caused by a mechanical failure of the operating circulating water pump. Major plant systems responded normally, including an auxiliary feedwater actuation due to the resultant low steam generator level. This condition was reported to the NRC via the Emergency Notification System on December 13, 2005 ( EN# 42199). |
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) POINT BEACH NUCLEAR PLANT UNIT 1 05000266 � YEAR SEQUENTIAL NUMBER
Event Description:
On December 13, 2005, the Unit 1 inboard circulating pump [P], 1P-030B, mechanically failed due to fatigue failure of the bolts in the coupling [CPLG] between the pump and motor [MO]. The motor continued to run uncoupled. Unit 1 main condenser [CONDI vacuum began lowering rapidly followed by the sound of steam in the turbine hall [NM]. At 0339, the operating crew manually tripped the Unit 1 reactor [RCT] and initiated Procedure EOP 0, "Reactor Trip or Safety Injection". During the performance of EOP 0, the main steam isolation valves (MSIVs) [ISV] were shut to isolate the source of steam. Auxiliary feedwater [BA] actuated as designed due to the resultant low steam generator [SG] water level.
At 0346 operators identified that the 1P-30B circulating water pump was not running. However, control room indicators [MC:BD] showed that the breaker [52] remained shut. At 0347, the crew placed 1P-30B circulating water pump control switch [JS] to stop, which opened the breaker and stopped the pump motor. The failure mechanism of the pump was that the coupling bolts between the pump and motor had failed due to fatigue.
This failure was consistent with the observed indications in the control room of reduced current to the pump.
Unit 1 was placed in a stable condition in Mode 3. All systems functioned as designed during the transient, with the exception of the audible nuclear instrumentation [IG] monitor [MON] in the control room, which necessitated a manual start. The rupture discs on the main condenser were ruptured due to condenser overpressure, which caused a low pressure steam release into the turbine hall.
This condition was reported to the NRC via the Emergency Notification System on December 13, 2005 (EN# 42199).
Component and system Description:
Circulating Water System The circulating water system [SG], described in FSAR 10.2, circulates water from Lake Michigan through the main condensers to condense the steam exhausting from the turbines. The water is discharged back to the lake through discharge flumes. Two circulating water pumps per unit are used to circulate the water. The circulating water system also supplies cooling water to the condensate cooler for maintaining the main generator hot gas temperature.
The circulating water intake system, common to both units, is designed to provide a reliable supply of Lake Michigan water, regardless of weather or lake conditions, to the suction of four circulating water pumps, six service water pumps and two fire water pumps. The pumphouse is Class I. The intake crib is located 1750 feet from the shore in a water depth of 22 feet. The structure consists of two annular rings of 12-inch structural steel H pile driven to a minimum depth of 23 feet below lake bed and reinforced with walers fabricated from 12 inch structural steel H pile. The annulus is filled with individually placed limestone blocks having two approximately parallel surfaces and weighing between 3 and 12 tons. The structure has an outside diameter of 110 feet, an inside diameter of 60 feet and a top elevation of approximately -11'-0".
Water enters the intake crib primarily through the 60-foot opening above the intake cones. The 60-foot opening is covered with a trash rack having approximately 7 inch x 18 inch openings. The intake crib has been designed to reduce the likelihood of ice blockage during the wintertime.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Water flows from the intake crib to the pumphouse forebay through two 14-foot diameter, corrugated, galvanized, structural plate pipes buried to a minimum depth of 3 feet below lake bed. Flow through either pipe can be reversed during winter operation to recirculate warm condenser discharge water to the intake to prevent freezing in the system. Water flows from the forebay through bar grates and through traveling screens having 3/8 inch mesh to the suction of the pumps.
Auxiliary Feedwater (AFW) System The AFW System automatically supplies feedwater to the steam generators to remove decay heat from the Reactor Coolant System upon the loss of normal feedwater supply. The AFW pumps provide cooling water to the steam generator secondary side via connections to the main feedwater (MFW) piping inside containment. The steam generators function as a heat sink for core decay heat. The heat load is dissipated by releasing steam to the atmosphere from the steam generators via the main steam safety valves (MSSVs) (LCO 3.7.1) or atmospheric dump valves (LCO 3.7.4). If the main condenser is available, steam may be released via the steam bypass valves and recirculated to the CST.
Event Analysis and Safety Significance:
The safety significance of this condition was minimal. The plant responded properly to the manual reactor trip and all safety systems operated as designed.
Cause:
The loss of condenser vacuum and a turbine and reactor trip was caused by the 1P3OB Circulating Water Pump failure.
The circulating water pump's lower shaft sleeve failed directly above the guide vane flanged connection.
The shaft sleeve failure caused an imbalance within the pump which resulted in a fatigue failure of the pump to motor coupling bolts. The preliminary determination is that the failure of the lower shaft sleeve was the result of age and fatigue from imbalance and looseness due to increased impeller and bearing clearances in the pump.
Historically, the circulating water pumps at PBNP have been very reliable. There have been no other circulating water pump failures that have resulted in a plant trip. The failure is classified as a maintenance preventable functional failure (MPFF). The pumps have normally been reassembled with wear clearances greater than original manufacturer tolerances following routine maintenance inspections. NMC staff initiated an evaluation regarding replacement of the circulating water pumps or refurbishment to original tolerances.
Corrective Action:
Unit 1 was placed in a stable condition in Mode 3. The main condenser rupture disks were replaced. The remaining operable circulating water pump (1P-30A) was evaluated and started to restore circulating water flow to the condenser. Following completion of the reactor post-trip review, an evaluation determined that Unit 1 was safe to restart. The reactor was taken critical and the unit was returned to full power.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3)
Interim Corrective Actions:
The intermediate term corrective action was to evaluate the physical failure mechanism and repair the 1P-30B circulating water pump. Repair activities include replacement of the coupling and coupling bolts in pump 1P-30B.
Corrective Actions to Prevent Recurrence:
Actions being planned to prevent recurrence include evaluating the need to remove coupling bolts from the other three circulating water pumps (1P-30A, 2P-30A, and 2P-30B) to check for cracks and assess replacement as necessary.
Additional actions being considered include evaluating the need to replace or refurbish pump 1P-30B to bring all tolerances back to within original manufacturer's tolerances to eliminate looseness and evaluating the need to replace or refurbish pumps 1P-30A, 2P-30A and 2P-30B to bring all tolerances back to within original manufacturer's tolerances to eliminate looseness.
Previous Similar Events:
A review of recent LERs (past three years) identified four events that involved automatic or manual reactor trips:
LER Number Title 266/2003-002-00 Reactor Trip due to Failure of "1G06" Rod Drive Motor Generator Voltage Regulator 301/2003-004-00 Reactor Trip due to Failure of "B" Main Feed Pump 301/2003-005-00 Manual Safety Injection and Reactor Trip due to Overcooling Transient 301/2004-002 -00 Concerns with Diver Safety Results in Manual Reactor Trip
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05000328/LER-2005-001 | Unit 2 Reactor Trip Following Closure of Main Feedwater Upon Inadvertent Opening of Control Breakers | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000388/LER-2005-001 | DDegradation of Primary Coolant Pressure Boundary due to Recirculation Pump Discharge Valve Bonnet Vent Connection Weld Flaw | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000423/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000455/LER-2005-001 | Unit 2 Automatic Reactor Trip Due to Low Steam Generator Level resulting from a Software Fault on the Turbine Control Power Runback Feature | | 05000370/LER-2005-001 | Automatic Actuation of Motor Driven Auxiliary Feedwater Pumps During Outage | | 05000244/LER-2005-001 | Failure of ADFCS Power Supplies Results in Plant Trip | | 05000247/LER-2005-001 | 0Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by an Inoperable Auxiliary Component Cooling Water Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000529/LER-2005-001 | REACTOR HEAD VENT AXIAL INDICATIONS CAUSED BY DEGRADED ALLOY 600 COMPONENT | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000336/LER-2005-001 | | | 05000266/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000269/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000289/LER-2005-001 | | | 05000293/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000298/LER-2005-001 | Reactor Scram due to Reactor Level Transient and Inadvertent Rendering of High Pressure Coolant Injection Inoperable | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000331/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000315/LER-2005-001 | Reactor Trip Following Intermediate Range High Flux Signal | | 05000316/LER-2005-001 | Reactor Trip from RCP Bus Undervoltage Signal Complicated by Diesel Generator Output Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000317/LER-2005-001 | Main Feedwater Isolation Valve Inoperability Due to Handswitch Wiring | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000323/LER-2005-001 | TS 3.4.10 Not Met During Pressurizer Safety Valve Surveillance Testing Due to Random Lift Spread | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000333/LER-2005-001 | Inoperable Offsite Circuit In Excess of Technical Specifications Allowed Out of Service Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000352/LER-2005-001 | Loss Of Licensed Material In The Form Of A Radiation Detector Calibration Source | | 05000353/LER-2005-001 | Core Alterations Performed With Source Range Monitor Alarm Horn Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000362/LER-2005-001 | Emergency Diesel Generator (EDG) 3G003 Declared Inoperable Due to Loose Wiring Connection on Emergency Supply Fan | | 05000263/LER-2005-001 | | | 05000456/LER-2005-001 | Potential Technical Specification (TS) 3.9.4 Violation Due to Imprecise Original TS and TS Bases Wording | | 05000454/LER-2005-001 | Failed Technical Specification Ventilation Surveillance Requirements During Surveillance Requirement 3.0.3 Delay Period | | 05000282/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2005-001 | Plant in a Condition Prohibited by Technical Specifications due to Error Making Control Room Ventilation System Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000400/LER-2005-001 | Reactor Auxiliary Building Emergency Exhaust System Single Failure Vulnerability | | 05000395/LER-2005-001 | Emergency Diesel Generator Start and Load Due To A Loss Of Vital Bus | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000382/LER-2005-001 | RCS Pressure Boundary Leakage Due to Primary Water Stress Corrosion Cracking of a Pressurizer Heater Sleeve | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000305/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2005-001 | Reactor Coolant System Leakage Detection Instrumentation Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2005-002 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000255/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-002 | Missing Taper Pins on CCW Valve Cause Technical Specification Required Shutdown | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000370/LER-2005-002 | Ice Condenser Lower Inlet Door Failed Surveillance Testing | | 05000353/LER-2005-002 | High Pressure Coolant Injection System Inoperable due to a Degraded Control Power Fuse Clip | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000263/LER-2005-002 | | | 05000454/LER-2005-002 | One of Two Trains of Hydrogen Recombiners Inoperable Longer Than Allowed by Technical Specifications Due to Inadequate Procedure | | 05000244/LER-2005-002 | Emergency Diesel Generator Start Resulting From Loss of Off-Site Power Circuit 751 | | 05000362/LER-2005-002 | Emergency Containment Cooling Inoperable for Longer than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2005-002 | DTechnical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by Gas Intrusion from a Leaking Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000265/LER-2005-002 | Main Steam Relief Valve Actuator Degradation Due to Failure to Correct Vibration Levels Exceeding Equipment Design Capacities | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000286/LER-2005-002 | • Entergy Nuclear Northeast Indian Point Energy Center 450 Broadway, GSB P.O. Box 249Entergy Buchanan. NY 10511-0249 Tel 914 734 6700 Fred Dacimo Site Vice President Administration July 5, 2005 Indian Point Unit No. 3 Docket Nos. 50-286 N L-05-078 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2005-002-00, "Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure." Dear Sir: The attached Licensee Event Report (LER) 2005-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2005-02478. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, 4F-/t R. Dacimo Vice President Indian Point Energy Center Docket No. 50-286 NL-05-078 Page 2 of 2 Attachment: LER-2005-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 3660 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request 50 hours.RReported lessons teamed are incorporated into the licensing process and fed back to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 29555-0001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to Infocoilectsenrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection. 1. FACIUTY NAME 2. DOCKET NUMBER 3. PAGE INDIAN POINT 3 05000-286 10OF06 4. TITLE Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000287/LER-2005-002 | Unit 3 trip with ES actuation due to CRD Modification Deficiencies | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2005-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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