05000388/FIN-2016008-03
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Finding | |
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Title | Failure to Implement or Develop Timely Interim or Final Corrective Actions for a Degraded Condition |
Description | The inspectors documented a self-revealing finding of very low safety significance (Green) against Susquehanna procedures LS-125 Revision 4, Corrective Action Program (CAP), and OI-AD-096 Revision 18, Operator Challenges, for the failure to correct and establish appropriate corrective actions for a known degraded condition for an uninterruptable power supply (UPS) for vital 120 VAC load centers. Specifically, Susquehanna did not correct nor establish compensatory actions for the transfer switch for a UPS which was failed for over one year. The degraded condition subsequently complicated operator response to the loss of a vital 480 VAC switchboard and resulted in an unplanned manual reactor scram and valid emergency core cooling system (ECCS) actuation on May 13, 2016. Susquehanna entered this issue into their CAP, conducted an apparent cause evaluation, and repaired the UPS transfer switch. The finding was more than minor because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone and adversely affected the associated cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the long standing degraded condition of UPS 2D14212/2B246082 was not corrected or compensated for and did not function as designed, as a result operators had to manually scram the reactor following the loss of a vital bus on May 13, 2016. In accordance with IMC 0609.04, Initial Characterization of Findings, dated June 19, 2012, and Exhibit 1 of IMC 0609, Appendix A, The SDP for Findings At-Power, dated June 19, 2012, the inspectors determined that this finding is of very low safety significance (Green) because the performance deficiency did not cause both a reactor trip and loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Specifically, while this performance deficiency resulted in a reactor scram, it was not the cause of the loss of mitigation equipment credited in the Susquehanna safety analysis. This finding had a cross-cutting aspect in the area of Problem Identification and Resolution Resolution because the organization did not take effective corrective actions to address issues in a timely manner commensurate with its safety significance. Specifically, failing to establish appropriate compensatory actions for this known degraded condition, prevented the operators from responding appropriately to a loss of a vital 480 VAC switchboard initiating event. [P.3]. [Section 4OA2.1.c(3)] |
Site: | Susquehanna ![]() |
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Report | IR 05000388/2016008 Section 4OA2 |
Date counted | Sep 30, 2016 (2016Q3) |
Type: | Finding: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | A Rosebrook A Siwy D Schroeder M Draxton T Daun |
CCA | P.3, Resolution |
INPO aspect | PI.3 |
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Finding - Susquehanna - IR 05000388/2016008 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Susquehanna) @ 2016Q3
Self-Identified List (Susquehanna)
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