05000416/LER-1982-163-03, /03L-0:on 821211,during Routine Power Supply Switching Operation,Both Shutdown Cooling Loops Isolated. Caused by Momentary Loss of Power to Rps.Shutdown Cooling Restored

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/03L-0:on 821211,during Routine Power Supply Switching Operation,Both Shutdown Cooling Loops Isolated. Caused by Momentary Loss of Power to Rps.Shutdown Cooling Restored
ML20028D326
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 01/07/1983
From: Freeman M
MISSISSIPPI POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028D325 List:
References
LER-82-163-03L, LER-82-163-3L, NUDOCS 8301170422
Download: ML20028D326 (1)


LER-1982-163, /03L-0:on 821211,during Routine Power Supply Switching Operation,Both Shutdown Cooling Loops Isolated. Caused by Momentary Loss of Power to Rps.Shutdown Cooling Restored
Event date:
Report date:
4161982163R03 - NRC Website

text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION At ent A

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LICENSEE EVENT REPORT Page 1 of 1 o

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8 60 61 OOCKET NUMBER 68 69 EVENT OATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lOl2l l On December 11, 1982, during a routine power supply switchinc operation. both shutdownl [o l3 l l cooling loops isolated.

A LCO was entered in accordance with T.S.3.4.9.2. however.

l l o l 4 l l shutdown cooling loop A vas returned to operation af ter 5 minutes. This event had noj [olst leffect on the health and safety of the public and did not constitute a threat to planti IOl6ll safety. The event is being reported pursuant to T.S.6.9.1.13.b.

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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 I i l o l lThe relays which control the isolation valves for shutdown cooline receive their I

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When the nower sunn11es for thin cy e nn lwere switched the isolation relays momentarilv lost power and caused a shutdown l

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l i l 3 l l cooling isolation.. Immediately after the switch, shutdown cooline was restored to l

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This is a finn 1 renorr.

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% POWE R OTHER STATUS DISCO RY DISCOVERY DESCRIPTION NA l

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8 9 10 68 69 80 5 NANIE OF PREPARE,priginal signed by M. Scott Freeman PHON E :