05000387/FIN-2016001-03
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Finding | |
|---|---|
| Title | Failure to Correct Fatigue Related Cracking of the B RRP Lower Seal Cavity Vent Line |
| Description | A self-revealing finding of very low safety significance (Green) and associated NCV of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, was identified for Susquehannas failure to establish measures to assure a condition adverse to quality was corrected. Specifically, vibration induced fatigue cracking on the Unit 1 B reactor recirculation pump (RRP) lower seal cavity vent piping was not corrected in December 2014 after a reactor coolant pressure boundary leak had occurred. This resulted in another reactor coolant pressure boundary leakage at the same location with Unit 1 operating in Mode 1, a condition prohibited by technical specifications (TS) LCO 3.4.4. Susquehannas entered the issue into the corrective action program (CAP) as CR-2015-30901 and replaced and modified the union that included the weld. The finding was more than minor because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The inspectors evaluated the finding in accordance with Exhibit 1 of IMC 0609, Appendix A, The significance determination process (SDP) for Findings At-Power, and determined the finding was of very low safety significance (Green) because the leakage would not have exceeded the reactor coolant system (RCS) leak rate for a small loss of coolant accident (LOCA) and it did not affect other systems used to mitigate a LOCA. This finding had a cross-cutting aspect in the area of Human Performance, Work Management, because Susquehanna did not implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority, in that Susquehanna did not adequately coordinate the work activities with different groups [H.5]. Specifically, welding engineers were not engaged in the decision making process during the December 2014 repair and consequently the repair was inadequate to ensure the entire crack had been removed. |
| Site: | Susquehanna |
|---|---|
| Report | IR 05000387/2016001 Section 4OA3 |
| Date counted | Mar 31, 2016 (2016Q1) |
| Type: | NCV: Green |
| cornerstone | Initiating Events |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71153 |
| Inspectors (proximate) | D Schroeder J Grieves N Floyd P Meier T Daun |
| Violation of: | 10 CFR 50 Appendix B Criterion XVI Technical Specification |
| CCA | H.5, Work Management |
| INPO aspect | WP.1 |
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Finding - Susquehanna - IR 05000387/2016001 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Susquehanna) @ 2016Q1
Self-Identified List (Susquehanna)
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