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Category:NPDES NONCOMPLIANCE NOTIFICATION
MONTHYEARML20065K1141994-03-14014 March 1994 NPDES Noncompliance Notification:On 940407,fecal Coliform Limitation Exceeded During Upset of Sewage Treatment Plant 2B (DSN011),as Result of Influent Flow Surge.Caused by Temporary Hydraulic Overload.Chlorine Feed Rate Maximized ML20011E8301990-02-0707 February 1990 NPDES Noncompliance Notification:Beginning on 891221,oil & Grease at River Water Bldg Sump Discharge Exceeded Permit Limit.No Specific Cause Could Be Determined.Sump Resampled on 900110 ML19332D3491989-11-21021 November 1989 NPDES Noncompliance Rept for Third Quarter 1989 ML20244A5051989-06-0606 June 1989 NPDES Noncompliance Notification:On 890517,discovered High Total Residual Chlorine Level from Sample Obtained on 890516 at Miscellaneous Cooling Waters Discharge Point.Caused by Improperly Functioning Valve.Valve Will Be Repaired ML20236P7081987-11-0909 November 1987 NPDES Noncompliance Notification:On 871020,TSS Limit Exceeded.Caused by Draining of Portions of Unit Circulating Water Sys Causing TSS Value of 167 Mg/H.Release Temporary Condition of Short Duration.Impact Negligible on Environ ML20213F9751987-05-0808 May 1987 Joseph M Farley Nuclear Plant Units 1 & 2 Quarterly NPDES Discharge Monitoring Rept & Noncompliance Summary for First Quarter 1987 ML20214H8901986-09-30030 September 1986 Summary of NPDES Noncompliances for Third Quarter 1986.W/ ML20203K3441986-08-0707 August 1986 Summary of NPDES Noncompliance Notifications for Second Quarter 1986,including Excessive Oil & Grease in Transformer Area Oil Separator 021 & Low Ph in Sewage Plant 011 ML20128D5601985-04-29029 April 1985 NPDES Noncompliance Notification:On 850419,analyses of Samples Collected Indicated Total Suspended Solids Concentration of 29.67 Kg/Day for Turbine Bldg Sump.Caused by Abnormally High Vol of Water from Various Sources ML20064D0861978-10-24024 October 1978 NPDES Noncompliance on 781020,6,500 Gallons of Water Containing Ph of 10.5 Discharged,Exceeding Permit Limit of 6-9.0.Caused by air-operated Valve Failing in Open Position 1994-03-14
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML20205S9571998-12-31031 December 1998 Annual Radioactive Effluent Release Rept for Farley Nuclear Plant for 1998 ML20207D7191998-12-31031 December 1998 Tabulation of Personnel Radiation Exposure for 1998 by Work & Job Function for Jm Farley Nuclear Plant. with L-99-016, 1998 Annual Environ Operating Rept (Nonradiological) for Jm Farley Nuclear Plant. with1998-12-31031 December 1998 1998 Annual Environ Operating Rept (Nonradiological) for Jm Farley Nuclear Plant. with L-99-174, Jm Farley Nuclear Plant Radiological Environ Operating Rept for 1998. with1998-12-31031 December 1998 Jm Farley Nuclear Plant Radiological Environ Operating Rept for 1998. with ML20206B5571998-12-31031 December 1998 Jm Farley Nuclear Plant Radiological Environ Operating Rept for 1998. with ML20217N8001997-12-31031 December 1997 Annual Radioactive Effluent Release Rept for CY97 for Jm Farley Nuclear Plant,Units 1 & 2 ML20217E1131997-12-31031 December 1997 Forwards 1997 Radiological Environmental Operating Rept ML20217G1091997-12-31031 December 1997 Annual Environ Operating Rept for 1997 (Nonradiological) ML20237C9841997-12-31031 December 1997 Amended Page 94 of Jm Farley Nuclear Plant Annual Radioactive Effluent Rept for 1997 ML20138B9071996-12-31031 December 1996 1996 Annual Environ Operating Rept (Nonradiological) ML20135D2401996-12-31031 December 1996 Tabulation of Personnel Radiation Exposure at Jm Farley Nuclear Plant for 1996 by Work & Job Functions ML20140E9591996-12-31031 December 1996 Radiological Environ Operating Rept for 1996 ML20138A3501996-12-31031 December 1996 Annual Radioactive Effluent Release Rept for FY96 ML20107L8581995-12-31031 December 1995 Annual Radioactive Effluent Release Rept for CY95 ML20107M1091995-12-31031 December 1995 Jm Farley Nuclear Plant,Radiological Environ Operating Rept for 1995 ML20100J5241995-12-31031 December 1995 Tabulation of Personnel Radiation Exposure at Jm Farley Nuclear Plant for 1995 by Work & Job Function ML20101H1791995-10-24024 October 1995 NPDES Permit AL0024619,issued to Southern Nuclear Operating Co Farley Nuclear Plant ML20078J1901994-12-31031 December 1994 Tabulation of Personnel Radiation Exposure at Jm Farley Nuclear Plant for 1994 Work & Job Function ML20087H4981994-12-31031 December 1994 Annual Environ Operating Rept Part B:Radiological Jm Farley Nuclear Plant Units 1 & 2 for Period Ending 941231. W/ ML20087H4531994-12-31031 December 1994 Annual Radioactive Effluent Release Rept CY94 ML20081G9311994-12-31031 December 1994 Annual Environ Operating Rept for 1994 (Nonradiological) ML20065K1141994-03-14014 March 1994 NPDES Noncompliance Notification:On 940407,fecal Coliform Limitation Exceeded During Upset of Sewage Treatment Plant 2B (DSN011),as Result of Influent Flow Surge.Caused by Temporary Hydraulic Overload.Chlorine Feed Rate Maximized ML20063L5971993-12-31031 December 1993 1993 Annual Rept of Radiation Dose Distribution ML20063K7681993-12-31031 December 1993 Tabulation of Personnel Radition Exposure at Jm Farley Nuclear Plant for 1993 by Work & Job Function ML20029C9901993-12-31031 December 1993 Semiannual Radioactive Effluent Release Rept Jul-Dec 1993. W/940427 Ltr ML20029D3271993-12-31031 December 1993 Annual Environ Operating Rept Part B:Radiological Jm Farley Nuclear Plant Units 1 & 2 Period Ending 931231. ML20056F1281993-06-30030 June 1993 Semiannual Radioactive Effluent Release Rept Jan-June 1993 ML20029D3291992-12-31031 December 1992 Amended Pages to Annual Environ Operating Rept Part B: Radiological Jm Farley Nuclear Plant Units 1 & 2 for Period Ending 931231. ML20128K4841992-12-31031 December 1992 1992 Annual Rept of Radiation Dose Distribution ML20128K5731992-12-31031 December 1992 Tabulation of Personnel Radiation Exposure at Jm Farley Nuclear Plant for 1992 by Work & Job Function ML20012G4401992-12-31031 December 1992 Semiannual Radioactive Effluent Release Rept Jul-Dec 1992. W/930226 Ltr ML20114B4441992-06-30030 June 1992 Semiannual Radioactive Effluent Release Rept,Jan-June 1992 ML20101A5611991-12-31031 December 1991 Jm Farley Nuclear Plant 1991 Annual Environ Operating Rept (Nonradiological) ML20095K0601991-12-31031 December 1991 Annual Environ Operating Rept Part B:Radiological. W/ ML20092N0131991-12-31031 December 1991 Semiannual Radioactive Effluent Release Rept Jul-Dec 1991 ML20082K9651991-06-30030 June 1991 Semiannual Radioactive Effluent Release Rept - Jan Through Jun 1991 ML20029B1661990-12-31031 December 1990 Semiannual Radioactive Effluent Release Rept Jul-Dec 1990. W/910226 Ltr ML20073D9071990-12-31031 December 1990 Annual Environ Operating Rept Part B:Radiological ML20073E8151990-12-31031 December 1990 Annual Environ Operating Rept for 1990 (Nonradiological) ML20029A9701990-12-31031 December 1990 1990 Annual Rept of Radiation Dose Distribution. W/910228 Ltr ML20065D6671990-08-15015 August 1990 NPDES Permit AL0024619,issued to Alabama Power Co Farley Nuclear Plant ML20059B5661990-06-30030 June 1990 Semiannual Radioactive Effluent Release Rept Jan-June 1990 ML20042G5351990-03-31031 March 1990 Summary of NPDES Noncompliances for First Quarter 1990. W/900508 Ltr ML20011E8301990-02-0707 February 1990 NPDES Noncompliance Notification:Beginning on 891221,oil & Grease at River Water Bldg Sump Discharge Exceeded Permit Limit.No Specific Cause Could Be Determined.Sump Resampled on 900110 ML20012A1651989-12-31031 December 1989 Amended, Semiannual Radioactive Effluent Release Rept for Jul-Dec 1989. ML20055C3811989-12-31031 December 1989 Annual Rept of Radiation Dose Distribution at Jm Farley Nuclear Plant for 1989 ML20011F7511989-12-31031 December 1989 Semiannual Radioactive Effluent Release Rept,Jul-Dec 1989. W/900223 Ltr ML20042E9191989-12-31031 December 1989 Annual Environ Operating Rept Part B:Radiological. W/900430 Ltr ML19332D3491989-11-21021 November 1989 NPDES Noncompliance Rept for Third Quarter 1989 ML20246P2241989-06-30030 June 1989 Semiannual Radioactive Effluent Release Rept Jan-June 1989 1998-12-31
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g NT 86-0354 Ciling Addre:4 Alibima Power Comp:ny 600 North 18th Street Post Office Box 2641 Birmingham Alabama 35291 Telephone 205 783-6090 R. P. Mcdonald Senior Vice President Flintndge Duilding AlabamaPower
~ysm .me...
August 7, 1986 Dr. J. N. Grace oF U. S. Nuclear Regulatory Comission -
Region II, Suite 2900 ,O, >
101 Marietta Street, $ [j Atlanta, Georgia 30323 .__
Subject:
J. M. Farley Nuclear Plant NPDES Noncompliance Report
Dear Dr. Grace:
In accordance with the J. M. Farley Nuclear Plant Technical Specifications Appendix B, Section 3.2, please find attached a summary of NPDES noncompliances for the second quarter of 1986.
Should you have further questions, please advise.
Yours very t y, R. P. Mcdonald RPM / MAT:emb Attachment xc: Mr. W. H. Bradford (w/ attachment) 8608200250 860807 PDR ADOCK 05000348 S PDR U.S.NRC REGION U OFFICIAL COPY TE.W fft-
Farley Nuc11er Plant AL 0024619 i Permit Analytical Cause of Test Period of Noncompliance
! Discharge Point Parameter Limit Value Noncompliance
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Corrective Measures Date 5egan Ended Sew y Plant pH 6.0 s.u. 5.95 s u. These low values A vendor was con-(011) 4/02/86 were caused by low tracted to remove
, 5.38 s.u. flow combined with some sludge on 4/07/96 4/02/86 4/10/86 i
aged sludge. 4/9/86 which helped 5.73 s.u. Increase the pH. 4/08/86 I
Sew y Plant TSS 45 mg/l 464 mg/l Failure of a clapper The valve was se- 4/23/86 4/17/86 4/19/86('I (009) valve in the fire curred on 4/19/86 protection system and a procedural at the Training change was made to Facility allowed give guidance on large quantitles investigating the of water to hy. fire protection drau11cally over- system when high in-load 009. fluent flow occurs.
Plant TSS 45 mg/l 104 mg/l A backflow of water A work request was(2) 4/28/86 Indeterminate Seef009) through 009's dis- made to reroute this charge line into discharge to prevent the final effluent the backflow from chamber. occurring and should be initiated in the fall of 1986.
(1) Indicates date effluent should have returned within permit Ilmits.
(2) stequest also covers occurrence on 5/20/86.
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Farley Nuclear Plant AL 0024619 Permit Analytical Cause of Test Period of Noncompliance Discharge Point Parameter Limit Value Noncompilance Corrective Measures Date Began Ended Transformer Oil 20 mg/l 28 mg/l Rainf all flow Change out of oli ab-Area Oil & 5/19/86 Indeterminate probably caused di- sorbent material will Separator Grease sintegration of continue on a weekly (021) the oli absorbent basis. A study of the material. separator has been re-quested to determine if further action is needed.
Sewage Plant 5/20/86 III TSS 45 mg/l 253 mg/l A backflow of water (009) See footnote (2) 5/22/8f. 5/20/86 into the STP's final effluent chamber occurred.
Seway Plant 6.0 s.u.
5/30/86 III pH 5.92 s.u. This was caused by A vendor was 5/29/86 5/27/B6 (011) a combination of low scheduled to waste 5.87 s.u. flow and aged sludge on 6/3/86 sludge. and at that time new micro-organisms will be added.
(1) Indicates date effluent should have returned within permit limits.
- 3) ,
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1 Farl:y Nuc11er Plant AL 0024619 Permit Analytical Caus1 of . TIst Period af Noncompilanct .
Discharge Point Parameter Limit value Moncompliance Corrective Measures Date Besen Ended Seway Plant pH 6.0 sou. 5.76 s.u. These noncompliances On 6/3/86 4,000 6/09/86 (011) 5.13 s.u. resulted from low gallons of sludge 6/11/86 6/09/86 6/16/86 5.56 s.u. flow, aged sludge was wasted. However, 6/14/86 and over aeration. this alone did not 5.06 s u. correct the pH level. 6/17/86 5.28 s.u. On 6/30/86 the 6/17/86 6/17/86 6/21/86 5.46 s.u. aeration time was 6/18/86 4.85 s u. reduced which brought 6/20/86 compliance. Procedures 5.72 s.u. were estab11shed 6/30/86 6/30/86 7/01/86 5.7 s.u. during periods of low 6/30/R6 sewage input, a low aeration rate will be maintained and sludge periodically wasted.
Daily Average Analytical Test Daily Maximum Discharge Point Parameter Permit Limit Value Date Permit Limit Turbine Building TSS 30 mg/l 53 mg/l 4/10/86 100 mg/l Sump Unit 2 (016) TSS 30 mg/l 40 mg/l 5/14/86 130 mg/l Transformer TSS 30 mg/l 96 og/l 5/06/86 100 mg/l Area Oil Separator 011 and 15 mg/l 16 mg/l 6/03/86 20 mg/l (021) Grease
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