05000387/FIN-2016004-04
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Finding | |
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| Title | Auxiliary Bus Load Shed when a Daisy Chained Neutral was Interrupted during Maintenance |
| Description | Green. A finding of very low safety significance (Green) for failure to develop an adequate work plan for replacement of a voltage potential indicating light on a breaker on the Unit 2 B auxiliary bus was self-revealed when the Unit 2 B reactor recirculation pump (RRP) tripped, along with other non-safety related loads on November 14, 2016, resulting in a rapid unplanned power change and transition to single loop operation. Specifically, operations and maintenance personnel did not recognize that disconnecting the neutral wires from the light socket would interrupt power to all of the degraded voltage relays for the auxiliary bus. Therefore, the relays de-energized when the maintenance was performed, tripping all the breakers on the bus. Susquehannas immediate corrective actions included stabilizing the plant, entering single loop operations, and entering the issue into their corrective action program (CAP). Additionally, Susquehanna performed a maintenance department stand down to communicate immediate lessons learned from the event while a more thorough causal analysis was conducted. The performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone and affected its objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, implementation of work instructions resulted in the trip of the Unit 2 B RRP, B and D circulating water (CW) pumps, B and D condensate pumps, and the B service water (SW) pump, which caused an automatic trip of the C reactor feed pump and runback of the A RRP, resulting in a rapid power reduction to 32 percent rated thermal power (RTP). The inspectors evaluated the finding in accordance with IMC 0609, Appendix A "The SDP for Findings At-Power," dated June 19, 2012, Exhibit 1 for the Initiating Events cornerstone and determined the finding was of very low safety significance (Green) because it did not cause a reactor trip. This finding was determined to have a cross-cutting aspect in the area of Human Performance, Work Management because Susquehanna did not implement a process of planning work activities such that nuclear safety is the overriding priority, including the identification and management of risk commensurate with the work. Specifically, Susquehanna did not recognize the risk of interrupting a daisy chained neutral when planning a minor maintenance work order and did not recognize the impact of the work activity in the field. [H.5] |
| Site: | Susquehanna |
|---|---|
| Report | IR 05000387/2016004 Section 4OA3 |
| Date counted | Dec 31, 2016 (2016Q4) |
| Type: | Finding: Green |
| cornerstone | Initiating Events |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71153 |
| Inspectors (proximate) | B Smith D Schroeder E Gray J Deboer J Furia J Greives P Ott S Anderson T Daun |
| CCA | H.5, Work Management |
| INPO aspect | WP.1 |
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Finding - Susquehanna - IR 05000387/2016004 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Susquehanna) @ 2016Q4
Self-Identified List (Susquehanna)
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