ML20217R014
ML20217R014 | |
Person / Time | |
---|---|
Site: | Byron |
Issue date: | 05/05/1998 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20217Q928 | List: |
References | |
50-454-98-09, 50-454-98-9, 50-455-98-09, 50-455-98-9, NUDOCS 9805130085 | |
Download: ML20217R014 (22) | |
See also: IR 05000454/1998009
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U. S. NUCLEAR REGULATORY COMMISSION
REGION 111
Docket Nos: 50-454;50-455
Report No: 50-454/455-98009(DRP)
Licensee: Commonwealth Edison Company
Facility: Byron Generating Station, Units 1 and 2
Location: 4450 N. German Church Road
Byron,IL 61010
Dates: February 23 - April 6,1998
Inspectors: E. Cobey, Senior Resident inspector
N. Hilton, Resident inspector
B. Kemker, Resident inspector
D. Muller, Reactor inspector
D. Pelton, Braidwood Resident inspector
T. Tongue, Project Engineer
C. Thompson, Illinois Department of Nuclear Safety
Approved by: Michael J. Jordan, Chief
Reactor Projects Branch 3
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9805130085 990505
PDR ADOCK 05000454
G PDR
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EXECUTIVE SUMMARY
Byron Generating Station Units 1 and 2 i
NRC Inspection Report No. 50-454/98009(DRP); 50-455/98009(DRP)
This inspection included aspects of licensee operations, maintenance, engineering, and plant
support. The report covers a six-week period of inspection activities by the resident staff and
region based inspectors.
Operations
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The inspectors concluded that overall operator performance during the aborted Unit i
reactor startup on March 6,1998, was good, including the development of trip
contingency actions, the use of procedures and three-way communications. The
inspectors also noted that conservative operating decisions were made, most notably the
decision to shutdown the reactor after failing to achieve criticality at the estimated boron
concentration. The inspectors noted one example where the Qualified Nuclear Engineer
created confusion while attempting to explain the boron concentration limits to the
operating crew (Section 01.2).
- The inspectors concluded that overall operator performance during restart on March 7,
1998, of the Unit i reactorwas good. The criteria for startup termination, based on boron
concentration and dilution volume, were clearly stated and fully understood. This
alleviated the confusion that was present during the aborted startup the previous night. j
The inspectors also concluded that procedure usage, crew communication, and crew
briefings were effective (Section 01.3).
- Observed portions of low power physics testing were conducted in a safe manner. Each
reactivity manipulation was closely monitored by the Unit Supervisor. However,
communications between the Qualified Nuclear Engineer and the Unit 1 Nuclear Station
Operator did not meet the station management's expectations for three-way
communications. At times unnecessary personnel congregated in the area of the center
desk and participated in discussions not related to the operation of the plant. Although
these discussions resulted in the background noise level being elevated, no adverse
consequences were noted (Section O1.4).
- The inspectors concluded that the replacement steam generators operated as designed
and the plant responded to the planned transients as expected with no significant
- anomalies noted. In addition, during the replacement steam generator testing, the
inspectors observed effective supervisory oversight of the evolutions and good .
coordination between operators, system engineers, and maintenance personnel. The
inspectors also noted that the control room operators generally adhered to the Nuclear
Operations Division Operations Department Standards (Section 01.5).
- The incpectors concluded that the entry of Unit 1 into Mode 4 (Hot Shutdown) from
Mode 5 (Cold Shutdown) with the seal table room floor drain plugged was a violation of
Technical Specifications and should have been prevented by corrective actions from
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previously identified issues with the floor drain system. The inspectors concluded that
significant contributions to not recognizing the inoperable seal table floor drain were poor
maintenance work request content and documentation, poor problem description on the
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problem identification form, and poor followup by the system engineer's when notified by
mechanics that the floor drains remained plugged. A violation was cited (Section O2.1).
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The inspectors concluded that the licensee's process for maintaining senior reactor
operator licenses active was weak, in that, an Operations Policy Momo allowec; credit for
proficiency to be taken for shift supervisor and administrative shift supervisor positions
contrary to the requirements of 10 CFR Part 55 and the licensee's operating surveillance
test. However, no violations of regulatory requirements were identified because all senior
reactor operators that conducted licensed duties during the quarter met the requirements
of 10 CFR Part 55 and the licensee's operating surveillance procedure. The inspectors
also concluded that several log entries for shift personnel did not meet the licensee
management's expectations (Section O3.1).
. The inspectors concluded that Byron Operating Procedure VC-2, " Shutdown of Control
Room HVAC System," Revision 2, was not appropriate to the circumstances due to an
inadequate technical review during the procedure revision completed on January 7,1998.
In addition, the inspectors concluded that on at least eight occasions, the control room
operators performed this procedure and did not identify the procedural deficiencies and
initiate corrective action, which was not in accordance with licensee managements's
expectations and standards for procedural adherence as described in Nuclear Operations
Division Operations Department Standards, Section Vill, " Procedural Adherence." A
violation was cited (Section O3.2).
Maintenance / Surveillance ,
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The inspectors concluded that each of the observed maintenance activities satisfied the
regulatory requirements. The inspectors also noted that based on the failure to conduct
an appropriate blue check and the additional seat flatness tests required to ensure a
correct seating surface, the licensee did not initially have the necessary expertise to
satisfactorily repair Safety injection Check Valve 1S189568 (Section M1.1).
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The inspectors noted that generally, work requests were adequately controlled and
scheduled; however, an example of unauthorized work in progress was identified by the
inspectors. Approximately 50 work requests were on hold with valid authorizing
signatures which indicated weaknesses in the authorization process. The inspectors
concluded that the control of WRs on hold was undocumented, inconsistent, and
problems were not identified by the licensee. A violation was cited (Section M3.1).
- Plant Support
- The inspectors concluded that the licensee failed to post a contamination area in
accordance with Byron Radiological Protection Procedure 5010-1. A violation was issued
(Section R1.1).
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Report Details
Summary of Plant Status
The licensee completed the Unit 1 steam generator replacement and refueling outage on j
March 8,1998. The licensee subsequently completed physics testing and steam generator j
replacement post modification testing and the unit was operating at or near full power at the end j
of the inspection period. I
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The licensee initiated coastdown operations on Unit 2 during the inspection period in preparation ]
for entering a refueling outage.
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1. Operations
01 Conduct of Operations
01.1 General Comments (71707)
During the inspection period, the inspectors conducted numerous observations of routine
control room activities. The inspectors observed effective heightened level of awareness
briefings for infrequently performed evolutions and good annunciator alarm response.
The inspectors also noted that the control room operators generally adhered to the
Nuclear Operations Division Operations Department Standards. However, the inspectors
also noted several instances where activities did not meet licensee management's
standards and expectations including: (1) three-way closed loop directed
communications were not always utilized; (2) the Unit 2 operators were not monitoring the
computer trend plots specified in the Unit 2 coast down daily order; (3) log entries were
not always sufficiently detailed to allow reconstruction of shift activities; and (4) on one
occasion an equipment operator failed to recognize and initiate action for an out of
specification parameter during a diesel generator surveillance. Overall, the inspectors
concluded that routine operations were conducted in a safe and controlled manner. i
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O1.2 Unit 1 Aborted Startuo Followina Steam Generator Replacement Outaae
a. Inspection Scope (71707 and 50001)
The inspectors observed the heightened level of awareness (HLA) briefing and the initial
Unit 1 startup. The inspectors also reviewed the following procedures:
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- 1BGP 100-2, " Plant Startup," Revision 21
- 1BGP 100-2A1, " Reactor Startup," Revision 11
- 1BVS XPT-4, " Unit 1 Initial Criticality After Refueling and Nuclear Heating Level,"
Revision 12
b. Observations and Findinas
On March 6,1998, the licensee commenced a Unit 1 plant startup following the steam
generator replacement and refueling outage. While monitoring the approach to criticality
using an inverse count rate ratio plot, the Qualified Nuclear Engineer (QNE) identified that
the reactor would not be critical with boron concentration at 1433 parts per million (ppm),
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the estimated critical concentration. During the ensuing discussion with the control room
operators, the QNE could not ensure that the reactor would be critical at a boron
concentration of 1383 ppm (the minimum limit specified in 1BVS XPT-4). In addition, the
QNE created confusion while attempting to explain the technical basis for the limits on
boron concentration. Consequently, ine shift manager directed the crew to halt the ,
startup and make preparations for a reactor shutdown. The inspectors concluded that the
operating crew's decision to retum Unit 1 to a shutdown condition was conservative.
While inserting control rods for the shutdown, control Bank C unexpectedly stopped at
eight steps. As a result, the crew stopped the shutdown and commenced troubleshooting
activities. Since the Bank C rod position and the Bank C demand signal were both at
eight steps, the operators concluded that, even though the manual rod control switch was
in the insert position, the rod control system stopped demanding the insertion of Bank C
at eight steps. After some discussion, the crew determined that inserting a manual trip
was the most appropriate action. After a short control room briefing, a manual trip was i
inserted. Following the reactor trip, the licensee verified all systems functioned as J
expected. Based on the inspectors' observations, the inspectors concluded that the '
licensee's actions were appropriate.
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c. Conclusions 4
The inspectors concluded that overall operator performance during the aborted Unit i
reactor startup on March 6,1998, was good, including the development of trip
contingency actions, the use of procedures and three-way communications. The
inspectors also noted that conservative operating decisions were made, most notably the
decision to shutdown the reactor after failing to achieve criticality at the estimated boron
concentration. The inspectors noted one example where the Qualified Nuclear Engineer-
created confusion while attempting to explain the boron concentration limits to the t
operating crew.
01.3 Unit 1 Startuo After Steam Generator Replacement Outaae
a. inspection Scope (71707 and 50001)
The inspectors interviewed operators and engineering personnel and obseived the
licensee's Hl.A briefing and plant startup activities. The inspectors also reviewed the
procedures referenced in Section 01.2.
- b. Observations and Findinas
On March 7,1998, the licensee corrected the problems observed during the startup and
subsequent shutdown that occurred on the previous midnight shift (see Section 01.2).
Specifically, the licensee: (1) developed a larger acceptance band (consistent with
Technical Specifications (TSs)) for the critical boron concentration, and (2) completed i'
troubleshooting and cleaning electrical contacts on the bank overlap unit in the rod control
system to correct the failure of Bank C to fully insert during the previous shutdown. In
addition, the licensee developed definitive operator actions for specific boron dilution
levels, to address the potential for problems similar to those encountered during the
previous startup. The inspectors observed that the criteria for startup termination, based
on boron concentration and dilution volume, was clearly stated and fully understood.
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The licensee subsequently withdrew control rods to the estimated critical rod height and
then diluted the reactor coolant system (RCS) to the estimated critical boron
concentration. After the dilution was completed, the reactor remained subcritical. Based
on the established boron concentration limits, the crew continued the dilution, but still
within the acceptance range. At 1:50 a.m. on March 8,1998, the reactor achieved
criticality. The chemistry sample indicated that the boron concentration was 1394 ppm, q
approximately 39 ppm below the estimated critical concentration of 1433 ppm. This was I
within the procedural and TS limits. 4
c. Conclusions
The inspectors concluded that overall operator performance during restart on March 7,
1998, of the Unit i reactor was good. The criteria for startup termination, based on boron
concentration and dilution volume, were clearly stated and fully understood. This
alleviated the confusion that was present during the aborted startup the previous night.
The inspectors also concluded that procedure usage, crew communication, and crew
briefings were effective.
01.4 Unit i Low Power Physics Testina i71707)
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The inspectors observed selected portions of Byron Engineering Surveillance (BVS)
1BVS XPT-5, " Unit 1 Rod and Boron Worth Measurements," Revision 9. The inspectors
noted that each reactivity manipulation was closely monitored by the Unit Supervisor.
The inspectors also noted that the communications between the Qualified Nuclear
Engineer and the Unit 1 Nuclear Station Operator routinely did not meet the expectations
for three-way closed loop directed communications delineated in the Nuclear Operations
Division Operations Department Standards,Section IX, " Communications." In addition, i
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the inspectors noted that at times the decorum in the control room declined, in that,
unnecessary personnel congregated in the area of the center desk and participated in
discussions not related to the operation of the plant. Although these discussions resulted
in the background noise level being elevated, the inspectors did not note any adverse
consequences. The inspectors concluded that 1BVS XPT-5 was conducted in a safe
manner.
01.5 Unit 1 Replacement Steam Generator Testina (50001)
The inspectors interviewed operations and engineering personnel, reviewed the test
procedures, and observed selected portions of Special Plant Procedure (SPP)97-048,
- "Large Load Reduction," Revision 2, SPP 97-049, "10 percent Load Decrease,"
Revision 1, and SPP 97-050, " Steam Generator Level Control Test," Revision 1. The
inspectors concluded that the replacement steam generators operated as designed and
the plant responded to the transients as expected with no significant anomalies noted. In
addition, during the replacement steam generator testing, the inspectors observed '
effective supervisory oversight of the evolutions and good coordination between
operators, system engineers, and maintenance personnel. The inspectors also noted
that the control room operators generally adhered to the Nuclear Operations Division
Operations Department Standards.
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02 Operational Status of Facilities and Equipment
O2.1 Pluaaed Unit 1 Seal Table Room Containment Floor Drain
a. Inspection Scope (71707)
On February 28,1998, the licensee changed from Mode 5 (Cold Shutdown) to Mode 4
(Hot Shutdown) with an inoperable containment floor drain. The inspectors interviewed
engineering management and the root cause investigator. The inspectors reviewed the
following documents' '
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- Work Request (WR) 970107702, " Equipment Drain Has Debris In it - CV System
Drain Bowl"
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Operability Assessment 98-019
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- Problem identification Forms (PIFs) B1998-00723, B1998-00977, and
B1998-01046
- Temporary Alteration 98-1-017, " Seal Table Room Floor Drains"
- On-Site Review Report 98-040, " Unit 1 Regen Heat Exchanger and Excess
Letdown Heat Exchanger Rooms Floor Drains Not Hydrolyzed during B1R08"
- Licensee Event Report (LER) 50-454-98004, " Reactor Coolant Leak Detection
System inopercble due to inadequate Communication"
b. Observations and Findinas
On March 15,1997, the licensee identified that the Unit 2 containment floor drain system
was plugged and inoperable. The licensee submitted LER 50-455/97001 and the issue
was documented in NRC Inspection Report No. 50-454/97005(DRP);
50-455/97005(DRP). As a result, a predecisional enforcement conference was
conducted on June 21,1997. In response to this issue, the licensee committed to
cleaning the containment floor drain system at the end of the next refueling outage on
both units.
At the request of the system engineer, mechanical maintenance personnel prepared
WR 970032868-01 to clean and inspect containment floor drains. On February 10,1998,
mechanics notified system engineering personnel that ffie Unit 1 seal table room floor
drain was plugged and that attempts to clear it had been unsuccessful. Maintenance
personnel closed the WR and initiated a PIF. However, the PIF identified several
unrelated discrepancies and was not clear that the seal table room floor drain was
- plugged and was unable to be cleared. Based on the problem description and the
immediate action taken identified in the PlF, the operators concluded that the system was
operable and the licensee's PlF screening committee agreed with the operators. No
initial action was taken. The inspectors found that a poor problem description on
PlF B1998-00723 contributed significantly to the licensee's failure to recognize that the
seal table room floor drain was plugged.
The system enginear assumed that the corrective action process would resolve the
plugged floor drain and did not take any action. However, the PlF was closed without any
corrective actions and the system engineer was not aware that corrective actions were
not in place or planned until February 27,1998. During routine PIF reviews by system
engineering personnel, and subsequent document research, the floor drain system
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engineer identified that the seal table room floor drain remained plugged. As a result, the
system engineer prepared an action request. However, the action request was
erroneously written as nonsafety-related and non-TS equipment. Therefore, the licensee
did not identify the significance of the plugged floor drain during initial reviews.
Consequently, the licensee did not recognize the significance of the plugged floor drain
untii February 28,1998, the day after changing to operational Mode 4.
As immediate corrective action, the licensee installed a temporary alteration in an existing
clean out port of the seal table room floor drain. The temporary alteration restored the J
floor drain system to operable status. The inspectors observed the temporary alteration
and considered it acceptable. At the end of the inspection period, the licensee was
evaluating long term corrective action for the plugged floor drain.
During the licensee's investigation for the associated LER 98-004, the licensee identified
that the work scope for WR 970032868-01 was not complete; specifically, clear direction
for which containment floor drains were to be cleaned was not provided. The licensee
concluded that work activities were not well documented on the completed WR. The I
inspectors' discussions with the root cause investigator indicated that the WR developed
for the floor drain cleaning had been an existing generic floor drain WR and the systc,m
engineer had given maintenance personnel marked-up drawings of the containment
building instead of a list of floor drains to clean. Both the licensee and the inspectors
concluded that WR 970032868-01 was not adequately revised to ensure all drains were
cleaned and inspected.
Technical Specification 3.4.6.1.b required that the containment floor drain and reactor
cavity flow monitoring systems be operable in Modes 1,2,3, and 4. The inspectors
noted that TS 3.0.4 required that entry into an operational mode shall not be made when i
tne conditions for the Limiting Condition for Operation (LCO) are not met and the
associated action required a shutdown if they are not met within a specified time interval.
The action requirement for TS 3.4.6.1.b stated that with the required leakage detection l
systems inoperable, restore to operable status within 7 days; otherwise, be in at least hot !
standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Therefore, the inspectors concluded that TS 3.0.4 was i
applicable.
The failure to meet the conditions specified in TS 3.4.6.1 when Unit 1 changed
operational modes from Mode 5 to Mode 4 on February 27,1998, is considered a
violation of TS 3.0.4 as described in the attached Notice of Violation. This violation is
being cited since it could have been prevented by effective corrective action to the
. March 1997 event or the PIF documenting the condition on February 12,1998,
(50-454/98009-01(DRP)).
After the seal table room floor drain issue was identified, the licensee reviewed the scope
of the original floor drain cleaning plan and identified that the floor drains for the
regenerative heat exchanger and excess letdown heat exchanger rooms were not
inspected as committed to during the predecisional enforcement conference. The
licensee concluded and documented in On-Site Review Report 98-040 that the two heat
exchanger room floor drains were operable based on the following: (1) the rooms were
High Radiation Areas and access to the rooms was very limited; (2) floor openings exist
in the heat exchanger rooms that would allow any water to flow out of the rooms to the
elevations below and be identified through a different floor drain if a floor drain in the
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room was plugged; (3) and a search of the work history on the heat exchanger room floor
drains did not identify any previous work, which would indicate that the drains had a
history of problems. The licensee concluded that there was no reason to believe that the
floor drains were incapable of collecting water for leak identification and planned a future
evaluation to determine the appropriate scope of future actions for the floor drains in the
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heat exchanger rooms. The inspectors also concluded that the failure to provide a clear
scope list in WR 970032868-01, as described above, also contributed directly to the
l licensee failing to clear and inspect the floor drains in the regenerative heat exchanger
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and excess letdown heat exchanger rooms.
c. Conclusions
The inspectors concluded that the entry of Unit 1 into Mode 4 (Hot Shutdown) from
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Mode 5 (Cold Shutdown) with the seal table room floor drain plugged was a violation of
Technical Specifications and should have been prevented by corrective actions from
previously identified issues with the floor drain system. The inspectors concluded that
significant contributions to not recognizing the inoperable seal table floor drain were poor
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maintenance work request content and documentation, poor problem description on the
l problem identification form, and poor followup by the system engineer's when notified by
mechanics that the floor drains remained plugged. A violation was cited.
03 Operations Procedures and Documentation
O3.1 Maintenance of Senior Reactor Operator (SRO) Active Licenses
a. Inspection Scope (71707)
The inspectors reviewed the licensee's process for maintaining SRO (SRO) licenses
active. The inspectors interviewed operations and training department management and
reviewed the following procedures:
- Byron Administrative Procedure (BAP) 320-1, " Shift Manning," Revision 7
- Byron Operating Surveillance (BOS) LIC-1, "NRC Active License Tracking,"
Revision 2
- BAP 350-1, " Operating Logs and Records," Revision 14
- Operations Policy Memo 400-12 " Operators' License Information," Revision 68
' * BOS LIC-1 documentation for the fourth quarter of 1997
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b. Observations and Findinas
The inspectors reviewed BOS LIC-1 and concluded that the requirements of
10 CFR Part 55 for maintaining operator licenses active were accurately translated. ;
However, the inspectors also noted that operations department management had issued !
an Operations Policy Memo which provided additional guidance to the operators. This
policy allowed shift supervisor and administrative shift supervisor duties to be credited
toward maintaining an active license, contrary to 10 CFR Part 55 and BOS LIC-1.
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However, the inspectors also noted that operations management expected shift
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Supervisor as required by BOS LIC-1. With one exception noted below, the shift
supervisors and administrative shift supervisors maintained their licenses active during
the fourth quarter of 1997.
During the review, the inspectors noted that one SRO had taken credit for administrative
shift supervisor duties to meet the requirements of BOS LIC-1 for the fourth quarter of
1997, in accordance with the Operations Policy Memo. The inspectors noted that the
BOS LIC-1 dated December 31,1997, indicated that this SRO maintained an active
SRO license but would not be considered for routine assignment as a Unit Supervisor.
As a result of the inspectors questions, the licensee determined the individual's license
was inactive. The inspectors also noted the individual had not assumed duties as a Unit
Superviso. since December 31,1997; therefore, no violation of regulatory requirements '
was identified. At the end of the inspection period, the licensee was continuing to
investigate the issue.
In addition, the inspectors had difficulty independently verifying which SROs and ROs
were responsible for specific shift positions. Although shift tumover sheets and control
room door security records confirmed that TS minimum manning requirements were met,
the inspectors noted that several log entries for shift personnel did not meet the licensee
management's expectations.
c. Conclusion
The inspectors concluded that the licensee's process for maintaining senior reactor
operator licenses active was weak, in that, an Operations Policy Memo allowed credit for 4
proficiency to be taken for shift supervisor and administrative shift supervisor positions I
contrary to the requirements of 10 CFR Part SS and the licensee's operating surveillance
test. However, no violations of regulatory requirements were identified because all senior
reactor operators that conducted licensed duties during the quarter met the requirements
of 10 CFR Part 55 and the licensee's operating surveillance procedure. The inspectors
also concluded that several log entries for shift personnel did not meet the licensee
management's expectations.
03.2 Inadeauste Control Room Ventilation System Operatina Proc +'"5
a. Inspection Scope (71707)
The inspectors reviewed Byron Operating Procedure (BOP) VC-2, " Shutdown of Control
Room HVAC [ Heating, Ventilation, and Air Conditioning) System," Revision 2, and
interviewed operators and procedure writers,
b. Observations a,1d Findinos ,
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On March 11,1998, during follow-up inspection activities into a four hour non-emergency l
report in accordance with 10 CFR Part 50.72(b)(2)(iii)(D), which the licensee l
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subsequently retracted on March 12,1998, the inspectors identified that BOP VC-2 was
incomplete as written. Specifically, the procedure did not provide direction to secure the
main control room supply, retum, or make-up air filter fans or provide appropriate
guidance to verify damper positions when the control room ventilation system was l
secured from the main control room. The inspectors noted that the licensee had revised 1
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BOP VC-2 on January 7,1998, in support of a modification which relocated controls for ]
one control room ventilation train. In response to the inspectors questions, the licensee
determined that approximately two pages of the procedure had been inadvertently deleted {
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during the revision which had not been identified during the review process. The failure
of BOP VC-2 to provide appropriate guidance to shutdown the control room ventilation {'
system from the main control room is considered an example of a violation of
10 CFR Part 50, Appendix B, Criterion V (50-454/455-98009-02a(DRP)).
Furthermore, the inspectors noted that the licensee had performed BOP VC-2 at least
eight times between January 7 and March 11,1998, and had not initiated a procedure
revision. Nuclear Operations Division Operations Department Standards, Section Vill,
" Procedural Adherence," specifies, in part, that when using operating procedures a
method of placekeeping shall be used. The standards also specify that when an
individual perceives that any procedure is technically incorrect the following actions are to
be taken: (1) stop and ensure the system is in a safe condition; (2) inform supervision of
the situation; and (3) the supervisor shall evaluate the situation and determine if the
procedure can be performed as written, otherwise the procedure shall be revised prior to
continuing the activity. The inspectors noted that if the procedure adherence standards
were implemented, the operators could not shutdown the control room ventilation system
from the main control room in accordance with BOP VC-2 without revising the procedure.
c. Conclusions
The inspectors concluded that the licensee's process for maintaining senior reactor
operator licenses active was weak, in that, an Operations Policy Memo allowed credit for
proficiency to be taken for shift supervisor and administrative shift supervisor positions
contrary to the requirements of 10 CFR Part 55 and the licensee's operating surveillance i
test. However, no violations of regulatory requirements were identified because all senior j
reactor operators that conducted licensed duties during the quarter met the requirements .
of 10 CFR Part 55 and the licensee's operating surveillance procedure. The inspectors !
also concluded that several log entries for shift personnel did not meet the licensee
management's expectations. l
08 Miscellaneous Operations issues l
08.1 10 CFR Part 50.54m Letter Commitment Review
a. Inspection Scood2%S
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The inspector 4 reviewed th3 status of commitments pertaining to Byron's March 28,
1997, response to the NRC's request for information pursuant to 10 CFR 50.54(f). The
commitment numbers correspond to those used by the licensee in their March 28,1997, l
response.
b. Observations and Findinas
Commitment 95: "As described in Section 4.7.4 below, we are also taking special
measures to assess and monitor our performance to ensure that areas of weakness
indicated by the LaSalle and Zion operational events are not present or are addressed at
all of our nuclear stations." The measures referred to included: (1) the development of
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Operations Department indicators; (2) the NOD [ Nuclear Operating Division) Vice
President of Nuclear Support (who headed the investigation of the Zion event) would visit
each site to observe and review control room activities; and (3) operations peer
assessments to evaluate safety culture, conservatism of operational decision making,
and implementation of operations standards.
The inspectors reviewed the licensee's operations department indicators and noted that
the indicators were current. The inspectors also noted that the licensee had recently
identified an adverse trend in out-of-service errors as a result of monitoring these
indicators. In addition, the inspectors noted that the NOD Vice President of Nuclear
Support, the Dresden Station Vice President, and an operation peer group had visited the
site, observed control rcom activities, and evaluated the safety culture and operations
standards. As part of each of the above site visits, the evaluators provided improvement
comments to the licensee.
c. Conclusions
The inspectors concluded that the licensee was meeting commitment 95. This item is
closed.
08.2 10 CFR Part 50.54(f) Performance Indicators
a. Inspection Scope (92901)
The inspectors reviewed the development of selected 50.54(f) performance indicators
and interviewed operations, engineering, and quality and safety assessment personnel.
b. Observations and Findinas
The inspectors reviewed the following performance indicators:
1.1 Automatic Scrams (Reactor Trios) While Critical
The licensee developed performance indicator 1.1 based on the number of unplanned
reactor trips (trips) per year while critical. Examples include trips from unplanned l
transients, equipment failures, spurious signals, or human error. Trips occurring during
the execution of procedures in which there was a high chance of a trip occurring, but the
occurrence of a trip was not planned, are included. Since February 1997, Byron Station
- has had only one unplanned automatic trip while critical (October 1997), which was less
than the action threshold of more than one trip per unit per year. However, during the
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Unit i startup in March 1998, the reactor was manually tripped on two separate
occasions, neither of which were counted against this performance indicator since they
were not automatic and the reactor was not yet critical. The first of these manual trips
occurred on March 6,1998, during the performance of rod drop testing, the operators
tripped the reactor as a result of losing communication with the field operators
participating in the testing. The second, on March 7,1998, during the aborted Unit 1
startup, the operators manually tripped the reactor due to being unable to fully insert the
control Bank "C" rods.
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! 12 Safety System Actuations
The licensee developed performance indicator 12 based on the number of manual or
automatic actuations of the logic or equipment of either certain emergency core cooling
systems (ECCS) or, in response to an actuallow voltage on a vital bus, the emergency
AC power system. Regarding the ECCS, only actuations of the high pressure injection
system, low pressure injection system, or safety injection tanks were counted. Actuations
of the emergency AC power systems were counted only if the emergency AC power
system's output breaker closed, or should have closed, to power a dead bus. Since
February 1997, Byron Station has had zero safety system actuations, which was less
than the action threshold of more than one safety system actuation per unit per year. The
performance indicator was derived from events that were reportable in accordance with
10 CFR Parts 50.72 and 50.73. However, the inspectors noted that this performance
indicator did not include all of the possibilities of safety system actuations that were
reportable such as radiation activated ventilation actuations or containment isolations.
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C16 Number of Problem Identification Forms Written
The licensee developed performance indicator C16 based on the number of PlFs written l
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at each site. Since March 1997, Byron Station has exceeded the action threshold of less
than 160 PIFs written per month. Consequently, the licensee has concluded that the
station's threshold for problem identification was sufficient to support the corrective action
program.
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c. Conclusions
The inspectors concluded thct the performance indicators li,12, and C16 indicated that
the licensee's performance in each area was satisfactory. !
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08.3 (Closed) Inspector Follow-up item (50-454/455-95003-01(DRP)) (92901): "RCS [ Reactor
Coolant System] Pressure Transient Required the Shutdown of the 2D RCP [ Reactor
Coolant Pump)." The initial review found that the licensee acted properly in response to
the transient; however, the issue remained open pending inspector review of the
licensees root cause analysis. The inspectors noted that the licensee's actions included i
stabilizing the plant and restoring pressure, revision of Procedures 1/2BVS 4.6.2.2-1, j
" Unit % Reactor Coolant System Pressure Isolation Valve and Cold Leg injection Isolation !
Valve Leakage Surveillance," to require that this portion of the test be done with a
pressurizer bubble, and counseling system engineers on better. communications which
- could have prevented the event. The inspectors reviewed the root cause report and the i
modified procedures and concluded that the licensee's actions were acceptable. This :
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item is closed.
08.4 (Closed) Violation (50-454/455-96012-05(DRP)) (92901): " Failure to Follosy a Procedure
for a Degraded Containment Floor Drain Monitoring System." The licensee confirmed
that the containment floor drain recorder,1RF008, should have been entered in the !
Degraded Equipment Log (DEL). Short term corrective action was to enter the affected j
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recorder in the DEL. In order to reaffirm the purpose of the DEL, the licensee discussed
the history, intent and purpose of the DEL in a supervisors meeting. The inspector j
reviewed BAP 390-13, " Degraded Equipment Program," to check for any notable 1
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weaknesses. None were identified and the corrective actions were found to be
acceptable. This violation is closed.
i 08.5 (Closed) LER 50-454/98004 (92700h " Reactor Coolant Leak Detection System
inoperable due to inadequate Communication." T his issue is discussed in detail in
Section O2.1. The inspectors considered LER 454/98-04 very good. The report was
critical and comprehensive. Corrective actions appeared strong. The licensee's
corrective actions will be reviewed during the inspectors review of the licensee response
to the violation will be cited in Section O2.1. The inspectors considered LER 454/98-04
closed and the issue will be followed with Violation 50-454/98009-01(DRP).
II. Maintenance
M1 Conduct of Maintenance
M1.1 Maintenance Observations
a. Lnspection Scope (62707)
.
The inspectors observed the performance of all or portions of the following work requests
l (WR). When applicable, the inspectors also leviewed TSs and the Updated Final Safety
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Analysis Report (UFSAR).
- WR 980024198-01 Bank A Insertion Limits Rod Position Annunciator 1-10-806
is in Alarm and Should Not Be
. WR 980018826-01 Replace Valve (2SI 89568) Intemals Due to Failed Leak
Test
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WR 970016380-02 Replace Damaged Piping on the 28 Essential Service
Water Pump (SX) Discharge Strainer Back Wash Line
- WR 970040570 Replace the Nuclear Loop Power Supply Card on the 2A
Steam Generator Loop
WR 980026819 Remove Lagging on Discharge of CV Pump to Support -
Ultrasonic Testing
b. Observations and Findinas
Safety iniection Accumulator B Outlet Check Valve Repair
.
The inspectors observed portions of the testing and maintenance of safety injection
accumulator B outlet Check Valve 1818956B. The valve failed the initial surveillance test.
Mechanics repaired the check valve and retumed the check valve to service after
completing a " blue check" satisfactorily However, the valve failed the leak check a
second time. The licensee reviewed actions taken during the first repair effort with !
non-station personnel who identified that a standard blue check could give false results ;
for this particular type check valve. Additional acceptance criteria for blue ?, hecks and l
other seat flatness tests were used to ensure the valve would not leak. After the second
repair and verification,1S189568 did not leak and was retumed to service. Mechanical
maintenancc personnel conducted a critique after the second repair effort to document j
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lessons leamed and incorporate the necessary steps into future WR instructions. The
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inspectors concluded that initially, the licensee did not have the necessary expertise to
satisfactorily repair 1Sl8956B.
c. Conclusions
,
The inspectors concluded that each of the observed maintenance activities satisfied the
regulatory requirements. The inspectors also noted that based on the failure to conduct
an appropriate blue check and the additional seat flatness tests required to ensure a
correct seating surface, the licensee did not initially have the necessary expertise to
satisfactorily repair safety injection check valve 1S189568.
M1.2 Surveillance Test Observations
a. Inspection Scope (61726)
The inspectors interviewed operations and engineering personnel, reviewed the
completed test documentation, and observed the performance of selected portions of the
following surveillance test procedures.
. 1BOS 3.1.1-35 Unit 1 Analog Channel Operational Test of Intermediate
Range Channel N35.
. 2BOS 3.2.1-970 ESFAS Instrumentation Slave Relay Surveillance. (Train B
Autc:natic Valve Actuation on Refueling Water Storage
Tank Lo-2 Level (K 648)).
. OBOS 3.2.1-990 ESFAS Instrumentation Slave Relay Surveillance (Train B
Feedwater isolation)
. BIS 3.1.1-203 Surveillance Calibration of Steam Generator Narrow Range
Level Protection Loop
. 1BOS 5.2.b-1 ECCS Wating and Valve Alignment Monthly Surveillance
. 1BOS 8.1.1.2.A-2 1B Diesel Generator Monthly Operability Surveillance l
c. Conclusion
1
The inspectors concluded that each of the observed surveillance tests satisfied the
regulatory requirements and all of the components tested were operable. The inspectors
also noted that the material condition of the tested components was generally good.
However, the inspectors identified several minor deficiencies on the 18 diesel generator
(e.g., oil and water leaks, missing ventilation gasket, and inadequate thread engagement
- on a relief valve) which the licensee subsequently addressed by initiating corrective
maintenance WRs.
M3 Maintenance Procedures and Documentation
M3.1 Maintenance Control of WRs
a. Inspection Scope (62707)
During routine maintenance observations, the inspectors noted a mechanic working on an
essential service water (SX) pump, performing a task that had been authorized
approximately 14 months prior to the inspectors' review. The inspectors noted that the
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authorizing signature on the work package had been deleted. The inspectors questioned
the licensee's program from the standpoint of controlling and authorizing WRs that had
previously been authorized but then placed on hold.
b. Observations and Findinas
I
During a review of WR 960100631, the inspector noted that electrical maintenance
personnel began removing the lube 1B-SX oil pump motor without authorization from the
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control room. The authorizing SRO's signature had been previously lined-out. Byron
Administrative Procedure (BAP) 1600-1, " Action / Work Request Processing Procedure,"
Revision 41, Section D, Paragraph 5, stated that an SRO shall authorize work to start,
and Section D, Paragraph 6, stated that the lead worker was to verify that the authorizing
signature was obtained on the WR prior to starting work. The WR was originally
authorized in December 30,1996, and then not performed as originally scheduled. The
authorizing signature was lined out the same day that the WR was originally scheduled.
The inspectors considered that the actual safety significance of the unauthorized WR was
minimal. The work had been scheduled and the SRO immediately authorized the work
after the issue was noted by the inspectors. The unauthorized work activities did not
create a personnel hazard and did not remove any operable safety-related equipment
from service. In addition, the inspectors had not identified any previous occasions of
working without appropriate authorization. Therefore, the inspectors concluded that the
failure to obtain the authorizing signature on the WR prior to starting work in accordance
with BAP 1600-1 was a violation of minor significance and is being treated as a Non-Cited
Violation, consistent with Section IV of the NRC Enforcement Policy
(50-454/98009-03(DRP)).
The inspectors' procedural reviews and interviews with licensee personnel identified that !
the work control process, as defined in BAP 1600-1, did not have steps to place a WR on
. hold, with the intention of later rescheduling the work activities. Generally, the
maintenance managers' expectations were that a WR was scheduled and controlled
using the scheduling process. However, no expectations or requirements existed to
control the signature page authorization to place a WR on hold and restart the work '
activity at a later date.
After being questioned by the inspectors, the licensee identified approximately 50 out of
160 WRs on hold in the maintenance department that still had authorized SRO
signatures. The inspectors were concemed that the plant conditions may not be
appropriate for the WRs and therefore, the SRO's work authorization signature should
- have been removed. ;
Title 10 CFR Part 50, Appendix B, Criterion V, " Instructions, Procedures, and Drawings,"
required, in part, that activities affecting quality shall be of a type appropriate to the
circumstances. The inspectors concluded that the failure to have established a written
procedure for the control of WRs while the WRs were on hold, was an example of a
violation of 10 CFR Part 50, Appendix B, Criterion V (50-454/455-98009-02b(DRP)).
At the end of the inspection period the licensee was in the process of revising
BAP 16001 to control WRs on hold. The licensee had also removed the signature pages
from the 50 WRs on hold that had contained the authorizing SRO signatures.
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c. Conclusions
The inspectors noted that generally, WRs were adequately controlled and scheduled.
However, the inspectors identified one example whace work was being accomplished
without proper SRO authorization. Also, approximately 50 WRs had SRO authorizations,
but the work activities were not on the current schedule, and were considered on " hold."
The inspectors concluded that Byren Administrative Procedure (BAP) 1600-1 was
inadequate in that it did not provide guidance on how to process a WR that had been
authorized by an SRO, and then the work activity had been put on " hold" for an extended
period of time. A violation was issued.
M8 Miscellaneous Maintenance issues
M8.1 (Closed) Violation (50-454/455-96012-03a(DRP)) (92902): " inadequate Corrective Action
for Heat Exchanger Assembly." The inspector reviewed the licenses corrective actions
which included coaching of the mechanical maintenance personnelinvolved in the event
on attention-to-detail and procedure adherence. The inspector also reviewed the
licensees root cause investigation and found it acceptable. This portion of the violation is
closed. It should also be noted that the second portion of this violation,
(50-454/455-96012-03b(DRP)), was previously closed and documented in NRC
Inspection Report No. 50-454/97018(DRP); 50-455/97018(DRP). Thus the entire
violation (50-454/455-96012-03(DRP)) is closed.
Ill. Enaineerina
E3 Engineering Procedures and Documentation
E3.1 Failure to Update the Uodated Final Safety Analysis Report (37551)
The inspectors walked down portions of the containment purge system while it was
operating. The inspectors reviewed safety evaluation T1-93-0152, completed on
October 16,1993, which documented a change to the operating procedure of the
containment purge system during refueling operations. The safety evaluation specified
that the containment mini-purge system would be in operation during refueling activities
and the main containment purge system would be secured. The UFSAR,
Section 15.7.4.2.2.3 indicated that during refueling operations, the containment purge
system was to be in operation and providing at least 50 feet per minute (fpm) air flow
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across the refueling cavity surface. The safety evaluation did not discuss the technical
basis for the acceptability of lower transport times associated with the decreased flow
provided by the containment mini-purge system.
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ln addition, the safety evaluation stated that a change to the UFSAR was required;
however, the licensee did not submit the required revision to the UFSAR in
December 1994 or December 1996. The UFSAR change was then scheduled for
submittal in December 1998, but was subsequently canceled. At the end of the
inspection period, the licensee was still investigating the technical basis for the
acceptability of the lower transport times associated with the operation of the containment
mini-purge system and the basis for the failure to update the UFSAR. This issue is
considered an Unresolved item (50-454/455-98009-04(DRP)) pending NRC review of the
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licensee's technical basis for the acceptability of the containment mini-purge system and
the causes for the failure to update the UFSAR.
IV. Plant Support
R1 Radiological Protection and Chemistry (RP&C) Controls
R1.1 Radioloalcal Postinas
1
i a. Inspection Scope (71750)
!
The inspectors routinely observed the status and posting of radiologically controlled areas
(e.g., radiologically posted areas, radiation areas, radiologically contaminated areas).
The inspectors interviewed operators and radiation protection personnel and reviewed
Byron Radiological Protection Procedure (BRP) 5010-1, " Radiological Posting and I
Labeling Requirements," Revision 15.
b. Observations and Findinas
During an inspection in the auxiliary building on March 9,1998, the inspectors noted a '
step-off pad and radiological waste .eceptacle within the 1 A SI pump cubicle adjacent to
the entrance. The inspectors noted radiological rope boundaries established with two
" CAUTION CONTAMINATED AREA" signs along two of three accessible sides of the
area. In the location where the step-off pad and radiological waste receptacle were
located, the inspectors did not identify any radiological tape, rope or " CAUTION
l CONTAMINATED AREA" sign present, leaving approximately a seven foot opening in the
contamination area boundary unposted. The two signs that had been posted could not
be read from the unposted side. The inspectors noted that BRP 5010-1, Paragraph F.3,
stated that any radiologically posted area shall be conspicuously posted so as to wam
personnel approaching the area from any direction. This problem was exacerbated by
the fact that the unposted area was immediately adjacent to the pump cubicle entrance.
In response to the inspectors concems, the shift manager had the posting immediately
corrected.
Technical Specification 6.8.1.a required that written procedures be established,
implemented and maintained for procedures recommended in Appendix A, of Regulatory '
Guide 1.33. Appendix A of Regulatory Guide 1.33, specified contamination control as an
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example of a radiation protection procedure. The failure to post the contamination area
within the 1 A Si pump cubicle in accordance with BRP 5010-1 was a violation of ,
TS 6.8.1.a (50-454/98009-05(DRP)), as described in the attached Notice of Violation.
c. Conclusions
The inspectors concluded that the licensee failed to post a contamination area in
accordance with radiological protection procedure Byron Radiological Protection
Procedure 5010-1.
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V. Manaaement Meetinas
X1 Exit Meeting Summary
l
The inspectors presented the inspection results to members of licensee management at
the conclusion of the inspection on April 6,1998. The licensee acknowledged the
i findings presented. The inspectors asked the licensee whether any materials examined
l during the inspection should be considered proprietary. No proprietary information was ,
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identified.
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PARTIAL LIST OF PERSONS CONTACTED
Licensee
' K Graesser, Site Vice-President
K Kofron, Byron Station Manager
J. Bauer, Health Physics Supervisor
D. Brindle, Regulatory Assurance Supervisor
E. Campbell, Maintenance Superintendent
T. Gierich, Operations Manager
.T. Schuster, Manager of Quality & Safety Assessment
M. Snow, Work Control Superintendent
B. Kouba, Engineering Manager
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INSPECTION PROCEDURES USED !
IP 50001: Steam Generator Replacement inspection l
lP 61726: Surveillance Observations
IP 62707: Maintenance Observations
IP 71707: Plant Operations
IP 37551: Engineering
IP 71750: Plant Support
IP 92700: Onsite Followup of Written Reports of Nonroutine Events at Power !
Reactor Facilities '
lP 92901: Followup operations
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IP 92902: Followup Maintenance 1
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ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
50-454/98009-01 VIO Unit i entered Mode 4 with portions of containment i
floor drain inoperable.
l
50-454/455-98009-02a VIO Inadequate procedure (BOP VC-2) for operation of )
control room ventilation
50-454/455-98009-02b VIO Failure to have established a written procedure for
the control of WRs while the WRs were on hold.
50-454/98009-03 NCV Failure to obtain authorizing signature on Work ;
Request.
50-454/455-98009-04 URI Potential failure to submit a UFSAR revision for
containment purge operation.
50-454/455-98009-05 VIO Failure to post the contamination area in
accordance with BRP 5010-1. I
Closed !
50-454/455-95003-01(DRP)
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IFl RCS Pressure Transient Required the Shutdown of ,
the 2D RCP
50-454/455-96012-03a(DRP) VIO Inadequate Corrective Action for Heat Exchanger
Assembly.
50-454/455-96012-05(DRP) VIO Failure to Follow a Procedure for a Degraded
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Containment Floor Drain Monitoring System. I
50-454/98004 LER Reactor Coolant Leak Detection System Inoperable
Due to inadequate Communication
50-454/98009-03(DRP) NCV Failure to obtain authorizing signature on Work
Request.
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LIST OF ACRONYMS USED
BAP Byron Administrative Procedure
BAR Byron Annunciator Response
BMP Byron Mechanical Maintenance Procedure
BOP Byron Operating Procedure
3OS Byron Operating Surveillance
i BRP Byron Radiological Protection Procedure
BVS Byron Engineering Surveillance
DEL Degraded Equipment Log
DG Diesel Generator
DRP Division of Reactor Projects l
DRS Division of Reactor Safety
ECCS Emergency Core Cooling System
l ER Engineering Request
l ESFAS Engineered Safety Feature Actuation Signal i
FME Foreign Material Exclusion l
FPM Feet per Minute l
HLA Heightened Level of Awareness l
HVAC Heating, Ventilating, and Air Conditioning
IFl inspector Follow-up item
IPSS In-Plant Shift Supervisor ,
LCO Limiting Condition for Operation I
LCOAR Limiting Conditio, for Operation Action Requirement
LER Licensee Event Report
NCV Non-cited Violation
NOD Nuclear Operating Division
NRC Nuclear Regulatory Commission
NSWP Nuclear Station Work Procedure
OOS Out-of-Service
PDR Public Document Room
PlF Problem identification Form
PPM Parts Per Million
QNE Qualified Nuclear Engineer
RCP Reactor Coolant Pump
RP Radiological Protection
RP&C Radiological Protection and Chemistry
SI Safety injection
SM Shift Manager
SPP Special Plant Procedure
SRO Senior Reactor Operator
SX Essential Service Water System
TS Technical Specification
UFSAR Updated Final Safety Analysis Report
US Unit Supervisor
VIO Violation