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Category:NPDES NONCOMPLIANCE NOTIFICATION
MONTHYEARML20206C9871999-04-27027 April 1999 NPDES Noncompliance Notification:On 990319,station Personnel Observed Foam Emanating from Manhole Vent Associated with Outfall 001,no Foam Was Observed on Any Waterway.Caused by Inappropriate Addition of Betz 3625 to Spray Pond ML20207D6171999-02-26026 February 1999 NPDES Noncompliance Notification:On 990111,discovered That Weelkly Analysis for non-oxidizing Biocide Betz 3625 Was Not Performed.Caused by Sample Being Inappropriately Delayed for Future Chemical Addition.Counseled Individuals Involved ML20202F0591999-01-19019 January 1999 NPDES Noncompliance Notification:On 990112,Auxiliary Boiler Source Number OAS502 Found to Have Malfunctioning Opacity Monitor.Caused by Stepdown Transformer within Power Supply. Power Supply Replaced ML20198J2811998-12-21021 December 1998 NPDES Noncompliance Notification:On 981102,release of 500 Gallons of 12% Sodium Hypochlorite to Environment Occurred. Caused by Failure of Tank Discharge Fittings.Integrity Testing Will Be Performed on All New Tanks.With ML20206R3491998-12-21021 December 1998 NPDES Noncompliance Notification:On 981102,500 Gallons of 12% Sodium Hypochlorite Released to Environ.Caused by Failure of Tank Discharge Fittings & Subsequent Leaks from Secondary Containment.Culvert Was Flushed Repeatedly ML20236V2001998-07-27027 July 1998 NPDES Noncompliance Notification:On 980619,geometric Mean Coliform Concentration Calculated to Be 223 Colonies Per 100 Ml.Sample Procedure Enhanced to Ensure Normal Operating Conditions ML20248C9461998-05-27027 May 1998 NPDES Noncompliance Notification:On 980414,total Iron Discharge Through Outfall 001 Exceeded Limits Set in Ltr Dtd 960508.Total Iron Discharge Limit Exceeded During Cleaning Evolution.Limit Revised ML20217N6921998-02-27027 February 1998 NPDES Noncompliance Notification:On 980107 Net Total Suspended Solids (TSS) for Units 1 & 2 Cooling Towers at Outfall 001 Exceeded NPDES Permit Daily Limit of 60 Ppm. Caused by Contaminated Sample Lines.Replaced Tygon Tubing ML20141G0271997-06-27027 June 1997 NPDES Noncompliance Notification:On 970512,sample for Kjeldahl Omitted Due to Personnel Error.Counseled Individual Responsible.On 970521,Net TSS Exceeded NPDES Daily Limit Due to Fouled Sample Tubing.Replaced Sample Tubing ML20137M5511997-03-27027 March 1997 NPDES Noncompliance Notification:On 970228,flow Integrator Used to Measure Spray Pond Effluent Flow Was Identified to Be Malfunctioning & Declared Inoperable Due to Lodged Debris.Revised Procedure for Spray Pond Effluent Flow ML20134G3241997-01-31031 January 1997 NPDES Noncompliance Notification:On 970108,util Informed NRC That PA Dept of Environ Protection Granted Approval for Temporary Discharge at Lgs,Per 961219 ML20138G9651996-12-24024 December 1996 NPDES Noncompliance Notification:On 960428,calibration of Flowmeter Used to Measure Spray Pond Flow Was Not Checked on Routine Basis Because Person Required to Develop Maint Was Unaware of Requirements.Installed New Meter ML20135A5851996-11-27027 November 1996 NPDES Noncompliance Notification:On July-Sept 1996 Re NPDES Limit for Fecal Coloform Concentration Not Met.Caused by Inadequate Gasket Installation.Ozonators Overhauled to Ensure Peak Performance ML20134E0641996-10-28028 October 1996 NPDES Noncompliance Notification:During Month of Sept 1996, NPDES Limit for Fecal Coliform Concentration at Discharge of Bradshaw Reservoir Pumps Was Not Met.Caused by Leaking Gaskets on Ozone Gas Diffusers.New Gaskets,Installed ML20129E5681996-09-27027 September 1996 NPDES Noncompliance Notification:On 960805,geometric Mean of Fecal Coliform Concentration Calculated to Be 641 Colonies Per 100 Ml.Cause Suspected to Be Due to Malfunctioning Ozone Disinfection Sys.Adjustments to Sys Have Been Made ML20129E5411996-09-26026 September 1996 NPDES Noncompliance Notification:On 960812,discharge Observed from Unit 2 Cooling Tower Overflow to Outfall 021. Caused by Personnel Error in Performing Required Analysis of Cooling Tower Overflow Sample.Individual Counseled ML20117G7071996-08-23023 August 1996 NPDES Noncompliance Notification:On 960715,geometric Mean of Fecal Coliform Concentration Exceeded NPDES Permit Limit. Caused by Leaking Seals on Ozone Diffusers.Temporary Adjustments Made to Ozone Gas Flow Balance ML20116B3851996-07-24024 July 1996 NPDES Noncompliance Notification:On 960602 Identified Ph Levels Exceeded NPDES Permit Limitations.Caused by Natural Biological activity.CO2 Injection Established,Maintained & Monitored Until 960612 ML20115G1151996-07-12012 July 1996 NPDES Noncompliance Notification:On 960619,resulting Net TSS Value 82.8 mg/1,exceeded Max Daily Limit of 60 Mg/L.Caused by Excessive Storm Water Runoff.Net TSS Revised ML20113C4451996-06-24024 June 1996 NPDES Noncompliance Notification:On 960318,flow Integrator Used to Measure Spray Pond Effluent Flow Declared Inoperable.Caused by Faulty Flow Integrator.Frequency of Use of Instrument Changed to Daily as Stated in Issue Number ML20108A3671996-04-28028 April 1996 NPDES Noncompliance Notification:On 960314,personnel Observed Sewage Overflowing from MH-07 & Into Storm Drain W-4.Caused by Blockage of Pipe Section Between MH-07 & MH-08.Sewer Contract Svc Pressure Cleaned ML20108A3801996-04-28028 April 1996 NPDES Noncompliance Notification:On 960223,identified Seven Issues of Administrative non-compliance/ambiguity W/Permits. Caused by Inadequate Administration.Individuals Gained Better Understanding W/Guidance ML20101K4661996-03-28028 March 1996 NPDES Noncompliance Notification:On 960218,discovered That No Records Existed for Bradshae Reservoir Discharge Water Temp for Listed Time Periods.Caused by Temporary Reassigment of Personnel.Review of Staffing in Progress ML20100P6311996-02-28028 February 1996 NPDES Noncompliance Notification:On 951108,discharge 001 Net TSS in Excess of Maximum Daily Limit.Caused by Flaw in Methodology to Calculate Net TSS concentration.Follow-up Composite Samples Taken ML20072R4601994-08-31031 August 1994 NPDES Noncompliance Notification:On 940708 & 0815,Discharge 001 Total Zinc Concentrations Exceeded Max Daily Limitations.Daily Zinc Trending Analysis Will Be Upgraded & Chemistry Technician Involved in 940815 Event Counselled ML20071L1761994-07-27027 July 1994 NPDES Noncompliance Notification:On 940609,zinc Analyses Indicated That Discharge 001 Total Zinc Levels in Excess of Max Daily Limitations in Both Cooling Towers.Daily Zinc Control Limits Will Be Administratively Maintained Lower ML20149E7291994-07-26026 July 1994 NPDES Discharge Monitoring Rept:On 940713,approx 18 Gallons of Betz Clamtrol CT-1 Inadvertently Released from Injection Sys Located South of LGS Spraypond Pumphouse.Caused by Break in Pump Discharge Line.Polyethylene Piping Replaced ML20065B9221994-03-25025 March 1994 NPDES Noncompliances Notification:On 940204,discharge 001 Maximum Daily Limit of 1.0 mg/1 Total Zinc Was Exceeded. Caused by Low Ph Transient in Unit 2 Cooling Tower Water Sys.Isolated Acid Injection Sys ML20064C7701994-02-25025 February 1994 NPDES Noncompliance Notification:On 940116 & 17 Manual Reactor Scram Occurred.Caused by Failure to Adequately Throttle Cooling Tower Bypass Valves.Procedure Revised ML20059C4941993-10-26026 October 1993 NPDES Noncompliance Notification:On 930907,cooling Tower Blowdown Water Discharged Into Possum Hollow Creek Due to Loss of Two of Four Operating Circulating Water Pumps. Procedures for Performing Excavations Revised ML20056G3921993-08-27027 August 1993 NPDES Noncompliance Notification:On 930710,13,14 & 25, Water Processing Facility (Wpf) Discharge Temp Exceeded Max Limitation of 74 Degrees F.Rev to NPDES Permit,Removing Temp Limits Approved & Wpf Chillers Removed from Svc ML20024H8441993-08-19019 August 1993 NPDES Noncompliance Notification Re Perkiomen Storage Tank Overflow to Possum Hollow Run.Application for Amend to Permit PA0051926 Submitted ML20046B8051993-07-29029 July 1993 NPDES Noncompliance Notification:On 930618,20 & 27,water Processing Facility Temp Exceeded Permitted Max Limitation of 74 Degrees F.Caused by Lack of Training & Written Instructions.Training Provided & Addl Instruction Issued ML20044G7641993-05-21021 May 1993 NPDES Noncompliance Notification:From 930417-18,equipment Problems Occurred Which Rendered Dissolved Oxygen & Ph Monitoring Instrumentation Inoperable.Caused by Debris in Sample Line.Methods for Filtering Flow Under Investigation ML20044C4051993-03-16016 March 1993 NPDES Noncompliance Notification:On 930222,discovered That Contractor Personnel Discharged Treated Water from Fire Hydrant Supplied by Unit 1 Cooling Tower Into Storm Water Drain E-3.2.Caused by Personnel Error.Label Applied ML20128N1251993-02-17017 February 1993 NPDES Noncompliance Notification:On 930103,cooling Tower Blowdown Water Overflowed from Discharge 001 Pipeline & Flowed Into Possum Hollow Creek.Caused by Failure to Throttle Unit 2 Bypass Valves.Procedure Changed ML20128A5071993-01-25025 January 1993 NPDES Noncompliance Notification:On 921117 & 25,analytical Results for inductively-coupled Plasma Analyzer at Discharge Point 001 Exceeded Zinc Concentration.Total Zinc Concentration Analysis Will Be Performed Onsite ML20126G9991992-12-24024 December 1992 NPDES Noncompliance Notification:On 921104,dissolved Oxygen Monitoring Equipment at Bradshaw Reservoir Discharge & Water Processing Facility Became Fouled by Organic Concentrations. Caused by Heavy Rainfall.Manual Samples Will Be Obtained ML20117A5761992-11-23023 November 1992 NPDES Noncompliance Notification:On 921013 & 14,four of Five Samples Collected from Discharge Point 001 Exceeded Daily Max Permit Limit of 1.0 Mg/L.Caused by Heavy Rains Across Southeastern PA on 921009.Injection Rates Decreased ML20101H5321992-06-26026 June 1992 NPDES Noncompliance Notification:On 920504,crack Discovered on Above Ground Cleanout for Sewage Line Leading from Plant Training Ctr to Plant Sewage Sys Holding Tanks.Caused by Expansion of Sewage Spill Line.Clamps Installed ML20095J1201992-04-23023 April 1992 NPDES Noncompliance Notification:On 920322,cooling Tower Blowdown Water Discharged Into Possum Hollow Creek.Caused by Procedure Deficiency.Sys Operating Procedure S09.4.A Expected to Be Revised by 920501 ML20141M0551992-03-25025 March 1992 NPDES Noncompliance Notification:On 920206,rain Water Pumped from Eletrical Manhole Into Storm Water Runoff Drain Due to Inadequate Procedural Guidance.Blue Drains to Be Labelled, Indicating Use for Storm Water Runoff Only by 920801 ML20091Q4301992-01-23023 January 1992 NPDES Noncompliance Notification:On 911218 Cooling Tower Blowdown Water Discharged to Possum Hollow Creek Resulting in Unpermitted Discharge Due to Failure to Identify & Revise All Appropriate Procedures.Procedure GP-3 to Be Revised ML20086E4981991-11-22022 November 1991 NPDES Noncompliance Notification:On 911016 Underground Fire Water Pipeline Inadvertently Punctured by Contractor Backhoe Ram During Excavation of Trench.Caused by Inadequate Review of Required Prints.Backhoe Ram Operator Terminated ML20082L9871991-08-28028 August 1991 NPDES Noncompliance Notification:On 910707 & 19,electrical Storm Caused Loss of Power to Bedminster Water Processing Facility & Tripped Chillers.On 910721,discharge Temp Exceeded Permitted Limits.Permit Limits Changed ML20217C2131991-07-0808 July 1991 NPDES Noncompliance Notification:On 910629,chillers at Bedminster Water Processing Facility for Bradshaw Reservoir Tripped Due to Unexpected Failure of Logic Control Unit. Chiller Control to Primary Computer Restored ML20077G5771991-06-20020 June 1991 NPDES Noncompliance Notification:On 910528,chiller C at Bedminster Water Processing Facility Tripped Due to High Vibration & Temp at Discharge 001 Exceeding Permitted Instantaneous Temp.Discharge Temp Setpoint Lowered ML20077D8701991-05-17017 May 1991 NPDES Noncompliance Notification:On 910512,cooling Tower Experienced Failure,Causing Large Vol of Cooling Tower Water to Bypass Normal Blowdown Discharge Pathway.Cooling Tower Will Be Inspected During mid-yr Outage ML20070S3071991-03-22022 March 1991 NPDES Noncompliance Notification:On 910204,discovered That Misalignment of Diverter Valve to Outfall 003 May Have Allowed Mixture of Storm Water & Steam Condensate to Be Released from Outfall.Valve Repositioned ML20065M6811990-11-29029 November 1990 NPDES Noncompliance Notification:On 901003,routine Weekly Discharge 001 Sample Exceeded Max Permit Limits for Grease & Oil.Sample Contained 43.7 Mg Per Liter of Oil & Grease. Abnormal Reading Believed to Be Caused by Oily Silt 1999-04-27
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML20206C9871999-04-27027 April 1999 NPDES Noncompliance Notification:On 990319,station Personnel Observed Foam Emanating from Manhole Vent Associated with Outfall 001,no Foam Was Observed on Any Waterway.Caused by Inappropriate Addition of Betz 3625 to Spray Pond ML20207D6171999-02-26026 February 1999 NPDES Noncompliance Notification:On 990111,discovered That Weelkly Analysis for non-oxidizing Biocide Betz 3625 Was Not Performed.Caused by Sample Being Inappropriately Delayed for Future Chemical Addition.Counseled Individuals Involved ML20202F0591999-01-19019 January 1999 NPDES Noncompliance Notification:On 990112,Auxiliary Boiler Source Number OAS502 Found to Have Malfunctioning Opacity Monitor.Caused by Stepdown Transformer within Power Supply. Power Supply Replaced ML20206E2161998-12-31031 December 1998 1998 Annual Environ Operating Rept (Non-Radiological) for Limerick Generating Station,Units 1 & 2 ML20205T0581998-12-31031 December 1998 Annual Radiological Environ Operating Rept 15 for 1998 ML20206R3491998-12-21021 December 1998 NPDES Noncompliance Notification:On 981102,500 Gallons of 12% Sodium Hypochlorite Released to Environ.Caused by Failure of Tank Discharge Fittings & Subsequent Leaks from Secondary Containment.Culvert Was Flushed Repeatedly ML20198J2811998-12-21021 December 1998 NPDES Noncompliance Notification:On 981102,release of 500 Gallons of 12% Sodium Hypochlorite to Environment Occurred. Caused by Failure of Tank Discharge Fittings.Integrity Testing Will Be Performed on All New Tanks.With ML20236V2001998-07-27027 July 1998 NPDES Noncompliance Notification:On 980619,geometric Mean Coliform Concentration Calculated to Be 223 Colonies Per 100 Ml.Sample Procedure Enhanced to Ensure Normal Operating Conditions ML20248C9461998-05-27027 May 1998 NPDES Noncompliance Notification:On 980414,total Iron Discharge Through Outfall 001 Exceeded Limits Set in Ltr Dtd 960508.Total Iron Discharge Limit Exceeded During Cleaning Evolution.Limit Revised ML20217N6921998-02-27027 February 1998 NPDES Noncompliance Notification:On 980107 Net Total Suspended Solids (TSS) for Units 1 & 2 Cooling Towers at Outfall 001 Exceeded NPDES Permit Daily Limit of 60 Ppm. Caused by Contaminated Sample Lines.Replaced Tygon Tubing ML20203H1911997-12-31031 December 1997 Annual Effluent Release Rept 23 for Jan-Dec 1997 ML20216F3371997-12-31031 December 1997 Annual Environmental Operating Rept (Non-Radiological) for 970101-1231 ML20203L5691997-12-31031 December 1997 Occupational Exposure Tabulation Rept for LGS Units 1 & 2 for 1997 ML20203H2201997-12-31031 December 1997 Tower 1 Joint Frequency Distributions of Wind Speed & Direction by Atmospheric Stability Class Rept 13 for 1997 ML20217P1941997-12-31031 December 1997 Annual Environ Operating Rept (Non-Radiological) for Jan-Dec 1997, for LGS Units 1 & 2 ML20217M6471997-12-31031 December 1997 Annual Radiological Environ Operating Rept 14,Jan-Dec 1997 for Limerick Generating Station,Units 1 & 2 ML20141G0271997-06-27027 June 1997 NPDES Noncompliance Notification:On 970512,sample for Kjeldahl Omitted Due to Personnel Error.Counseled Individual Responsible.On 970521,Net TSS Exceeded NPDES Daily Limit Due to Fouled Sample Tubing.Replaced Sample Tubing ML20137M5511997-03-27027 March 1997 NPDES Noncompliance Notification:On 970228,flow Integrator Used to Measure Spray Pond Effluent Flow Was Identified to Be Malfunctioning & Declared Inoperable Due to Lodged Debris.Revised Procedure for Spray Pond Effluent Flow ML20134G3241997-01-31031 January 1997 NPDES Noncompliance Notification:On 970108,util Informed NRC That PA Dept of Environ Protection Granted Approval for Temporary Discharge at Lgs,Per 961219 ML20135D0161996-12-31031 December 1996 Occupational Exposure Tabulation Rept for LGS Units 1 & 2 for 1996 ML20148B6671996-12-31031 December 1996 LGS Units 1 & 2 Annual Radiological Environ Operating Rept 13 for 960101-1231 ML20135C7691996-12-31031 December 1996 1996 Annual Effluent Release Rept No 22 ML20138J5291996-12-31031 December 1996 Annual Environ Operating Rept (Non-Radiological) for Jan- Dec 1996 ML20135C7731996-12-31031 December 1996 1996 Annual Tower No 1 Joint Frequency Distribution of Wind Speed & Direction by Atmospheric Stability Class Rept No 12 ML20138G9651996-12-24024 December 1996 NPDES Noncompliance Notification:On 960428,calibration of Flowmeter Used to Measure Spray Pond Flow Was Not Checked on Routine Basis Because Person Required to Develop Maint Was Unaware of Requirements.Installed New Meter ML20135A5851996-11-27027 November 1996 NPDES Noncompliance Notification:On July-Sept 1996 Re NPDES Limit for Fecal Coloform Concentration Not Met.Caused by Inadequate Gasket Installation.Ozonators Overhauled to Ensure Peak Performance ML20134E0641996-10-28028 October 1996 NPDES Noncompliance Notification:During Month of Sept 1996, NPDES Limit for Fecal Coliform Concentration at Discharge of Bradshaw Reservoir Pumps Was Not Met.Caused by Leaking Gaskets on Ozone Gas Diffusers.New Gaskets,Installed ML20129E5681996-09-27027 September 1996 NPDES Noncompliance Notification:On 960805,geometric Mean of Fecal Coliform Concentration Calculated to Be 641 Colonies Per 100 Ml.Cause Suspected to Be Due to Malfunctioning Ozone Disinfection Sys.Adjustments to Sys Have Been Made ML20129E5411996-09-26026 September 1996 NPDES Noncompliance Notification:On 960812,discharge Observed from Unit 2 Cooling Tower Overflow to Outfall 021. Caused by Personnel Error in Performing Required Analysis of Cooling Tower Overflow Sample.Individual Counseled ML20117G7071996-08-23023 August 1996 NPDES Noncompliance Notification:On 960715,geometric Mean of Fecal Coliform Concentration Exceeded NPDES Permit Limit. Caused by Leaking Seals on Ozone Diffusers.Temporary Adjustments Made to Ozone Gas Flow Balance ML20116B3851996-07-24024 July 1996 NPDES Noncompliance Notification:On 960602 Identified Ph Levels Exceeded NPDES Permit Limitations.Caused by Natural Biological activity.CO2 Injection Established,Maintained & Monitored Until 960612 ML20115G1151996-07-12012 July 1996 NPDES Noncompliance Notification:On 960619,resulting Net TSS Value 82.8 mg/1,exceeded Max Daily Limit of 60 Mg/L.Caused by Excessive Storm Water Runoff.Net TSS Revised ML20113C4451996-06-24024 June 1996 NPDES Noncompliance Notification:On 960318,flow Integrator Used to Measure Spray Pond Effluent Flow Declared Inoperable.Caused by Faulty Flow Integrator.Frequency of Use of Instrument Changed to Daily as Stated in Issue Number ML20108A3801996-04-28028 April 1996 NPDES Noncompliance Notification:On 960223,identified Seven Issues of Administrative non-compliance/ambiguity W/Permits. Caused by Inadequate Administration.Individuals Gained Better Understanding W/Guidance ML20108A3671996-04-28028 April 1996 NPDES Noncompliance Notification:On 960314,personnel Observed Sewage Overflowing from MH-07 & Into Storm Drain W-4.Caused by Blockage of Pipe Section Between MH-07 & MH-08.Sewer Contract Svc Pressure Cleaned ML20101K4661996-03-28028 March 1996 NPDES Noncompliance Notification:On 960218,discovered That No Records Existed for Bradshae Reservoir Discharge Water Temp for Listed Time Periods.Caused by Temporary Reassigment of Personnel.Review of Staffing in Progress ML20100P6311996-02-28028 February 1996 NPDES Noncompliance Notification:On 951108,discharge 001 Net TSS in Excess of Maximum Daily Limit.Caused by Flaw in Methodology to Calculate Net TSS concentration.Follow-up Composite Samples Taken ML20108C9281995-12-31031 December 1995 LGS Units 1 & 2 1995 Annual Environ Operating Rept (Non- Radiological) Jan-Dec 1995 ML20100L8861995-12-31031 December 1995 Annual Effluent Release Rept 21,Jan-Dec 1995 ML20108B7391995-12-31031 December 1995 Annual Radiological Environ Operating Rept 12 Jan-Dec 1995 ML20100L8961995-12-31031 December 1995 Tower 1 Joint Frequency Distributions of Wind Speed & Direction by Atmospheric Stability Class 1995 Rept 11 ML20080N1061994-12-31031 December 1994 Annual Effluent Release Rept 20 Jan-Dec 1994 PECO Energy LGS Units 1 & 2 ML20082N5061994-12-31031 December 1994 Annual Environ Operating Rept ML20087H7231994-12-31031 December 1994 Annual Radiological Environ Operating Rept 11 for Jan-Dec 1994 ML20080N1121994-12-31031 December 1994 Tower 1 Joint Frequency Distributions of Wind Speed & Direction by Atmospheric Stability Class 1994 Rept 10 ML20072R4601994-08-31031 August 1994 NPDES Noncompliance Notification:On 940708 & 0815,Discharge 001 Total Zinc Concentrations Exceeded Max Daily Limitations.Daily Zinc Trending Analysis Will Be Upgraded & Chemistry Technician Involved in 940815 Event Counselled ML20071L1761994-07-27027 July 1994 NPDES Noncompliance Notification:On 940609,zinc Analyses Indicated That Discharge 001 Total Zinc Levels in Excess of Max Daily Limitations in Both Cooling Towers.Daily Zinc Control Limits Will Be Administratively Maintained Lower ML20149E7291994-07-26026 July 1994 NPDES Discharge Monitoring Rept:On 940713,approx 18 Gallons of Betz Clamtrol CT-1 Inadvertently Released from Injection Sys Located South of LGS Spraypond Pumphouse.Caused by Break in Pump Discharge Line.Polyethylene Piping Replaced ML20065B9221994-03-25025 March 1994 NPDES Noncompliances Notification:On 940204,discharge 001 Maximum Daily Limit of 1.0 mg/1 Total Zinc Was Exceeded. Caused by Low Ph Transient in Unit 2 Cooling Tower Water Sys.Isolated Acid Injection Sys ML20064C7701994-02-25025 February 1994 NPDES Noncompliance Notification:On 940116 & 17 Manual Reactor Scram Occurred.Caused by Failure to Adequately Throttle Cooling Tower Bypass Valves.Procedure Revised 1999-04-27
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. PHILADELPIHA ELECTRIC COMPANY h LIMER]CK GENERATING STATION P. O. BOX 2300 SANATOGA, PA 19464-2300 (215) 327-1200 EXT, 2000 ROBERT W. BoYCE etAur umcER July 29, 1993 j LIMERICK CENERATING STATION l
Mr. Peter G. Noll Department of Health Neshaminy Manor Center l '
Doylestown, PA 18901
Subject:
Noncompliances with NPDES Permit Bradshaw Reservoir NPDES Permit No. PA-0052221 l l
Dear Mr. Noll:
l I
During the month of June 1993, six noncompliances with NPDES !
Permit No. PA-0052221, Bradshaw Reservoir, occcrred. Each
! noncompliance is described below including the causes and corrective actions.
- 1. DESCRIPTIONS OF THREE TEMPERATURE LIMITATION-NONCOMPLIANCES
- a. On June 18, following a trip of the Bradshaw Reservoir pumps, the Bedminster Water Processing Facility (WPF)' chillers shutdown as designed on low facility inlet flow. A delay'in the restoration of the WPF chillers caused the discharge temperature to exceed the permitted maximum limitation of 74 degrees F between 1200 and 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> with a maximum temperature of 75.4 degrees F.
I
- b. On June 20 at 2116 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.05138e-4 months <br />, an electrical storm caused a loss 1 of power to the Bedminster WPF chillers, the Bradshaw Reservoir Pump Station, and the Point Pleasant. Pumping i Station. Operations personnel responded and operators were i dispatched to the facilities; however, adequate steps were i not taken to restore the chillers to service by reclosing l electrical breakers for the WPF chillers. A Bradshaw Pump _
i was restarted at 2359 hours0.0273 days <br />0.655 hours <br />0.0039 weeks <br />8.975995e-4 months <br /> to restore flow to the East Branch Perkiomen Creek. On June 21 at approximately 0645 hours0.00747 days <br />0.179 hours <br />0.00107 weeks <br />2.454225e-4 months <br />, the chillers were returned to service and by 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br /> discharge temperature was less than 74 degrees F. As a result of a delay in the restoration of the WPF chillers, the WPF discharge temperature exceeded the permitted maximum limitation'of 74 degrees F between 2359 hours0.0273 days <br />0.655 hours <br />0.0039 weeks <br />8.975995e-4 months <br /> on June 20 and .l $
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.I 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br /> on June 21 with a maximum temperature of 79.5 degrees F. t I
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Additionally, at about 1030 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91915e-4 months <br /> on June 21, plant personnel i determined that the' discharge temperature control setpoint ;
for the WPF chillers had changed from 72 degrees F to 75.5 l degrees F. As a result, the WPF chillers were maintaining j
the discharge temperature at approximately 75 degrees F from {
0900 to 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on June 21. The setpoint change was l concluded by plant personnel to be the result of the !
electrical storm disturbances. The setpoint change incident I had never occurred previously, and was concluded to be an ;
isolated occurrence. The WPF chiller setpoint was lowered to. l 72 degrees F at 1030 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91915e-4 months <br />, and the discharge temperature '
stabilized below the permit limit by 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />.
?
- c. On June 27, plant personnel again identified that the i Bedminster WPF discharge temperature setpoint had changed i from 72 degrees F_to 75.5 degrees F. This resulted in the ;
discharge temperature exceeding the permitted maximum i limitation of 74 degrees F between 0700 and 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> with a !
maximum temperature of about 75 degrees F., The WPF chiller !
setpoint was lowered to 72 degrees F and the discharge !
temperature stabilized below the permit limit.
CAUSES OF THE NONCOMPLIANCES' o The cause of the delay in the restoration of the WPF !
chillers discussed in noncompliances la and^1b was the ;
lack of adequate training and written instructions to t Operations personnel regarding the necessary prompt ;
restoration of the WPF chillers following a trip. [
o A contributing factor to the noncompliance discussed in la was the frequent tripping of_the Bradshaw pumps which had been occurring over the preceeding several days for !
indeterminate reasons. Each trip challenges operators _j to promptly respond in order te control WPF chiller ;
dischange temperature.
I o The cause of the discharge temperature setpoint change j which occurred in noncompliances 1b and Ic was 'l
-incorrectly concluded to be the result of electrical i storm disturbances. An investigation performed by a WPF-computer specialist on June 27, determined that the electrical storm on June _20 did not cause the WPF ,
computer malfunction. The investigation ~ revealed that ')
the WPF computer temperature control setpoint change '
occurred as a result of a programming deficiency in the WPF computer software. j 1
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1 H 4 i
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Page 3 l PREVENTION OF FUTURE OCCURRENCES ,
o Training was given to appropriate Shift Operations personnel regarding WPF chiller restoration following a e trip, WPF chiller system status recognition utilizing the WPF computer, and the required operator actions to i be implemented in the event the discharge temperature i control setpoint cannot be maintained below 74 degrees ,
P. ;
o Additional written instructions were issued to Operations personnel specifying the necessary prompt, complete responses to Brad' haw Reservoir and Bedminster i WPF system trips, and loss of power events.
o Station Management stressed to Operations Supervision l the importance of immediate responses to Bradshaw ;
Reservoir and Bedminster WPF system problems. l o To address the contributing factor identified for j noncompliance la, internal and external power and 1 control circuits at the Bradshaw facility.are being !
monitored via event recorders to identify and isolate i the component failures ce_ sing the frequent tripping of the Bradshaw pumps. The appropriate corrective action j will be taken (e.g., replacement or design change) based on the information gatnered. ;
o On June 27 at 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />, numerous WPF computer software i I
programming changes were incorporated to ensure that the discharge temperature control setpoint cannot change to ,
a value which is greater than 74 degrees F without j manual manipulations. i l
o The revision to the NPDES permit in response to our j thermal variance request is pending issuance following :
the 30 day public comment period. Once issued, ,the WPF '
chiller operation will no longer be required since there _
will be no thermal limits.
- 2. DESCRIPTIONS OF TWO pH LIMITATION NONCOMPLIANCES-
- a. On June 19 at 0200 hrs, Operations. personnel identified-that the 'Bedminster WPF discharge pH exceeded the' permitted
. maximum limitation of 9.0 at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on June 18. The pH j of the discharge exceeded 9.0 through 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> on June-19, with a maximum pH of 9.2.
't In response to the identified increasing trend in pH over..the previous day, a temporary carbon dioxide (CO2) injection
-system was installed at the Bradshaw Reservoir in 'rder'to l avoid high pH however,-the initial CO2 flow rate vos insufficient. The CO2 flow rate was increased to its ;
maximum, and the pH stabilized below the permit limit at 0800 H hours on June 19. j e
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'b. On the evening of June 19, Operations personnel identified that the WPF discharge-pH permit limit of 9.0 was again being exceeded-(between 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br /> on June 19, and 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> on June 20, with a maximum pH of 9.2). At 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br /> on June 19 a manual grab sample was taken to confirm the indicated pH.
CAUSE OF THE NONCOMPLIANCES The cause of both noncompliances was determined to be the result of natural biologial activity enhanced by a raw sewage spill into the Delaware River which occurred on June 12, in the area of Easton, PA. Delaware River pH was equally elevated during this period of time.
PREVENTION OF FUTURE OCCURRENCES A second temporary CO2 sparger and additional-CO2 tanks were installed on June 22, to increase CO2 injection capability.
Since the occurrence on June 19, the natural biological activity has subsided, and pH values have remained below the permit limit. Presently, CO2 injection is not being.
performed.
- 3. DESCRIPTION OF ONE CADMIUM LIMITATION NONCOMPLIANCE' On June 22, the results of a cadmium grab sample _from June 8, were received and the concentration was slightly greater than the permit daily average limit of 0.0022 mg/L. The actual value was 0.0023 mg/L. This parameter was resampled on three more occasions and in each case-the value was less than 0.0022 mg/L. The monthly average was 0.00054 mg/L.
Inadvertently, this permit limit exceedance was not recognized as a 24-hour reportable condition. Notification was made on July 21.
CAUSE OF THE NONCOMPLIANCE o The cause of the honcompliance is suspected to be the result of a natural occurrence in the Delaware River, o The reason why this noncompliance was not identified as reportable on June 22, was due to an oversight by the System Manager.
PREVENTION OF A FUTURE OCCURRENCE No'long term corrective actions to prevent recurrence are planned.
Notifications of these noncompliances.were made to the Department of Health pursuant to NPDES permit requirements. In each instance, the requirement for submittal of a 5-day report was L
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' waived by the Department.and therefore, the required written !
report is being submitted in this letter. !
If you have any-questions please contact Jim Kantner at 327-1200 ' tl extention 3400.
i
.i Sincerely, i
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{ l I
.i DMS:cah cc: U.S. Nuclear Regulatory Commission l Document Control Desk !
Docket Nos. 50-352/50-353 .
Washington, D.C. 20555 1 l
T. T. Martin Administrator, Region I, USNRC I Docket Nos. 50-352/50-353 N. S. Perry j USNRC Senior Resident Inspector, LGS e Docket Nos. 50-352/50-353 ;
J. A. Feola -
Pennsylvania Department of Environmental Resources j Regional Water Quality Manager I Lee Park, Suite 6010 .
555 North Lane l Conshocken, PA 19428 !
Program Management Section (3WM52) .
Permits Enforcement Branch. ' '
, Environmental-Protection Agency }
Water Management-Division ,
. Environmental Protectior. Agency -j Water Permits Section Region'III ,
841 Chestnut Building *
-Philadelphia, PA 19107 ,
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