-27027 November 2023 ISFSI Tribal Letter to Northern Chumash Tribal Council ML24003A7242023-11-27027 November 2023 Independent Safety Committee; Diab Lo Canyon Nuclear Power Plant Operations, Thirty-Third Annual Report on the Safety ML23325A1292023-11-27027 November 2023 ISFSI Tribal Letter to Coastal Band of Chumash ML23320A1502023-11-17017 November 2023 Individual Notice of Consideration of Issuance of Amendment to Facility Operating License, Proposed No Significant Hazards Consideration Determination, & Opportunity for Hearing (Exigent Circumstances) (EPID L-2023-LLA-0155) - LTR DCL-23-121, Supplement to License Amendment Request 23-03, Revision to Technical Specification3.7.8, Auxiliary Saltwater System2023-11-16016 November 2023 Supplement to License Amendment Request 23-03, Revision to Technical Specification3.7.8, Auxiliary Saltwater System ML23296A0982023-11-15015 November 2023 Notification and Request for Consultation Regarding Pacific Gas and Electric Diablo Canyon Independent Spent Fuel Storage Installation Material License Renewal Request (Docket Number: 72-26) DCL-23-120, License Amendment Request 23-03 Revision to Technical Specification 3.7.8, Auxiliary Saltwater (Asw) System2023-11-14014 November 2023 License Amendment Request 23-03 Revision to Technical Specification 3.7.8, Auxiliary Saltwater (Asw) System ML23293A1052023-11-14014 November 2023 Receipt and Availability of License Renewal Application IR 05000275/20230032023-11-13013 November 2023 Integrated Inspection Report 05000275/2023003 and 05000323/2023003 ML23311A2082023-11-0909 November 2023 Reassignment of U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch IV DCL-23-118, License Renewal Application2023-11-0707 November 2023 License Renewal Application ML23318A2102023-10-31031 October 2023 Independent Safety Committee; Thirty-Third Annual Report on the Safety of Diablo Canyon Nuclear Power Plant Operations DCL-2023-520, Discharge Self-Monitoring at Diablo Canyon Power Plant (DCPP)2023-10-19019 October 2023 Discharge Self-Monitoring at Diablo Canyon Power Plant (DCPP) DCL-23-103, Independent Spent Fuel Storage Installation - Withdrawal of License Amendment Request 22-01, Request for Approval of Alternative Security Measures for Early Warning System2023-10-13013 October 2023 Independent Spent Fuel Storage Installation - Withdrawal of License Amendment Request 22-01, Request for Approval of Alternative Security Measures for Early Warning System IR 05000275/20240152023-10-10010 October 2023 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection (050002752024015 and 050003232024015) 2024-02-09
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000323/LER-2017-0012017-10-0303 October 2017 Relief Valve Leakage Resulting in Inoperable Pressurizer Power Operated Relief Valve, LER 17-001-00 for Diablo Canyon, Unit 2, Regarding Relief Valve Leakage Resulting in Inoperable Pressurizer Power Operated Relief Valve 05000323/LER-2016-0012016-07-28028 July 2016 Reactor Trip Breakers Manually Opened During Shutdown Due to a Control Rod Movable Gripper Fuse Failure, LER 16-001-00 for Diablo Canyon, Unit 2, Regarding Reactor Trip Breakers Manually Opened During Shutdown Due to a Control Rod Movable Gripper Fuse Failure 05000275/LER-2015-0012016-02-11011 February 2016 Both Trains of Residual Heat Removal Inoperable Due to Circumferential Crack on a Socket Weld, LER 15-001-01 for Diablo Canyon, Unit 1, Regarding Both Trains of Residual Heat Removal Inoperable Due to Circumferential Crack on a Socket Weld DCL-15-042, Supplemental Licensee Event Report 1-2014-004-01 for Diablo Canyon, Units 1 and 2 Regarding Actuation of Six Emergency Diesel Generators Due to Loss of Offsite Power2015-03-30030 March 2015 Supplemental Licensee Event Report 1-2014-004-01 for Diablo Canyon, Units 1 and 2 Regarding Actuation of Six Emergency Diesel Generators Due to Loss of Offsite Power DCL-15-041, Supplemental LER 2-13-004-01 for Diablo Canyon, Unit 2 Regarding Technical Specification 3.8.1 Not Met Due to Failed Wire Lug on Emergency Diesel Generator 2-32015-03-30030 March 2015 Supplemental LER 2-13-004-01 for Diablo Canyon, Unit 2 Regarding Technical Specification 3.8.1 Not Met Due to Failed Wire Lug on Emergency Diesel Generator 2-3 DCL-13-034, Licensee Event Report 12-005-00 for Diablo Canyon Regarding Expected Submittal Date2013-04-0101 April 2013 Licensee Event Report 12-005-00 for Diablo Canyon Regarding Expected Submittal Date DCL-11-118, LER 11-05-001 for Diablo Canyon Unit 1, Emergency Diesel Generator Actuations Upon Loss of 230 Kv Startup Due to Electrical Maintenance Testing Activities2011-11-0808 November 2011 LER 11-05-001 for Diablo Canyon Unit 1, Emergency Diesel Generator Actuations Upon Loss of 230 Kv Startup Due to Electrical Maintenance Testing Activities DCL-11-119, LER 11-04-001 for Diablo, Unit 1, Regarding Emergency Diesel Generator Actuated Upon 230 Kv Isolation Due to Maintenance Activities on Relay Panel2011-11-0808 November 2011 LER 11-04-001 for Diablo, Unit 1, Regarding Emergency Diesel Generator Actuated Upon 230 Kv Isolation Due to Maintenance Activities on Relay Panel 2017-10-03
[Table view] |
L Reportable Event Classification This event is reportable pursuant to 10 CFR 50.73(a)(2)(iv)(A), System Actuation.
II. Plant Conditions
Unit 2 was in Mode 4, Hot Shutdown, preparing for restart following the nineteenth refueling outage (2R19).
Ill. Description of Problem
A. Background
The rod control system [AA] is a Design Class II system for positioning the reactor control rods for reactor power modulation by manual or automatic control of control rod banks. The rod control system is provided motive power through the redundant Design Class I Reactor Trip breakers that open to perform the safety-related function of rod insertion by removing all motive power to the control rod drive mechanism. The rod group demand position indication is located in the control room on the control board and indicates the individual rod position demands made for rod motion.
The digital rod position indication (DRPI) system measures the position of the control rod drive mechanism shafts within the control rod drive housings so that the positions of the control rods within the core are verified.
Equipment Control Guideline (ECG) 41.2, "Special Test Exceptions - Position Indication System — Shutdown", requires that position indication systems be operable when the reactor trip breakers are closed. With less than the above required position indication systems operable, the reactor trip breakers are required to be immediately opened. Surveillance Requirement (SR) 41.2.1 requires verification "that the demand position indication system and the DRPI system agree within 12 steps when rods are stationary.
Surveillance Test Procedure (STP) R-1C, "Digital Rod Position Indicator Functional Test," verifies the OPERABILITY of the DRPI System. The rod banks are individually withdrawn in 24 step increments while a comparison is made between the DRPI indication and the demand step counter for each rod. When the bank is fully withdrawn, it is then inserted to the rod bottom light emitting diode (LED) point and the position at which each rod bottom LED was actuated is recorded.
B. Event Description
During plant restart following 2R19, plant operators initiated DRPI operability testing of Shutdown Bank A in accordance with STP R-1C.
On May 30, 2016, at 0930 PDT with Unit 2 in Mode 4, licensed operators responded to an indicated difference between the Rod B4 demand position indication and DRPI indication greater than 12 steps and initiated manual opening of the reactor trip breakers in accordance with plant procedures.
On May 30, 2016, at 1611 PDT, operations made an 8-hour, nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A).
C. Status of Inoperable Structures, Systems, or Components that Contributed to the Event Control rod moveable gripper fuse (FU49) for Rod B4 was open.
D. Other Systems or Secondary Functions Affected
None.
E. Method of Discovery
The condition was discovered during the performance of STP R-1C as required by plant ECG 41.2.
F. Operator Actions
Licensed operators initiated manual opening of the reactor trip breakers removing motive power from the rod control system in accordance with plant procedures.
G. Safety System Responses
Unit 2 rod control system was deactivated by opening the reactor trip breakers, which deenergized the gripper circuits and control rods that were withdrawn then reinserted into the core as designed.
III. Cause of the Problem
A. Immediate Cause
The rod control demand position indication and DRPI had an observed difference of 14 steps, requiring the immediate opening of the reactor trip breakers.
B. Cause
A failure of the Rod B4 moveable gripper fuse (FU49) prevented Rod B4 from movement upon demand. This caused the Rod B4 to remain at the core bottom as indicated by the DRPI system while the demand counter counted up to 14 steps.
Gripper coil fuses are replaced every refueling outage to prevent failure due to cyclic fatigue. Handling and installation stress can weaken fuses and cause them to fail when first energized. These issues are detected when post maintenance testing is performed.
STP R-1C, Revision 21, did not explicitly specify actions to identify improper DRPI indications prior to exceeding a 12 step difference between rod demand and rod position indication. STP R-1C, Revision 17, dated March 19, 2009, had steps to withdraw the rod bank to 10 steps and then check rod control fuse integrity. These steps were added to STP R-1C, as a corrective action to a previous Licensee Event Report (LER) 2-2003-004-00.
Subsequently, this step was removed in Revision 18 of the procedure dated July 14, 2009. If this step had been in STP R-1C at the time of the event, the faulted fuse would have been detected prior to exceeding the 12-step limit and a manual opening of the reactor trip breakers would not have been required.
IV. Assessment of Safety Consequences
Procedure controlled pre-operation testing discovered the inoperable system prior to pulling more than one shutdown bank. A control rod moveable gripper fuse (FU49) was identified as failed open preventing Rod B4 from being moved, thus, no unanticipated positive reactivity change was possible. At the time of this event, the boron concentration in the reactor coolant system was approximately 2100 ppm; therefore, compliance with shutdown margin requirements was maintained. This event was not safety significant and it did not adversely affect the health and safety of the public.
V. Corrective Actions
A. Immediate Corrective Actions 1. Unit 2 rod control system was deactivated by opening the reactor trip breakers, which deenergized the gripper circuits and control rods that were withdrawn then reinserted into the core as designed.
2. Plant staff identified a failed moveable gripper coil fuse (FU49) for Rod B4 and replaced the failed fuse.
B. Corrective Actions to Prevent Recurrence 1. STP R-1C has been revised to provide adequate guidance regarding confirmation of rod motion prior to exceeding 12 steps demand indication.
2. Plant operators will receive training on the changes to STP R-1C.
VI. Additional Information
A. Failed Components:
Component: Fuse, 10A 250V ceramic cartridge Manufacturer: BUSSMANN # 2432659
B. Previous Similar Events
of a Control Rod F2 moveable coil power supply fuse which caused Rod F2 to remain on the core bottom, as indicated by the DRPI system. Corrective actions included revising STP R-1C to provide adequate guidance regarding confirmation of rod motion prior to exceeding 12 steps demand indication.
However, as noted above, these steps were inadvertently deleted in a subsequent revision to the procedure.
Diablo Canyon Power Plant, Unit 2 05000323