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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20028D9531983-01-0808 January 1983 LER 82-007/03L-0:on 821211,during Mode 5,review of Strip Chart Recordings of RCS Temps During Filling & Venting Operations on 821210 Indicated RCS Heatup Rate Exceeded. Caused by Inadequate Attention to Heatup Restrictions ML20028D3011982-12-23023 December 1982 LER 82-157/03L-0:on 821124,samples from Control Room Emergency Air Cleanup Sys Train a Charcoal Absorber Failed to Satisfy Methyl Iodine Removal Capability.Caused by Activated Charcoal Degradation.Charcoal Replaced 1983-01-08
[Table view] Category:RO)
MONTHYEARML20028D9531983-01-0808 January 1983 LER 82-007/03L-0:on 821211,during Mode 5,review of Strip Chart Recordings of RCS Temps During Filling & Venting Operations on 821210 Indicated RCS Heatup Rate Exceeded. Caused by Inadequate Attention to Heatup Restrictions ML20028D3011982-12-23023 December 1982 LER 82-157/03L-0:on 821124,samples from Control Room Emergency Air Cleanup Sys Train a Charcoal Absorber Failed to Satisfy Methyl Iodine Removal Capability.Caused by Activated Charcoal Degradation.Charcoal Replaced 1983-01-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217B4471999-10-0707 October 1999 Safety Evaluation Supporting Amends 159 & 150 to Licenses NPF-10 & NPF-15,respectively ML20217E3381999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Songs,Units 2 & 3 05000361/LER-1999-005-01, :on 990831,loss of Physical Separation in Control Room,Occurred.Caused by Personnel Error.Creacus Train a Was Returned to Standby on 9908311999-09-23023 September 1999
- on 990831,loss of Physical Separation in Control Room,Occurred.Caused by Personnel Error.Creacus Train a Was Returned to Standby on 990831
ML20212A1471999-09-13013 September 1999 Special Rept:On 990904,condenser Monitor Was Declared Inoperable.Difficulties Encountered During Component Replacement Precluded SCE from Restoring Monitor to Service within 72 H.Alternate Method of Monitoring Was Established ML20211R0571999-09-0909 September 1999 Safety Evaluation Supporting Amends 158 & 149 to Licenses NPF-10 & NPF-15,respectively ML20212A2391999-09-0707 September 1999 Safety Evaluation Supporting Amends 157 & 148 to Licenses NPF-10 & NPF-15,respectively ML20211N0511999-09-0303 September 1999 SER Approving Exemption from Certain Requirements of 10CFR50.44 & 10CFR50 App A,General Design Criterion 41 to Remove Requirements from Hydrogen Control Systems from SONGS Units 2 & 3 Design Basis ML13316A3631999-08-31031 August 1999 Change Notice 47,Amend 19 to Topical Rept SCE 1-A, QA Program Approvals 05000206/LER-1999-001-02, :on 990808,unattended Security Weapon Was Discovered Inside Pa.Caused by Posted Security Officer Falling Asleep.Officer Was Relieved of Duties,Pa Access Was Removed & Officer Was Placed on Investigatory Suspension1999-08-31031 August 1999
- on 990808,unattended Security Weapon Was Discovered Inside Pa.Caused by Posted Security Officer Falling Asleep.Officer Was Relieved of Duties,Pa Access Was Removed & Officer Was Placed on Investigatory Suspension
ML20211Q8201999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Songs,Units 2 & 3. with ML20211H8621999-08-23023 August 1999 Safety Evaluation Accepting Licensee Requests for Relief RR-E-2-03 - RR-E-2-08 from Exam Requirements of Applicable ASME Code,Section Xi,For First Containment ISI Interval ML20211E9441999-08-19019 August 1999 Safety Evaluation Supporting Amends 156 & 147 to Licenses NPF-10 & NPF-15,respectively ML20211F2211999-08-19019 August 1999 Safety Evaluation Supporting Amends 155 & 146 to Licenses NPF-10 & NPF-15,respectively ML20210P4791999-08-11011 August 1999 COLR Cycle 10 Songs,Unit 3 ML20210P4731999-08-11011 August 1999 COLR Cycle 10 Songs,Unit 2 05000361/LER-1999-004-01, :on 990708,automatic Tgis Actuation Occurred. Caused by Small Leak in Suction Side of Tgis Train a Sample Pump.Small Leak Repaired1999-08-0606 August 1999
- on 990708,automatic Tgis Actuation Occurred. Caused by Small Leak in Suction Side of Tgis Train a Sample Pump.Small Leak Repaired
ML20210Q6521999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Songs,Units 2 & 3 ML20210L2771999-07-30030 July 1999 SONGS Unit 3 ISI Summary Rept 2nd Interval,2nd Period Cycle 10 Refueling Outage U3C10 Site Technical Services 05000362/LER-1999-005, :on 990630,discovered LTOP Sys Relief Valve Setpoint Was Higher than Allowed by Ts.Cause Indeterminate. Subject Valve Will Be Disassembled & Inspected to Determine Caused of High Setpoint.With1999-07-28028 July 1999
- on 990630,discovered LTOP Sys Relief Valve Setpoint Was Higher than Allowed by Ts.Cause Indeterminate. Subject Valve Will Be Disassembled & Inspected to Determine Caused of High Setpoint.With
05000362/LER-1999-006, :on 990623,EDG 3G003 Was Inadvertently Made Inoperable.Caused by Operators Aligning EDG to Inoperable Automatic Voltage Regulator.Licensee Will Revise Process of Locating Tags.With1999-07-26026 July 1999
- on 990623,EDG 3G003 Was Inadvertently Made Inoperable.Caused by Operators Aligning EDG to Inoperable Automatic Voltage Regulator.Licensee Will Revise Process of Locating Tags.With
ML20209G8991999-07-12012 July 1999 Safety Evaluation Supporting Amends 154 & 145 to Licenses NPF-10 & NPF-15,respectively ML20209C9281999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Songs,Units 2 & 3. with 05000362/LER-1999-003-01, :on 990513,reactor Manually Tripped Due to Loss of Main Feedwater.Caused by Open Relay Contact in Output of Feedwater Regulation Control Sys.Faulty Relay Was Replaced1999-06-11011 June 1999
- on 990513,reactor Manually Tripped Due to Loss of Main Feedwater.Caused by Open Relay Contact in Output of Feedwater Regulation Control Sys.Faulty Relay Was Replaced
05000362/LER-1999-004, :on 990515,reactor Manually Tripped Due to Feedwater Control Valve Opening.Caused by Faulty Valve Positioner.Faulty Positioner Was Replaced1999-06-11011 June 1999
- on 990515,reactor Manually Tripped Due to Feedwater Control Valve Opening.Caused by Faulty Valve Positioner.Faulty Positioner Was Replaced
ML20195D3061999-06-0202 June 1999 Safety Evaluation of TR SCE-9801-P, Reload Analysis Methodology for San Onofre Nuclear Generating Station,Units 2 & 3. Rept Acceptable ML20195H5491999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Songs,Units 2 & 3 05000362/LER-1999-002-01, :on 990328,RWST Outlet Isolation Valve Failed to Open After Being Closed for Testing.Caused by Degradation of Valve.Rwst Oulet Valve Was Repaired.With1999-05-20020 May 1999
- on 990328,RWST Outlet Isolation Valve Failed to Open After Being Closed for Testing.Caused by Degradation of Valve.Rwst Oulet Valve Was Repaired.With
ML20207A0211999-05-13013 May 1999 Safety Evaluation Supporting Amends 153 & 144 to Licenses NPF-10 & NPF-15,respectively ML20196L3221999-05-11011 May 1999 SONGS Unit 2 ISI Summary Rept 2nd Interval,2nd Period Cycle-10 Refueling Outage ML20206H2611999-05-0505 May 1999 Part 21 Rept Re Defect Found in Potter & Brumfield Relays. Sixteen Relays Supplied in Lot 913501 by Vendor as Commercial Grade Items.Caused by Insufficient Contact Pad Welding.Relays Replaced with New Relays ML20206S7281999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Songs,Units 2 & 3 ML20206G6561999-04-27027 April 1999 SER Accepting Proposed Exemption from 10CFR50.71(e)(4) for SONGS Units 2 & 3 ML20206D1461999-04-26026 April 1999 Safety Evaluation Supporting Amend 152 to License NPF-10 ML20205Q6221999-04-19019 April 1999 Safety Evaluation Authorizing Proposed Alternative to Use Wire Penetrameters for ISI Radiography in Place of ASME Code Requirement ML20205R0371999-04-16016 April 1999 SER Approving Proposed Deviation from Approved Fire Protection Program Incorporating Technical Requirements of 10CFR50,App R,Section III.0 That Applies to RCP Oil Fill Piping ML20205N2691999-04-0909 April 1999 Safety Evaluation Supporting Amends 151 & 143 to Licenses NPF-10 & NPF-15,respectively ML20205G2611999-04-0101 April 1999 Special Rept:On 990328,3RT-7865 Was Removed from Service. Monitor Is Scheduled to Be Returned to Service Prior to Mode 4 Entry (Early May 1999) Which Will Exceed 72 H Allowed by LCS 3.3.102.Alternate Method of Monitoring Will Be Used ML20205Q0981999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Songs,Units 2 & 3 05000362/LER-1999-001-01, :on 990211,TS 3.0.3 Entered Due to Both Chilled Water Trains Being Inoperable.Warm Main Condenser Discharged Water Diverted in Salt Water Cooling (Swc)(Bs) Intake.With1999-03-12012 March 1999
- on 990211,TS 3.0.3 Entered Due to Both Chilled Water Trains Being Inoperable.Warm Main Condenser Discharged Water Diverted in Salt Water Cooling (Swc)(Bs) Intake.With
05000361/LER-1999-002, :on 990208,pressurizer Safety Valves Were Above TS Limit.Caused by Setpoint Drift.Sce Submitted License Amend Application on 980904 Requesting Tolerence Be Changed to +3/-2%.With1999-03-10010 March 1999
- on 990208,pressurizer Safety Valves Were Above TS Limit.Caused by Setpoint Drift.Sce Submitted License Amend Application on 980904 Requesting Tolerence Be Changed to +3/-2%.With
05000361/LER-1999-001, :on 990201,automatic Start of EDG Was Noted. Caused by Workers Closing Breaker 2A0418 by Discharging Closing Springs.Operators Restored SDC in Approx 26 Minutes. with1999-03-0303 March 1999
- on 990201,automatic Start of EDG Was Noted. Caused by Workers Closing Breaker 2A0418 by Discharging Closing Springs.Operators Restored SDC in Approx 26 Minutes. with
ML20204F8101999-02-28028 February 1999 Monthly Operating Repts for Songs,Units 2 & 3.With ML20203J1981999-02-12012 February 1999 Safety Evaluation Supporting Amends 149 & 141 to Licenses NPF-10 & NPF-15,respectively ML20203J1131999-02-12012 February 1999 Safety Evaluation Supporting Amends 150 & 142 to Licenses NPF-10 & NPF-15,respectively ML20202F7041999-01-21021 January 1999 Special Rept:On 990106,SCE Began to Modify 2RT-7865.2RT-7865 to Allow Monitor to Provide Input to New Radiation Monitoring Data Acquisition Sys.Monitor Found to Exceeds 72 H Allowed Bt LCS 3.3.102.Alternate Monitoring Established 05000206/LER-1998-006-01, :on 981207,unattended Security Weapon Was Noted Inside Pa.Cause of Event Is Under Investigation.Officer Was Relieved of All Duties,Removed PA Access & Was Placed on Investigatory Suspension1999-01-0606 January 1999
- on 981207,unattended Security Weapon Was Noted Inside Pa.Cause of Event Is Under Investigation.Officer Was Relieved of All Duties,Removed PA Access & Was Placed on Investigatory Suspension
ML20199F0771998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Songs,Units 2 & 3 ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML13309A4481998-12-31031 December 1998 Riverside Public Utilities 1997-1998 Annual Rept ML13309A4421998-12-31031 December 1998 SCE 1998 Annual Rept 1999-09-09
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- U.S. NUCLS Agt ESSUL ATO30Y CSMM13Cl3N APPMSVED OY SM2
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EVENT DESCRIPTION AND PROBABLE CONSEGUENCES bl0 o2 l On July 10. 1983, with Unit 2 and UrTit 3 in Modes 1 and 4, respectively, it was l lo l3 ll determined that routine 6-month surveillance conducted in February 1983 had not l 1014 ll demonstrated the operability of Fire Panel 3L-198 and compensatory measures l j o Is l l prescribed by LC0 3.3.3.7, Action Statement 'a' were not implemented. It was l lo le ll also determined that operability of Fire Panel 3L-198 was demonstrated on l J o l 7 l l July 5,1983. Public health and safety were not affected. l IoIell l
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ATTACHMENT 'IO LER 83-067 i SO(JIllERN CALIPNNIA EDISON COMPANY i SAN ONOFRE NUCLEAR GENERATING STATION UNIT NO. 2, DOCKET NO. 50-361 SUPPLEME?TTAL INFORMATION POR CAUSE DESCRIPTION AND CORRECTIVE ACTIWS Inoperability of this instrumentation defeated the supervisory r apability of the panel (i.e., annunciating circuit interruption or shorting) and, therefore, rendered the panel inoperable but would not have prevented the panel from annunciating fire / smoke detection in the fire zones required by the Technical Specifications. Inoperability of this instrumentation did prevent the satisfactory conpletion of the routine six month surveillance. Fire Panel 3L-198 had been demonstrated operable in July 1982 and was demonstrated operable on July 5, 1983, after repair of the supervisory capability of the panel. .
Conpensatory fire watches were in effect from July 15, 1983, until August 1, 1983, when a review of additional records established that Fire Panel 3L-198 had been determined operable by surveillance testing subsequent to February 1983. (As noted above, it was demonstrated operable by surveillance testing on July 5, 1983.)
Our review of this matter has identified other possible instances wherein conpensatory measures required by LCO 3.3.3.7 ancVor associated reporting requirements have not been met. 'Ihose instances that are verified by our review will be report 6d by separate LER(s).
We conclude that the detail of fire protection surveillance procedures and the training provided personnel in the inplementation of such procedures have, in the past, not been adequate to assure that all fire protection equipaent found inoperable during routine surveillance, have resulted in proper and timely implementation of compensatory measures and 30-day report submittal.
Consequently, our review will include examination of all fire protection surveillance procedures and their inplementation. Corrective measures developed will be identified in a revision to this LER which will be submitted by September 1, 1983.
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p .O. B O K 128 S AN C LEMEN T E. C A LIF OR Nt a 92672 H. B. R A Y k [{ l v e g g pwon g s v a r.o ~ = A ~.. i . August 5,1983 ,,,.,.,,.,,,,
U.S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region V 1450 Maria Lane, suite 210 Walnut Creek, California 94596-5368 Attention: Mr. J. B. Martin, Regional Administrator
Dear Sir:
Subject:
Docket Nos. 50-361 and 50-362 14-Day Follow-Up Report Licensee Event Report No.83-067 San Onofre Nuclear Generating Station, Units 2 and 3
Reference:
Letter, H. B. Ray (SCE) to J. B. Martin (NRC),
dated July 19, 1983, same subject W e referenced letter provided you with confirmation of our prompt notification, pursuant to Section 6.9.1.12.b of Appendix A, Technical Specifications to Facility Operating Licenses 12F-10 and IGF-15 for San Onofre Units 2 and 3, respectively, for an occurrence involving deficiencies in the implementation of the fire protection surveillance program. This submittal provides the 14-day follow-up report and copy of Licensee Event Report (LER) No.83-067. Since this occurrence involves a shared system between Units 2 and 3, a single LER for Unit 2 (Docket No. 50-361) is enclosed in accordance with ITJREG 0161.
Although the referenced letter indicated a follow-up report would be provided by August 2,1983, additional time was required to provide a conplete response.
If you have any further questions, please so advise.
Sincerely,
1 l
Enclosure:
LER No.83-067 (Unit 2)
- XE. " 21
August 5,1983 Mr. J. B. Martin cc: A.E. 01affee (US!EC Resident Inspector, Units 2 and 3)
J.P. Stewart (UStaC Resident Inspector, Units 2 and 3)
U.S. Nuclear Regulatory Comission Office of Inspection and Enforceraent U.S. Nuclear Regulatory Comission Division of Technical Information and Document Control Institute of Nuclear Power Operations (I!PO) 1 5
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