05000387/FIN-2016004-02
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Finding | |
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Title | Failure to Promptly Correct a Condition Adverse to Quality with LPCI Swing Bus Automatic Transfer Switches |
Description | Green. A finding of very low safety significance (Green) and associated NCV of Title 10 Code of Federal Regulations (CFR) 50, Appendix B, Criterion XVI, Corrective Action, was self-revealed when Susquehanna failed to assure that conditions adverse to quality were promptly identified and corrected on two separate occasions. Both examples resulted in the failures of safety-related automatic transfer switches (ATSs) associated with the low pressure coolant injection (LPCI) swing buses. Corrective actions included enhancing the work instructions for all applicable ATSs based off original equipment manufacturer (OEM) input and scheduling the enhanced work instructions to be performed on the four swing bus ATSs during their next scheduled bus outages. Inspectors determined that the finding was more than minor because it was associated with the Equipment Performance attribute of the Reactor Safety Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). In both examples, the failure to correct conditions adverse to quality resulted in the loss of power to the LPCI swing bus and inoperability of the respective division of LPCI. In accordance with IMC 0609.04, Initial Characterization of Findings, dated June 19, 2012, inspectors and Exhibit 2 of IMC 0609, Appendix A, The SDP for Findings At-Power, dated June 19, 2012, inspectors determined that the finding was of very low safety significance (Green). Specifically, though a single train was inoperable for greater than its technical specification (TS) allowed outage time, in consultation with regional senior reactor analysts, inspectors determined it did not represent an actual loss of function. The finding is related to the cross-cutting area of Problem Identification and Resolution, Evaluation, because Susquehanna did not thoroughly evaluate issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, Susquehanna either failed to evaluate deficiencies encountered during maintenance or failed to ensure that corrective actions aligned with and corrected the identified causes. [P.2] |
Site: | Susquehanna |
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Report | IR 05000387/2016004 Section 1R12 |
Date counted | Dec 31, 2016 (2016Q4) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71111.12 |
Inspectors (proximate) | B Smith D Schroeder E Gray J Deboer J Furia J Greives P Ott S Anderson T Daun |
Violation of: | 10 CFR 50 Appendix B Criterion XVI |
CCA | P.2, Evaluation |
INPO aspect | PI.2 |
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Finding - Susquehanna - IR 05000387/2016004 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Susquehanna) @ 2016Q4
Self-Identified List (Susquehanna)
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