NRC-93-0055, LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr

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LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr
ML20044F156
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 05/20/1993
From: Conen J, Gipson D
DETROIT EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
CON-NRC-93-0055, CON-NRC-93-55 LER-93-007, LER-93-7, NUDOCS 9305270022
Download: ML20044F156 (6)


Text

. ..

Douglas R. Gipson  !

, vice f rrscent >

NcD3r OperMQ95 Detroit r-ma Ecison !EsEF" m1. l 10CFR50.73 May 20, 1993 NRC-93-0055 I

U. S. Nuclear Regulatory Commission Attention: Document Control Desk '

Washington, D.C. 20555  ;

Reference:

Fermi 2 NRC Docket No. 50-341 .

NRC License No. NPF-43  !

Subject:

Licensee Event Report (LER) No.93-007 Please find enclosed LER No.93-007, dated May 20, 1993 for a i reportable event that occurred on April 20, 1993

~

A copy of this LER is also being sent to the Regional Administrator, USNRC Region III.

If you have any questions, please contact Mr. Joseph Conen at (313) 586-1960 .

Sincerely, {

hMN i i

Enclosure:

NRC Forms 366, 366A .

I cc: T. G. Colburn W. J. Kropp J. B. Martin M. P. Phillips  ;

P. L. Torpey f

Wayne County Emergency  !

Management Division t i

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Fermi 2 l 05000341 1 OF 4

%m Re6ctor irlp on intermediate R6nge Monitor Upscale During keactor Fressure and Feedwater Transient.

EVENT DATE (5) LER NUtABER (6' REPORT NUMBER (7) OTHER F ACILITIES INVOLVE D (B) m ,3 m. ys m ,uw w mve v a.:,, cu o <t w qu , ,,, en cu vtw 95999 04 20 93 93 - 007 -

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Joseph E. Conen, Compliance Engineer (313) 5S6-1960 ,

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SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED N W +-

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m:.o t rf ato sav uos tcr" X ABSTRACT tum:t to20, On April 1400 spaces 1993, i e . the with approca*e'y reactor 15atsmg'e-spaced 510 psig dur t@eemen imes) (16)ing startup, a control room  ;

operator noticed that the main steam manifold pressure control system was unexpectedly switching between the "A" and "B" regulators when the Electric Governor Trouble Alarm actuated and the turbine bypass valves opened approximately i 40 percent. Reactor pressure began to decrease and reactor water level increased -

due to increased void fraction resulting from the increased steam flow. The increased void fraction also led to a decrease in reactor power. When control room operators began to gradually close the bypass valves, reactor water level decreased. As water level decreased through the normal operating band, feedwater  ;

flow automatically increased. The addition of cold feedwater caused reactor power .

to increase until the reactor automatically tripped on Intermediate Range Monitor  !

upscale. All safety systems responded properly.

i This event occurred because leakage past a threaded adapter allowed steam and water to leak into an instrument cabinet which contained the pressure transmitters used to control main steam manifold pressure, causing failure of these transmitters. ,

The cause of the event was personnel error in that a threaded adapter used to  !

install temporary test equipment for startup monitoring did not match the fitting l

< into which it was threaded. Training will be conducted on this event to reinforce '

the need for control of contractor activities. .

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REQUIRED NUMBER OF DIGITS / CHARACTERS FOR EACH BLOCK BLOCK NUMBER OF E

NUMBER DIGITS / CHARACTERS 1 UP TO 46 FACILITY NAME 2 DO N NUMBER 3 IN ADDITION TO 05000 3 VARIES FAGE NUMBER 4 UP TO 76 TITLE U^

2 PER BL CK 7 TOTAL j 6

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FACILITY NAME p) DOCAfT NUMBER (21 LER NUMBER (,) PAGE (3)

YEAA NJMF!81 NUVBER Fermi 2 05000341 OF 93 - 00,/ -

00 2 4

,w m .,v.n. n .a ... m . w m um on Initial Plant Conditions:

Operational Condition: 2 Startup Reactor Power: 3 Percent Reactor Pressure: 510 psig Reactor Temperature: 472 degrees Fahrenheit Description of Event:

On April 20, 1993 a plant startup was in progress. The reactor was at 510 psig and power was being maintained on Intermediate Range Monitor [(IRM)(IG)] ranges 7 and 8 (estimated at 3 percent power) for heatup to rated pressure. At 1127 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.288235e-4 months <br /> alarm 4D91 " Electric Governor Trouble" ( ANN) actuated and a control room operator noticed that main steam manifold pressure control was unexpectedly switching between the two regulators (PC). The main turbine bypass valves (JI) opened approximately 40 percent, corresponding to the limit imposed by the reactor flow limiter setting.

(Note that prior to this transient the bypass valves were fully closed, as expected.) As reactor pressure began to decrease, water level increased due to void formation from the increased steam flow. This caused a high water level trip of the north reactor feedpump turbine (SK) which was being warmed in preparation for feeding the vessel. This pump was not being utilized for level control at this stage of reactor startup. Reactor power decreased due to higher core void i fraction, and the operator [ utility, licensed] ranged down the IRM's to ranges 3 and 4 to maintain indication on scale.

In accordance with the Abnormal Operating Procedure, an operator [ utility, licensed] began to lower the reactt. flow limiter setting to gradually close the bypass valves. 'Ihis reduced steam flow, and reactor water level began to decrease due to decreasing void fraction. In response to decreasing water level, the startup level control valve [(SULCV)(LCV) automatically opened resulting in an  ;

increase in feedwater flow to the reactor. This addition of cold water caused reactor power to increase. At 1131 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.303455e-4 months <br />, while the operator [ utility, licensed]

was attempting to range up the IRM's in response to the increase in reactor power, the reactor tripped on IRM upscale.

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Cause of Event:

Following the trip, an engineer [ utility, non-licensed] investigating the pressure regulator problems found steam and water leaking from a fitt.ing in instrument mI tes c FORW 366A (5-02)

NRp FORM 366A U.S. NUCLE.AR HEGULAToRY COMMISSION APPROVED BY oMB No. 3150-0104 se EXP!RES 5/31/95 I STtMA'ED BJADEN PER REEPONSE TD COMr'iy wvM TH$

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un - u .. .- - e w m on cabinet H21P258 (CAB) which contains the two pressure transmitters (PT) used by the main steam manifold pressure regulators. The leaking fitting was isolated and the ,

transmitters were inspected for damage. Both transmitters had water inside their protective housings and had failed electrically. This failure of the main steam manifold pressure signal initiated the pressure transient.

The subject fitting was installed on April 17, 1993 to connect a test instrument for monitoring main steam manifold pressure during the startup. The leak occurred because a 3/8 inch 24 thread per inch (3/8-24 TPI) adapter was mistakenly used where a 1/8 inch National Pipe Thread (1/8 NPT) adapter was needed. This is considered to be a personnel error. The technician [ contractor, non-licensed] had both types of adapters and failed to adequately verify that the correct adapter was ,

selected in this case. Additionally, contractor control contributed to the event.

Fermi 2 personnel [ utility, non-licensed] relied too heavily on a technically ,

experienced contractor and failed to ensure adequate verification was performed for '

the installed parts.

A total of six pressure transducers were installed to monitor pressure at various locations during startup. The vendor had only four adapters of each type available for these transducers. Thus, it was necessary to use botn types to install the ,

required test instruments. Although the adapters are physically similar, it was i understood that t. hey were not interchangeable, and the adapters were marked with part numbers to distinguish types. The use of two different types of adapters contributed to the event by creating the opportunity for this error.

I Analysis of Event:

The steam and water leakage which initiated this event was small and its effects ,

confined to the instrument cabinet where it occurred. The leak was easily isolated i by an adjacent manual instrument valve without incident. Operator action to terminate the depressurization transient kept Reactor Coolant System cooldown I within limits specified by Technical Specifications. The automatic reactor shutdown initiated by the IRM Upscale trip terminated the reactor power transient  !

as designed, such that reactor power did not increase beyond the startup range. j Reactor water level briefly exceeded the high level trip setpoint for turbine '

driven equipment, which resulted in a trip of the north reactor feedpump (the only turbine driven equipment operating) which was being warmed in preparation for ,

feeding the reactor. Water level never decreased below the setpoints for actuation of any safety system. Therefore, the health and safety of the public and plant personnel were not affected by this event. Had this event occurred in Operational 1

NRO FORM 36bA (5 G2)

MRC FORM 366A U.S. NUCLEAR PEGULAToRY COMMISSloN APPROVED BY oMB NO. 3150-0104

!S ei EXPIRES 5/31/95  :

ESTfMPED BURDEN PER RESPONSE TO COMPuY WTM TH:S LICENSEE EVENT REPORT (LER) $ % s% &R$ fe% % $ E 5 ?o O d % h*2 TEXT CONTINUATION QS "MSc3"^7^$*M87.5"1788 ",d'Ay,LM THE FAptrewoRK Rcos: TON Fu!ECT c1504tos;. OrFCE Or M ANAGEMENT AND BUDGE'T, w ASHiNGTON. DO 23533 F ACiLITY NAME (t) l DOCKET NUMEER !2) LJ R NUMBE R (5) PAGE (3) q LLWiMA. HE v50N NJVBE R NUMBER Fermi 2 05000 341 4 or 4 93 -

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00

,w m. ,vu . n,1 - .n- an.w += w xm <m Condition 1 (power operation) the reactor pressure and power transients would have been less severe; however, decrease in reactor water level would have been larger due to the trip of the reactor feed pumps at rated pressure. This transient is discussed in UFSAR Section 15.1 3 -

Corrective Actions:

The affected pressure transmitters were replaced. Other instrumer.ts in the instrument cabinet were inspected for water intrusion and no water was found. All

)

of the remaining pressure transducers installed for this testing were removed, '

verified to be correctly assembled, and shop tested to correct any leakage prior to ,

reinstallation. The transducer / adapter assembly which leaked was removed and a L replacement was installed on an open rack considered to be less susceptible to damage should the assembly fa'.l. The locations of the other 5 transducer I assemblies were also examined to ensure similar problems wou'ld not occur if they I failed.

An accountability meeting for this event was conducted with Fermi management, the involved engineer [ utility, non-licensed] and his supervisor to discuss causes for the event. Lessons learned from this incident will be communicated to other appropriate personnel through maintenance personnel Continuing Training, Licensed Operator Requalification Training, and Tech Staff and Managers Continuing Training. This training will be completed by October 31, 1993 t

In addition, special training will be conducted for personnel who are responsible for preparing, checking and approving permanent and temporary design changes. This special training will deal with both contractor control and the design and ,

installation of test and monitoring equipment. This special training will be  !

completed by August 31, 1993 Guidance for designing test and monitoring equipment will also be put into FIP-OP1-02, Temporary Modifications, and this procedure will '

be revised by June 30, 1993 Previous Similar Events:

LER 87-035 and 88-020 discuss previous reactor trips caused by IRM upscale trips during feedwater transients.

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I NRO FORM 3e% @421

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