ML20011E830
| ML20011E830 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 02/07/1990 |
| From: | Hairston W ALABAMA POWER CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9002220552 | |
| Download: ML20011E830 (2) | |
Text
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'. 40 inverness Center Parkway. :;
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Post Office Box 1295.
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. Birmingham, Alabama 35201.
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' Telephone 205 868 6581 4
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. W. G. Hairston. H1
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' Senior Vice President :
@n Nuclear Operations AlabamaPower
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the southern electic system -
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^ February 7,1990 3
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Docket Nos.
50;348
~50-364 U. S. Nuclear Regulatory Commission-1
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- Attention:
Document Control Desk y'
Washington,.D. C.
20555 LGentlemen:.
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< Joseph M. Farley Nuclear Plant
!Duarterly NPDES Noncomoliance Reoort 8
Enclosed in accordance with Subsection 3.2 of the Joseph.M. Farley Nuclear
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Plant ~ Environmental Protection Plan '(Units 1: and 2), Appendix B~ to Facility J'
Operating License Nos. NPF-2 and NPF-8, is'a' summary of NPDES
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noncompliances-for the fourth quarter of 1989 as transmitted to the Alabama R
~ Department of Environmental Management.
If you have any questions,- please advise.
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Respectfully. submitted, 1
' W.k h W. G; Hairston, III
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.WGH,III/TCH
' Enclosure t
cc:
Mr.'S. D. Ebneter
- Mr. E. A. Reeves Mr. G. F. Maxwell 1
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9002220552 900207
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. This tabliis submitted ta fctrill reguirements.of PaEt18.8.5 and Part III.0 ' -
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'Farley Nuc1 car Plant NP065 Permit No.' ALOD24619
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~Cause ofa.
Test'. Period of Wilance ; U"~
Permit ~
- Analytical
' Eischarge Point
' Parameter Lielt.
Value Noncompliance':
1 Corrective Measures L Sete -
Began --
Emees-
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..15.1 mg/l
~No spectfic cause.. Since no cause.could 1/10/90;.12/21/89. ~ prior toi
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' River Water Building 011 & Grease-15.0 mg/l'
.1/10/90-Sump Discharge
.(daily average).
- could be determined. be determined, no; (DSN 022)
.The area was inspect. specific action could i
-ed upon notification be taken. The sump
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s; and no indication was resampled on 1/10/90,'
of oil leaks was-the day the plant was '
.found.
'A review'of -notified of the value-s 3.f records of previous. of.15.1 mg/1, and the 3-area inspections in-value was 1.2 og/1.
dicated no o11' leaks-were det,ected.
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