ML20009E620

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LER 81-011/03L-0:on 810528,during Insp of Unexpected Alarm, CS Header Break Detection Instrument Switches Found Piped to Incorrect Lines.Caused by Connection to Wrong Line at Drywell Penetration.Instruments Connected to Proper Lines
ML20009E620
Person / Time
Site: Cooper Entergy icon.png
Issue date: 06/16/1981
From: Flannigan R
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20009E596 List:
References
LER-81-011-03L, NUDOCS 8107280319
Download: ML20009E620 (1)


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' NRC)oRM 36r, U. S. NUCLE AR REGULATO'.Y COMMISSION (77H' # e-LICENSEE EVENT REPORT

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" ' 'o 69 R. D. Flannigan 402-825-3811 o i8107280319 810616 PHONE: g lPDR ADOCK 05000298 PDR LS