ML20011E830

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NPDES Noncompliance Notification:Beginning on 891221,oil & Grease at River Water Bldg Sump Discharge Exceeded Permit Limit.No Specific Cause Could Be Determined.Sump Resampled on 900110
ML20011E830
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 02/07/1990
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9002220552
Download: ML20011E830 (2)


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'. 40 inverness Center Parkway. :;

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Post Office Box 1295.

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. Birmingham, Alabama 35201.

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' Telephone 205 868 6581 4

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. W. G. Hairston. H1

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' Senior Vice President :

@n Nuclear Operations AlabamaPower

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the southern electic system -

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^ February 7,1990 3

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Docket Nos.

50;348

~50-364 U. S. Nuclear Regulatory Commission-1

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- Attention:

Document Control Desk y'

Washington,.D. C.

20555 LGentlemen:.

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< Joseph M. Farley Nuclear Plant

!Duarterly NPDES Noncomoliance Reoort 8

Enclosed in accordance with Subsection 3.2 of the Joseph.M. Farley Nuclear

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Plant ~ Environmental Protection Plan '(Units 1: and 2), Appendix B~ to Facility J'

Operating License Nos. NPF-2 and NPF-8, is'a' summary of NPDES

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noncompliances-for the fourth quarter of 1989 as transmitted to the Alabama R

~ Department of Environmental Management.

If you have any questions,- please advise.

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Respectfully. submitted, 1

' W.k h W. G; Hairston, III

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.WGH,III/TCH

' Enclosure t

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Mr.'S. D. Ebneter

- Mr. E. A. Reeves Mr. G. F. Maxwell 1

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9002220552 900207

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. This tabliis submitted ta fctrill reguirements.of PaEt18.8.5 and Part III.0 ' -

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'Farley Nuc1 car Plant NP065 Permit No.' ALOD24619

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~Cause ofa.

Test'. Period of Wilance ; U"~

Permit ~

- Analytical

' Eischarge Point

' Parameter Lielt.

Value Noncompliance':

1 Corrective Measures L Sete -

Began --

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..15.1 mg/l

~No spectfic cause.. Since no cause.could 1/10/90;.12/21/89. ~ prior toi

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' River Water Building 011 & Grease-15.0 mg/l'

.1/10/90-Sump Discharge

.(daily average).

could be determined. be determined, no; (DSN 022)

.The area was inspect. specific action could i

-ed upon notification be taken. The sump

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s; and no indication was resampled on 1/10/90,'

of oil leaks was-the day the plant was '

.found.

'A review'of -notified of the value-s 3.f records of previous. of.15.1 mg/1, and the 3-area inspections in-value was 1.2 og/1.

dicated no o11' leaks-were det,ected.

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