IR 05000247/2009002
Download: ML091320023
Text
May 11, 2009
Mr. Joseph Site Vice President Entergy Nuclear Operations, Inc.
Indian Point Energy Center 450 Broadway, GSB Buchanan, NY 10511-0249
SUBJECT: INDIAN POINT NUCLEAR GENERATING UNIT No. 3 - NRC INTEGRATED INSPECTION REPORT 05000286/2009002
Dear Mr. Pollock:
On March 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit No. 3. The enclosed integrated inspection report documents the inspection results, which were discussed on April 15, 2009, with you and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. This report documents one finding of very low safety significance (Green), which was also determined to be a violation of NRC requirements. However, because of the very low safety significance, and because the finding was entered into your corrective action program, the NRC is treating the finding as a non-cited violation (NCV), consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest this NCV, you should provide a written response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Indian Point Nuclear Generating Unit 3. In addition, if you disagree with the characterization of this finding, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspectors at Indian Point Nuclear Generating Unit 3. The information you provide will be considered in accordance with Inspection Manual Chapter 0305. In accordance with Title 10 of the Code of Federal Regulations (10 CFR) Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room of the Publicly Available Records System (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA/ Mel Gray, Chief Projects Branch 2 Division of Reactor Projects Docket No. 50-286 License No. DPR-64
Enclosure:
Inspection Report No. 05000286/2009002 w/
Attachment:
Supplemental Information cc w/encl: Senior Vice President, Entergy Nuclear Operations Vice President, Operations, Entergy Nuclear Operations Vice President, Oversight, Entergy Nuclear Operations Senior Manager, Nuclear Safety and Licensing, Entergy Nuclear Operations Senior Vice President and COO, Entergy Nuclear Operations Assistant General Counsel, Entergy Nuclear Operations Manager, Licensing, Entergy Nuclear Operations P. Tonko, President and CEO, New York State Energy Research and Development Authority C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law A. Donahue, Mayor, Village of Buchanan J. G. Testa, Mayor, City of Peekskill R. Albanese, Four County Coordinator S. Lousteau, Treasury Department, Entergy Services, Inc. Chairman, Standing Committee on Energy, NYS Assembly Chairman, Standing Committee on Environmental Conservation, NYS Assembly Chairman, Committee on Corporations, Authorities, and Commissions M. Slobodien, Director, Emergency Planning P. Eddy, NYS Department of Public Service Assemblywoman Sandra Galef, NYS Assembly T. Seckerson, County Clerk, Westchester County Board of Legislators A. Spano, Westchester County Executive R. Bondi, Putnam County Executive C. Vanderhoef, Rockland County Executive E. A. Diana, Orange County Executive T. Judson, Central NY Citizens Awareness Network M. Elie, Citizens Awareness Network D. Lochbaum, Nuclear Safety Engineer, Union of Concerned Scientists Public Citizen's Critical Mass Energy Project M. Mariotte, Nuclear Information & Resources Service
SUMMARY OF FINDINGS
......................................................................................................... 3
REPORT DETAILS
REACTOR SAFETY
.............................................................................................................. 5 1R01 Adverse Weather Protection ................................................................................... 5 1R04 Equipment Alignment ............................................................................................. 5 1R05 Fire Protection ........................................................................................................ 6 1R06 Flood Protection Measures ..................................................................................... 6 1R07 Heat Sink Performance ) ......................................................................................... 7 1R08 In-service Inspection ............................................................................................. 7 1R11 Licensed Operator Requalification Program .......................................................... 9 1R12 Maintenance Effectiveness .................................................................................... 9 1R13 Maintenance Risk Assessments/Emergent Work Control .................................... 10 1R15 Operability Evaluations ........................................................................................ 10 1R18 Plant Modifications .............................................................................................. 11 1R19 Post-Maintenance Testing ................................................................................... 11 1R20 Refueling and Outage Activities ........................................................................... 12 1R22 Surveillance Testing
RADIATION SAFETY
......................................................................................................... 13 2OS1 Access Control to Radiologically Significant Areas .............................................. 13 2OS2 ALARA Planning and Controls
OTHER ACTIVITIES
.......................................................................................................... 19
4OA1 Performance Indicator Verification ......................................................................... 19 4OA2 Identification and Resolution of Problems .............................................................. 19 4OA3 Event Followup ...................................................................................................... 20 4OA5 Other Activities ...................................................................................................... 21 4OA6 Meetings, including Exit ......................................................................................... 23
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
.............................................................................................. A-1
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED .................................................... A-2
LIST OF DOCUMENTS REVIEWED
................................................................................... A-2
LIST OF ACRONYMS
......................................................................................................... A-8
Enclosure
- OF [[]]
- FINDIN [[]]
GS IR 05000286/2009-002; 01/01/2009 - 03/31/2009; Indian Point Nuclear Generating Unit 3; Radiological Access Control. This report covered a three-month period of inspection by resident and region-based inspectors.
One finding of very low significance (Green) was identified, which was also determined to be a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process." The cross-cutting aspect for each finding was determined using IMC 0305, "Operating Reactor Assessment Program." Findings for which the significance determination
process (SDP) does not apply may be Green, or be assigned a severity level after
NRC-Identified and Self-Revealing Findings Cornerstone: Occupational Radiation Safety * Green. The inspectors identified a Green non-cited violation of Technical Specification 5.4.1.a, "Procedures," because Entergy personnel did not generate condition reports or investigation paperwork for multiple high dose-rate alarms as required by station procedures. Specifically, personnel did not generate the required condition reports and adequately document the investigations for 21 instances of
unplanned or un-briefed electronic dosimeter alarms that occurred between January 2009 and March 2009. The performance deficiency resulted in workers receiving unanticipated dose rate alarms with no formally-documented investigation prior to returning to work in a Radiologically Controlled Area. Entergy entered the finding into the corrective action program as condition report
IP3-2009-01253 and
01318. The finding is more than minor because it is associated with the Occupational Radiation Safety cornerstone attribute of programs and process, and adversely affected the objective to ensure adequate protection of worker health and safety from
exposure to radiation. Moreover, the inspectors identified a programmatic deficiency to maintain and implement programs to keep exposures as low as reasonably achievable, because multiple examples were identified regarding the failure to satisfy station radiation protection procedures. Using the Occupational Radiation Safety Significance Determination Process, the inspectors determined that the finding was
of very low safety significance (Green) because it did not involve: (1) as low as is reasonably achievable planning and controls, (2) an overexposure of an individual, (3) a substantial potential for overexposure, or (4) an impaired ability to assess dose. The inspectors determined that the finding had a cross-cutting aspect related to procedural adherence in the Work Practices component of the Human Performance area. Specifically, Entergy employees did not follow procedures to generate
condition reports and document investigations when high dose-rate alarms were received by workers.
OS1)
Enclosure B. Licensee-Identified Violations None.
Enclosure
- REPORT [[]]
DETAILS Summary of Plant Status Indian Point Nuclear Generating (Indian Point) Unit 3 began the inspection period at full reactor power. On March 10, 2009, a planned downpower was initiated that culminated in the Unit
being taken off-line to begin refueling outage No. 15 (3R15). The Unit remained off-line to refuel for the remainder of the inspection period.
1.
SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01 - 2 samples) .1 Impending Cold Weather Review a. Inspection Scope The inspectors performed a detailed review of Entergy's procedures to address impending cold weather conditions due to a forecasted arctic front on January 15, 2009. The inspectors evaluated Entergy's preparation and readiness for cold weather conditions, evaluated applicable compensatory measures, conducted walk downs of
plant equipment, and verified that cold weather deficiencies from previous years have been addressed. In addition, the inspectors reviewed the status of deficiencies identified during the current seasonal preparations, and verified that adverse conditions were being adequately addressed to ensure the impending cold weather conditions would not have significant impact on plant operation and safety. The documents reviewed during
this inspection are listed in the Attachment. This review of cold weather preparations represented one inspection sample. b. Findings No findings of significance were identified. 1R04 Equipment Alignment (71111.04Q - 3 samples) a. Inspection Scope The inspectors performed partial system walkdowns to verify the operability of redundant or diverse trains and components during periods of system train unavailability, and where applicable, following return to service after maintenance. The inspectors reviewed system procedures, the Updated Final Safety Analysis Report (UFSAR), and system drawings to verify that the alignment of the applicable system or component supported its required safety functions. The inspectors also reviewed applicable
condition reports or work orders to ensure that Entergy personnel had identified and properly addressed equipment deficiencies that could potentially impair the capability of the available train. The documents reviewed during this inspection are listed in the Attachment.
Enclosure The inspectors performed partial walkdowns of the following systems or components, which represented three inspection samples: * Auxiliary feedwater system following return to service of the 31 auxiliary boiler feedwater pump on February 20, 2009; * 31 and 33 emergency diesel generators (EDG) while the
- 32 EDG was out-of-service for 8-year and 16-year planned maintenance activities; and * 31 and 33 safety injection (
SI) pumps during planned maintenance on the 32 SI pump on February 6, 2009. b. Findings No findings of significance were identified. 1R05 Fire Protection (71111.05Q - 6 samples) a. Inspection Scope The inspectors conducted tours of various fire areas to assess the material condition and operational status of applicable fire protection features. The inspectors verified, consistent with the applicable administrative procedures, that: combustible material and ignition sources were adequately controlled; passive fire barriers, manual fire-fighting equipment, and suppression and detection equipment were appropriately maintained; and compensatory measures for out-of-service, degraded, or inoperable fire protection
equipment were implemented in accordance with Entergy's fire protection program. The inspectors also evaluated the fire protection program against the requirements of License Condition 2.K. Additionally, the inspectors reviewed the circumstances surrounding a fire main component leak located at the header isolation valve associated with the Outage Support Building (Fire Zones 391 and 392). The documents reviewed
during this inspection are listed in the Attachment. This inspection represented six inspection samples and was conducted in the areas covered by the following Pre-Fire Plans: * Pre-Fire Plan Nos. 391 and 392; * Pre-Fire Plan 306; * Pre-Fire Plan 306A; * Pre-Fire Plan 362; * Pre-Fire Plan 362A; and * Pre-Fire Plan
- 362B. b. Findings No findings of significance were identified. 1R06 Flood Protection Measures (71111.06 - 1 sample) a. Inspection Scope The inspectors reviewed the Unit 3 Individual Plant Examination, the
RPT-06-00071, "Indian Point Unit 3 Probabilistic Safety Assessment (PSA)," Rev. 2,
Enclosure concerning internal flooding events. The inspectors assessed flood mitigation attributes within the turbine building that are utilized to minimize potential impacts of flooding on the vital 480 Volt switchgear room that adjoins the turbine building. The inspectors also reviewed a surveillance test conducted on February 3, 2009, associated with flood level indicators in the turbine building, 3-PT-R22, "Turbine Building (Lower Level) Level Sensors," Rev. 10. This inspection represented one sample for internal flood protection
measures. b. Findings No findings of significance were identified. 1R07 Heat Sink Performance (71111.07 - 1 sample) a. Inspection Scope The inspectors evaluated maintenance activities and reviewed inspection data associated with periodic inspections of service water system piping. The inspectors
reviewed applicable design basis information and commitments associated with Entergy's Generic Letter 89-13 program to validate that maintenance activities were adequate to ensure the system could perform its required safety function. The inspectors reviewed radiographic results for selected piping segments to ensure pipe corrosion and conditions adverse to quality were being identified and corrected. This
inspection represented one sample for heat sink performance. b. Findings No findings of significance were identified. 1R08 In-service Inspection (71111.08 - 1 sample) a. Inspection Scope Activities inspected during the Unit 3 refuel outage 15 (3R15) included observations of ultrasonic testing (UT) calibration or in-progress component testing using manual and computer based
- UT observations included the main steam 6" diameter, loop 32, pipe welds 22 and 23 shown on drawing 2201, Rev 6, and review of the
RHR) pipe welds W13 and W16. The
sample of visual inspection (VT) included the areas of the containment inner boundary at the containment liner and containment penetrations. The task work orders and test data for several ultrasonic and visually identified indications were reviewed and confirmed to be evaluated by Entergy personnel as part of the in-service inspection process. The inspectors observed the video-visual examination results for a sample of the reactor pressure vessel (RPV) upper head-to-control rod drive mechanism (CRDM) penetrations
per the
- EPRI guidelines. This inspection included the sequence of Entergy's evaluation of the as-found conditions, conducted in accordance with procedure 3-
- CRDM for boric acid leakage. This inspection also included a comparison of the 2009 visual observations with those of the previous (2007) outage which included
CRDMs 17,
24, 41, 53, 60, and 76.
Enclosure The inspectors reviewed a sample of computer-based, eddy current (ET) and ultrasonic testing (UT) records and results of the upper
CRDM penetrations and weld examinations as conducted from the underside of the RPV head. In the area of boric acid corrosion control activities, the inspectors confirmed the extent of boric acid walkdowns during plant operation and the plant shutdown process, and
verified that identified problem areas were documented in condition reports for evaluation and resolution. In particular, the inspectors reviewed visual records of the as-found and as-left conditions of a reactor vessel head mechanical penetration, Conoseal #3, which had experienced some leakage and was identified by Entergy personnel at shutdown. The inspectors confirmed the Conoseal leakage to be from a mechanical
joint and not pressure boundary leakage that was repaired during this refueling outage. Additionally, the inspectors evaluated the as-left condition on the
- RPV head in that area and other potentially affected areas. The condition of the upper threads on vessel stud #29 and the status of eight other studs were visually inspected to confirm that no significant degradation was present. The inspectors noted that steam generator (
SG) tube inspection results from the 2007
(3R14) outage provided the basis for not performing eddy current testing (ECT) of
RPT-07-00031) of the acceptability of SG operation for two cycles until 3R17. It was noted that the operating conditions between 3R15 and 3R16 would be assessed to confirm that
those conditions were consistent with the
ECT and UT records and examination results of the four hot leg and four cold leg primary piping-to-reactor vessel nozzles consistent
with the dissimilar metal weld program under
UT records and examination results of the bottom-mounted RPV penetrations
that were accessed from inside the RPV. The inspectors reviewed the video record of the visual examinations of the three 6" safety and one 4" pressure relief pressurizer upper cast head inner radius to nozzle surfaces to verify the adequacy of the examination technique and to confirm the status of
the inner radius and related areas. The accessible areas around the 4" spray nozzle were also viewed although the inner radius of the spray nozzle was not accessible. No items of degradation were observed in any of the visually accessible areas. The inspectors noted that the surge nozzle-to-pipe dissimilar metal, stainless steel weld, located at the bottom of the pressurizer was ultrasonically examined after appropriate
preparation of the exterior surface by grinding flush. The inspectors examined the
grinding mockup, the as-ground condition, the engineering analysis including thickness
calculation, and the UT results.
b. Findings No findings of significance were identified.
Enclosure 1R11 Licensed Operator Requalification Program (71111.11Q - 1 sample) Quarterly Resident Inspector Evaluation a. Inspection Scope The inspectors observed licensed operator requalification training conducted on February 25, 2009, in the Unit 3 plant-reference simulator. The inspectors assessed the scope and breadth of the training, which focused on specific activities that were planned for the Unit 3 refueling outage. In particular, the inspectors observed simulated activities associated with the normal cooldown process that occurs following entry into the outage
as the plant transitions into lower modes of operation as defined by technical specifications. The inspection also included the following: (1) discussions with Entergy staff regarding deficiencies in operator performance and/or training being addressed in the current requalification training cycle; and (2) assessment of the implementation of abnormal operating procedures utilized by Unit 3 control room operators to respond to, and mitigate the effects of, simulated loss of residual heat removal cooling.
The inspectors reviewed simulator fidelity to verify correlation with the actual plant control room, and to verify that differences in fidelity that could potentially impact training effectiveness were either identified or appropriately dispositioned. Licensed operator training was evaluated for conformance with the requirements of 10 CFR 55, "Operator Licenses." Documents reviewed during this inspection are listed in the Attachment. This
review represented one inspection sample for licensed operator requalification training. b. Findings No findings of significance were identified. 1R12 Maintenance Effectiveness (71111.12Q - 3 samples) a. Inspection Scope The inspectors reviewed performance-based problems that involved selected structures, systems, and components (SSCs), to assess the effectiveness of maintenance activities and to verify activities were conducted in accordance with site procedures and
- 10 CFR [[50.65 (The Maintenance Rule). The reviews focused on: * Evaluation of Maintenance Rule scoping and performance criteria; * Verification that reliability issues were appropriately characterized; * Verification of proper system and/or component unavailability; * Verification that Maintenance Rule (a)(1) and (a)(2) classifications were appropriate; * Verification that system performance parameters were appropriately trended; and * For]]
SSCs classified as Maintenance Rule (a)(1), that goals and associated corrective actions were adequate and appropriate for the circumstances. The inspectors also reviewed system health reports, maintenance backlogs, and Maintenance Rule basis documents. The documents reviewed during this inspection are listed in the Attachment. The following Unit 3 systems and/or components were
reviewed and represented three inspection samples:
Enclosure * Intake structure; * Emergency diesel generators; and *
- RWST [[level indication system. b. Findings No findings of significance were identified. 1R13 Maintenance Risk Assessments/Emergent Work Control (71111.13 - 5 samples) a. Inspection Scope The inspectors reviewed maintenance activities to verify that the appropriate on-line and shutdown risk assessments were performed prior to removing equipment for work as required by 10]]
CFR 50.65 (a)(4). When planned work scope or schedules were altered to address emergent or unplanned conditions, the inspectors verified that the plant risk
was promptly reassessed and managed. Additionally, the inspectors utilized
- IMC [[0609, Appendix G, during various refueling outage periods, to assist in the evaluation of Entergy's shutdown risk assessments. The documents reviewed during this inspection are listed in the Attachment. The following activities represented five inspection samples: * Planned risk during containment fan cooler and N42 power range nuclear instrumentation activities on January 26, 2009; * Planned risk during troubleshooting activities associated with 480-Volt safety bus 6A conducted on February 5, 2009; * Planned risk during quarterly calibrations of power range nuclear instrumentation channels N41 and N42 on February 17, 2009; * Initial]]
RCS drain down for reactor vessel head removal on March 13, 2009; and * Defense-in-depth contingency 3A during 138kV electrical system outage on March 20, 2009. b. Findings No findings of significance were identified.
1R15 Operability Evaluations (71111.15 - 5 samples) a. Inspection Scope The inspectors reviewed operability evaluations to assess the acceptability of the evaluations, the use and control of compensatory measures when applicable, and compliance with Technical Specifications. These reviews included verification that
operability determinations were performed in accordance with procedure
- OP -104, "Operability Determinations." The inspectors assessed the technical adequacy of the evaluations to ensure consistency with the
- UFSAR and associated design and licensing basis documents. The documents reviewed are listed in the Attachment. The following operability evaluations were reviewed and represented four inspection samples: *
CR-IP3-2009-00052: Noise from 32 service water pump bearing;
Enclosure *
IP3-2008-01589: 33 emergency diesel generator past operability evaluation (3R/4R cylinder lockout event from June/July 2008). b. Findings No findings of significance were identified. 1R18 Plant Modifications (71111.18 - 1 sample) Temporary Emergency Diesel Generator (EDG) Cooling Water Modification
a. Inspection Scope The inspectors reviewed design change documentation that supported Entergy's installation of temporary end bells on the 31 and 33 EDG jacket water heat exchangers. This modification diverted service water to a local storm drain to support maintenance
activities on the Service Water System. The inspectors verified that the design bases, licensing bases, and performance capability of the system was not degraded by the temporary modification. The inspectors verified that Entergy utilized established procedures governing the use of temporary end bells while they were in service. In addition, the inspectors interviewed plant staff, and reviewed issues that had been
entered into the corrective action program to determine whether Entergy had been effective in identifying and resolving problems associated with temporary modifications. The documents reviewed are listed in the Attachment. b. Findings No findings of significance were identified. 1R19 Post-Maintenance Testing (71111.19 - 7 samples) a. Inspection Scope
The inspectors reviewed post-maintenance test procedures and associated testing activities for selected risk-significant mitigating systems, and assessed whether the effect of maintenance on plant systems was adequately addressed by control room and plant personnel. The inspectors verified that: test acceptance criteria were clear; tests demonstrated operational readiness and were consistent with design basis
documentation; test instrumentation had current calibrations and appropriate range and accuracy for the application; tests were performed as written; and applicable test prerequisites were satisfied. Upon completion of the tests, the inspectors verified that equipment was returned to the proper alignment necessary to perform its safety function. Post-maintenance testing was evaluated against the requirements of 10 CFR 50,
Appendix B, Criterion XI, "Test Control." The following post-maintenance activities were reviewed and represented seven inspection samples: * 33 containment fan cooler air flow switch replacement on January 8, 2009;
Enclosure * Fuel storage building ventilation following charcoal and filter replacement on January 26, 2009; * 31 residual heat removal pump load sequence calibration on February 12, 2009; * Valve diagnostic test and calibration of
- PM [[s on March 16, 2009; and * 31 auxiliary boiler feedwater pump cutback controller repair. b. Findings No findings of significance were identified. 1R20 Refueling and Outage Activities (71111.20 - 1 partial sample) Refueling Outage No. 15 (3R15) a. Inspection Scope The inspectors observed and/or evaluated the selected outage activities listed below to verify that (1) shutdown risk was considered during schedule preparation and implementation, and high risk significant evolutions such as mid-loop or reduced inventory conditions; (2) defense-in-depth (]]
DID) measures were utilized to mitigate impacts on key safety functions (e.g., reactivity control, electrical power availability,
containment integrity, etc.) due to plant configuration control changes and ensure compliance with technical specifications and the operating license throughout the outage period; and (3) risk significant activities were conducted in accordance with procedures and evaluated in a manner appropriate for the circumstances. * Fuel receipt and inspection activities; Special nuclear material (SNM) accountability and transfer; * Plant shutdown, cooldown (in accordance with
- TS limits) entry into residual heat removal operation; and refueling operations (e.g., reactor vessel head lift, core offload, etc); * Changes in daily plant risk and implementation of
- DID measures; * Post-shutdown boric acid inspection inside the vapor containment to assess effectiveness of unidentified leakage monitoring and compliance with
- TS [[; * Evaluated multiple reactor and refueling cavity draindown evolutions to verify procedural compliance, and operability and functionality of the redundant and diverse reactor coolant system level instrumentation; * A sample of lockout/tagouts and clearances, were reviewed to verify appropriate controls of plant configuration changes were being implemented for the protection of plant equipment and personnel; * Open outage constraints (work orders and condition reports) were reviewed to verify appropriate disposition of issues, both technical and /or administratively, to ensure compliance with procedural and/or]]
DID-C4) and contingency implementation, team make-up, briefings, and inspection of staged tools; * Evaluated refueling cavity upender sheave failure and replacement activities; * Evaluated boration flowpath activities to ensure appropriate reactivity controls; and * Observed and/or evaluated several surveillance tests, which included:
Enclosure o 3-PT-R145, "AMSAC System Functional Check," Rev. 14;3 o 3-PC-R62C, "Inadequate Core Cooling Monitor-86 Calibration," Rev. 12; o 3-PC-R45, "Calibration Procedure For The Gamma-Metrics Excore Nuclear Instrumentation System," Rev. 15; o 3-PT-V51, "Overpressure Protection System Channel Operational Test," Rev. 2; and o 3-PT-R003G, "31
AT5A Interlock Test," Rev. 2. b. Findings No findings of significance were identified. 1R22 Surveillance Testing (71111.22 - 6 samples) a. Inspection Scope The inspectors witnessed performance of surveillance tests and/or reviewed test data of selected risk-significant structures, systems, and components, to assess whether test
results satisfied Technical Specification,
- UFS [[]]
AR, Technical Requirements Manual, and Entergy procedure requirements. The inspectors verified that: test acceptance criteria were sufficiently clear; tests demonstrated operational readiness and were consistent with design basis documentation; test instrumentation had accurate calibrations and appropriate range and accuracy for the application; tests were performed as written; and
applicable test prerequisites were satisfied. Following the tests, the inspectors verified that the equipment was capable of performing the required safety functions. The documents reviewed during this inspection are listed in the Attachment. The following surveillance tests were reviewed and represented six inspection samples, which includes
- IST [[surveillances: * 3-PT-Q116C, "33 Safety Injection Pump Functional Test," Rev. 13, conducted on January 28, 2009; * 0-SOP-LEAKRATE-001, "RCS Leakrate Surveillance, Evaluation and Leak Identification," Rev. 1, conducted on March 9, 2009; * Bus 6A portion of 3-PT-R003B, "Safety Injection System Test Breaker Sequencing/ Bus Stripping," Rev. 26, conducted on March 13, 2009; * 3-PT-Q120C, "33]]
IST," Rev. 9, conducted on January 23, 2009; * 3-PT-M62C, "480V Undervoltage/Degraded Grid Protection System Bus 6A Functional," Rev. 7, conducted on February 5, 2009; and * 3-PT-R006A, "Main Steam Safety Valves Setting Test Using Set Pressure Verification Device," Rev. 8, conducted on March 10, 2009. b. Findings No findings of significance were identified.
2.
- RADIAT [[]]
- ION [[]]
OS) 2OS1 Access Control to Radiologically Significant Areas (71121.01 - 16 samples)
Enclosure a. Inspection Scope During March 23 - 27, 2009, the inspectors conducted the following activities to verify that Entergy personnel were properly implementing physical, engineering, and administrative controls for access to high radiation areas, and other radiologically controlled areas, and that workers were adhering to these controls when working in
these areas. Implementation of the access control program was reviewed against the criteria contained in 10 CFR 20 and Entergy's procedures required by the Technical Specifications as criteria for determining compliance. During the inspection, the inspectors interviewed the radiation protection manager, radiation protection supervisors, and radiation workers. This inspection activity represents completion of
sixteen (16) samples relative to this inspection area. The inspectors performed independent radiation dose rate measurements and reviewed the following items: Plant Walk Downs and Radiation Work Permit (RWP) Reviews
(1) Exposure-significant work areas were identified for review within radiation areas, high radiation areas, and airborne areas in the plant. Associated administrative controls and surveys were reviewed for adequacy. This review included: Refuel floor split pin and reactor head inspections, refuel floor lower internals removal and installation, refuel floor and fuel support building fuel transport equipment
repairs requiring an underwater diver, reactor coolant pump (RCP) work including
- RCP #31 impeller replacement, containment valve work including pressurizer safety valves, various containment and auxiliary building activities. (2) With the use of a survey instrument and assistance from a Health Physics Technician, performed a walkdown of these areas to determine whether the appropriate
- RWP s, procedure, and engineering controls were in place, and whether surveys and postings were adequate. (3) The inspectors reviewed
- RWP [[s that provide access to exposure-significant areas of the plant including high radiation areas. Specified electronic personal dosimeter alarm set points were reviewed with respect to current radiological condition applicability, and workers were queried to verify their understanding of plant procedures governing alarm response and knowledge of radiological conditions in their work area. (4) The inspectors noted there were no]]
- RWP [[s for airborne radioactivity areas with the potential for individual worker internal exposures of >50 mrem]]
- CEDE. (5) The inspectors noted there were no internal dose assessments that resulted in actual internal exposures greater than 50 mrem
CEDE. Internal assessments were reviewed to determine adequacy and assurance that they were not in fact
equal to or greater than 50 mrem
- CE [[]]
DE. Problem Identification and Resolution (6) The inspectors reviewed condition reports associated with access controls since the last inspection in this area. Staff members were interviewed and documents
Enclosure reviewed to determine whether follow-up activities were being conducted in an effective and timely manner, commensurate with their safety and risk. (7) For repetitive deficiencies or significant individual deficiencies in problem identification and resolution, the inspectors determined if Entergy's assessment activities were also identifying and addressing these deficiencies. (8) The inspectors noted there were no events associated with performance indicator occurrences that involved dose rates greater than 25 Rem/hour at 30 cm, dose rates greater than 500 Rem/hour at 1 meter, or unintended exposures greater than 100 mrem
SDE or greater than 1.5
Rem LDE). Job-in-Progress Reviews (9) The inspectors observed aspects of various on-going activities to confirm that radiological controls, such as required surveys, area postings, job coverage, and job site preparations were conducted. The inspectors verified that personnel
dosimetry was properly worn and that workers were knowledgeable of work area conditions. The inspectors attended pre-planning meetings for work described earlier in the report. (10) The inspectors reviewed the adequacy of underwater diving activities associated with repairs to the fuel transport system, which included dosimetry requirements, bioassay requirements and controls. High Risk Significant, High Dose Rate High Radiation Areas (HRA) and Very
LHRAs were properly secured and posted during plant tours.
(12) The inspectors discussed with Radiation Protection supervision the adequacy of high dose rate
VHRA controls and procedures and verified that no programmatic or procedural changes have occurred that reduce the effectiveness and level of worker protection.
Radiation Worker Performance (13) During observation of the work activities listed above, the inspectors evaluated radiation worker performance with respect to the specific radiation protection work requirements, and their knowledge of the radiological conditions in applicable work areas.
(14) The inspectors reviewed condition reports related to radiation worker performance to determine if an observable pattern, traceable to a similar cause was evident. Radiation Protection Technician Proficiency
Enclosure (15) During observation of the work activities listed above, the inspectors evaluated radiation protection technician work performance with respect to their knowledge of the radiological conditions, the specific radiation protection work requirements and radiation protection procedures. (16) The inspectors reviewed condition reports related to radiation protection technician proficiency to determine if an observable pattern traceable to a similar cause was evident. b. Findings Introduction: The inspectors identified a Green non-cited violation of Technical Specification 5.4.1.a, "Procedures," because Entergy personnel did not generate condition reports or investigation paperwork for multiple high dose-rate alarms as required by station procedures. Specifically, personnel did not generate the required condition reports and adequately document the investigations for 21 instances of unplanned or un-briefed electronic dosimeter alarms that occurred between January 2009 and March 2009. Description: During the period January 2009 through March 2009, 21 instances of electronic dosimeter dose rate alarms were recorded by the access control system. During this period, Entergy personnel inconsistently utilized an informal process of reviewing the alarms without a full investigation or approval process. Moreover, in three
of the 21 instances, the inspectors identified that no investigation or follow-up had occurred. In some cases, the occurrences were over two months old, which the inspectors noted would have made resultant investigations more challenging to perform. In other cases, the alarms were not identified until the worker attempted to re-enter the radiologically controlled area (RCA) and the access control system required manual
override to "un-lock" the occurrence to allow entry into the
- EN [[-RP-203, "Dose Assessment," specifies that for a dose-rate alarm that is unanticipated or un-briefed, several actions are required, one of which is to initiate a condition report, another is to document the investigation using an attachment in the procedure. Contrary to]]
RP-203, for these
instances, no condition reports or attachments were generated with a detailed investigation prior to the workers re-entering the radiologically controlled area. The highest exposure received by these workers during their entry, as indicated by their electronic dosimeter and logged by the access control system, was 33 mRem, while most dosimeters indicated less than 1 mRem for the entry.
Analysis: The inspectors determined that the failure to generate a condition report, as well as the failure to adequately investigate 21 unplanned or un-briefed electronic dosimeter alarms prior to re-entry into the
- RCA [[, as required by station procedure was a performance deficiency. This performance deficiency was within Entergy personnel's ability to foresee and correct, and should have been prevented. This issue was not subject to traditional enforcement, in that it did not have actual safety consequence, it was not an issue that had the potential to impact]]
NRC's ability to perform its regulatory function, and there were no willful aspects. The finding is more than minor because it is associated with the Occupational Radiation Safety cornerstone attribute of programs and process, and adversely affected its
objective to ensure adequate protection of worker health and safety from exposure to radiation. Moreover, the inspectors identified a programmatic deficiency to maintain and
Enclosure implement programs to keep exposures as low as reasonably achievable, because multiple examples were identified regarding the failure to satisfy station radiation protection procedures. Specifically, in 21 cases, Entergy did not fully evaluate dose rate alarms received by workers in radiologically controlled areas of the plant. Using the Occupational Radiation Safety Significance Determination Process, the inspectors determined that the finding was of very low safety significance (Green) because it did not
involve: (1) as low as is reasonably achievable planning and controls, (2) an overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to assess dose. The inspectors determined that the finding had a cross-cutting aspect related to
procedural adherence in the Work Practices component of the Human Performance area. Specifically, Entergy employees did not follow procedures to generate condition reports and document investigations when high-dose rate alarms were received by workers. (H.4 (b)) Enforcement. Technical Specification 5.4.1.a, "Procedures," requires that Entergy establish, implement, and maintain procedures specified in Regulatory Guide (RG) 1.33,
Revision 2, Appendix
EN-RP-203, Revision 2, Section 5.11, requires that a condition report be written for each unplanned or un-briefed electronic dosimeter dose-rate alarm. Contrary to the above, the inspectors identified through a review of electronic dosimeter log information from January 2009 through March 2009, 21
instances of unanticipated or un-briefed electronic dosimeter dose-rate alarms when the procedure was not implemented and condition reports were not generated. Because this finding was of very low safety significance and it was entered into the corrective action program as
- NRC Enforcement Policy. (NCV 05000286/2009002-01, Failure to Follow Radiation Protection Procedures)
- ALARA [[Planning and Controls (71121.02 - 12 samples) a. Inspection Scope During March 23 - 27, 2009, the inspectors conducted the following activities to verify that Entergy personnel were properly maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA). Implementation of the]]
CFR 20, applicable industry
standards, and Entergy's procedures. This inspection activity represents completion of twelve (12) samples relative to this inspection area. Inspection Planning (1) The inspectors reviewed pertinent information regarding cumulative exposure history, current exposure trends, and on-going activities to assess current
performance and outage exposure challenges. The inspectors determined the site's 3-year rolling collective average exposure. (2) The inspectors reviewed Unit 3 outage work-related activities that occurred during the inspection period, the associated
- ALA [[]]
Committee Reviews, exposure estimates, actual exposures and post job reviews. Work reviewed included: refuel floor split pin and reactor head inspections,
Enclosure refuel floor lower internals removal and installation, refuel floor and fuel support building fuel transport equipment repairs requiring an underwater diver, reactor coolant pump (RCP) work, which included
- RCP #31 impeller replacement, containment valve work including pressurizer safety valves, and various containment and primary auxiliary building activities. (3) The inspectors reviewed implementing procedures associated with maintaining occupational exposures
- ALARA. This included a review of the processes used to estimate and track work activity exposures. Radiological Work Planning (4) With respect to the work activities listed above, the inspectors reviewed dose summary reports, related post-job
- ALA [[]]
RA Committee meeting paperwork. This review was also performed to verify that dose was appropriately managed and evaluated by station management.
(5)
- ALA [[]]
RA work activity evaluations, exposure estimates, and exposure mitigating requirements were reviewed for work packages previously mentioned, to verify whether Entergy had established procedures, as well as engineering and work controls, based on sound radiation protection principles. (6) The inspectors compared the results achieved with the intended dose that was established in the planning of the work. The inspectors determined the reasons for inconsistencies between the intended and actual work activity doses and station management awareness and involvement.
(7) The inspectors evaluated for adequacy, the interfaces between operations, radiation protection, maintenance, maintenance planning and others for interface problems or missing program elements. Verification of Dose Estimates and Exposure Tracking Systems (8) Methods for adjusting exposure estimates, or re-planning work, when unexpected changes in scope or emergent work is encountered, were reviewed by the inspectors for adequacy.
Job Site Inspections and
- ALARA [[Controls (9) The inspectors reviewed work activities that present the highest radiological risk to workers. The inspectors evaluated Entergy personnel's use of engineering controls to achieve dose reductions and to verify that procedures and controls are consistent with]]
RWPs were reviewed to determine if appropriate exposure and contamination controls were
being employed. Radiation Worker Performance (10) Through observations and interviews by the inspectors, workers and technicians were found to be knowledgeable of the work area radiological conditions and low dose waiting areas.
Enclosure Declared Pregnant Workers (11) The inspectors reviewed information associated with declared pregnant workers during the assessment period and whether appropriate monitoring and controls were being utilized to ensure compliance with 10CFR20. Problem Identification and Resolution (12) The inspectors reviewed elements of the Entergy's corrective action program related to implementing radiological controls to determine if problems are being
entered into the program for timely resolution. b. Findings No findings of significance were identified. 4.
- OTHER [[]]
ACTIVITIES (OA)
4OA1 Performance Indicator Verification Resident Inspector Baseline Inspection (71151 - 3 samples)
a. Inspection Scope The inspectors reviewed performance indicator data for the cornerstones listed below and used Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, to verify individual performance indicator accuracy and completeness. The documents reviewed during this inspection are listed in the Attachment. Initiating Events Cornerstone * Unplanned Scrams per 7000 Critical Hours; * Unplanned Power Changes per 7000 Critical Hours; and * Unplanned Scrams with Complications. b. Findings No findings of significance were identified.
PI&R) Program Review a. Inspection Scope As required by Inspection Procedure 71152, "Identification and Resolution of Problems," and to identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into Entergy's corrective action program. The review was accomplished by accessing Entergy's
Enclosure computerized database for condition reports, and attending condition report screening meetings. In accordance with the baseline inspection procedures, the inspectors selected corrective action program items across the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for further follow-up and review. The inspectors assessed
Entergy personnel's threshold for problem identification, the adequacy of the cause analysis, extent of condition reviews, operability determinations, and the timeliness of the associated corrective actions. The condition reports reviewed during this inspection are listed in the applicable inspection sections.
b. Findings No findings of significance were identified. .2 Occupational Radiation Safety Cornerstone a. Inspection Scope The inspectors reviewed 23 corrective action condition reports associated with the radiation protection program that were initiated between December 2008 and March 2009. The inspectors verified that problems identified by these condition reports were properly characterized in the licensee's event reporting system, and that applicable
cause and corrective actions were identified commensurate with the safety significance of the radiological occurrences. b. Findings No findings of significance were identified. .3 In-Service Inspection Activities (1R08) a. Inspection Scope The inspectors reviewed the extent of oversight of in-service inspection (ISI) nondestructive examination (NDE) activities, including the topics of current
- ISI [[oversight and surveillances. This review included a sample of issue reports, which are listed in Attachment 1, to confirm that identified problems were being documented for evaluation and proper resolution. b. Findings No findings of significance were identified. 4]]
OA3 Event Follow-up Loss of 480 Volt Emergency Safety Bus 6A During Surveillance Testing on January 2, 2009
Enclosure a. Inspection Scope The inspectors evaluated the response of control room personnel following the unexpected loss of 480 Volt safeguards bus 6A that occurred during the performance of a degraded grid/undervoltage relay surveillance test on January 2, 2009. The inspectors reviewed plant computer data, evaluated plant parameter traces, and discussed the
event with plant personnel, to verify that plant equipment responded as expected, and to ensure that operating procedures were appropriately implemented. The inspectors verified that Entergy's short term corrective actions were appropriate in response to the event. This event was entered into Entergy's corrective action program as
- CR [[]]
IP3-2009-00011. b. Findings and Observations No findings of significance were identified. The inspectors noted, however, that corrective actions for the current event were tracked in an on-going root cause evaluation for a similar event that occurred on October 9,
2008. In addition, the inspectors noted a failure analysis was planned for applicable equipment and components, and extensive troubleshooting was planned for the current 3R15 outage period.
- 4OA [[5 Other Activities .1 Continued Groundwater Sampling Effort to Monitor Tritium (Deviation Memorandum Inspection) a. Inspection Scope During the week of March 23-27, 2009, the inspectors met with Entergy representatives to review the results of recent groundwater samples, as well as those taken and analyzed in 2008. The review was conducted against criteria contained in 10]]
CFR20, 10CFR50, and applicable industry standards.
The review of the data included a comparison of Entergy's data with split samples taken by the
MW-66 and MW-67, as well as the LaFarge sample point. In all, 47 samples were analyzed and compared from January 2008 through January 2009. Isotopic analyses were performed and compared at each of the sample
points for: Tritium, Strontium 90, Nickel 63, and gamma emitters such as Cobalt-60 and Cesium-137. Results of the
- ML 090920949. Entergy=s evaluation of recent groundwater results are documented in condition reports:
IP2-2009-01114. b. Findings No findings of significance were identified.
Enclosure The inspectors concluded that overall, there was agreement between Entergy personnel's results and those independently analyzed by the NRC, and that actions taken by Entergy have been appropriate. The inspectors also noted that conservative estimates indicate that the samples represent a very small fraction of the permissible public dose limits and are negligible with respect to natural background radiation levels.
.2 Inspection Results for
TI) 2515/172, provides for confirmation that owners of pressurized-water reactors (PWRs) have implemented the industry guidelines of the Materials Reliability Program (MRP)-139 regarding nondestructive examination and evaluation of certain dissimilar metal (DM) welds in reactor coolant systems containing Alloy 600/82/182. The TI requires documentation of specific questions in an inspection report, and those questions and responses applicable to Indian Point are included below.
In summary, the Indian Point Units 2 and 3 have
RCS welds in only the hot (HL) and cold leg (CL) pipe-to-reactor pressure vessel (RPV) nozzle connections. These were examined from the inside diameter (ID) surface volumetrically by ultrasonic testing (UT), and on the ID surface by eddy current testing
(ECT) at Unit 2 in the 2006 refueling outage, and on Unit 3 from the outside surface visually during the 2007 refueling outage. For Unit 3 during 3R15 in Spring 2009, eight alloy 82/182 welds were examined from the nozzle inner diameter by
- XI examination coverage confirmed. The safe end-to-pipe or cast elbow stainless steel welds were also examined by
- NDE examiners. No significant indications were found on these welds. One very small indication in the weld cladding of
- IP Unit 3 in 2009: Qa1. Have the baseline inspections been performed or are they scheduled to be performed in accordance with
- ECT examinations and performed during the Spring 2009 3R15 refueling outage. Qa2. Is the licensee planning to take any deviations from the
MRP-139 baseline inspection requirements? If so, what deviations are planned and what is the general basis for the
deviation? If inspectors determine that a licensee is planning to deviate from any
MRP-required examination scope.
Enclosure b. For each examination inspected at
- MRP -139 Section 5.1 for unmitigated welds or mechanical stress improved welds and consistent with NRC staff relief request authorization for weld overlaid welds?
DM weld location. Also, the outside surfaces of these welds were visually examined in 2007.
Qb2. Performed by qualified personnel? (Briefly describe the personnel training/qualification process used by the licensee for this activity.)
- UT was performed with a qualified procedure and by qualified individuals. The eddy current examinations were done in accordance with procedure
- ECT individuals as part of the pre-job preparations. Qb3. Performed such that deficiencies were identified, dispositioned, and resolved? A. One minor indication in the weld internal surface clad material was identified on the 34
III data
reviewer. The condition was not surface interfacing and was not an eddy current indication. b. Findings No findings of significance were identified .3 Quarterly Resident Inspector Observations of Security Personnel and Activities a. Inspection Scope During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that these activities were consistent with Entergy security procedures and applicable regulatory requirements. Although these observations did not constitute additional inspection samples, the inspections were
considered an integral part of the normal, resident inspector plant status reviews during implementation of the baseline inspection program. b. Findings No findings of significance were identified.
4OA6 Meetings, including Exit Exit Meeting Summary On April 15, 2009, the inspectors presented the inspection results to Mr. Joe Pollock and
other Energy staff members, who acknowledged the inspection results. While some
Enclosure proprietary items were reviewed and returned during the inspection, no proprietary information is presented in this report.
- ATTACH [[]]
- MENT [[:]]
- SUPPLE [[]]
- MENTAL [[]]
- INFORM [[]]
- SUPPLE [[]]
- MENTAL [[]]
- INFORM [[]]
- ATION [[]]
- KEY [[]]
- POINTS [[]]
- OF [[]]
CONTACT Entergy Personnel
J. Pollock, Site Vice President A. Vitale, General Manager, Plant Operations K. Davison, Assistant General Manager, Plant Operations P. Conroy, Director, Nuclear Safety Assurance D. Gagnon, Manager, Security
R. Walpole, Manager, Licensing B. Beckman, Manager, Maintenance J. Dinelli, Assistant Operations Manager, Unit 3 V. Myers, Supervisor, Mechanical Design Engineering T. Orlando, Engineering Director R. Burroni, Manager Programs, Components and Engineering D. Loope, Manager, Radiation Protection
- S. Verrochi, Manager System Engineering F. Inzirillo, Manager, Quality Assurance N. Azevedo, Supervisor, Code Programs T. Morzello, Maintenance Supervisor G. Dahl, Licensing Engineer
- ALARA Specialist G. Hocking, Supervisor, Radiation Protection Support R. Blaine, Supervisor, Radiation Protection Operations S. Sandike, Specialist, Effluent & Environmental Monitoring
QA B. Allen, Code Programs
Attachment
- LIST [[]]
- OF [[]]
- ITEMS [[]]
- CLOSED [[]]
- AND [[]]
- DISCUS [[]]
SED Open and Closed 05000286/2009002-01 NCV Failure to Follow Radiation Protection
Procedures (Section
- LIST [[]]
- OF [[]]
- REVIEW [[]]
- OAP -008, "Severe Weather Preparations," Rev. 5 3-PT-W011, "TSC Diesel Generator Support System Inspection," Rev. 18 Section 1R04: Equipment Alignment Miscellaneous
Other Flow Diagram 9321-F-27503, "Safety Injection System, Sheet No. 2," Rev. 48 3-COL-FW-2, "Auxiliary Feedwater System," Rev. 29 3-COL-EL-005, "Diesel Generators," Rev. 33 3-COL-SI-001, "Safety Injection System," Rev. 38
Section 1R05: Fire Protection
Procedures
- SMM [[-DC-901, "IPEC Fire Protection Program," Rev. 6 Pre-Fire Plans 391, 392, 306, 306A, 362, 362A, and 362B 3-COL-FP-2, "Fire Protection System Ring Header," Rev. 10 Condition Reports (CR-IP3-2009-) 00499 00504 00511 00556 00584 00600 00604 Section 1R07: Heat Sink Performance]]
- IP [[]]
UT-1, Rev 20, Ultrasonic Examination of Ferritic Piping Welds
Attachment 3-PT-R114, Rev 10.
- 9 ET [[]]
- 2 ET [[]]
- RV [[]]
- 5 UT [[]]
- RV [[]]
- 4 UT [[]]
- RV [[]]
IP U2 Reactor Coolant Pump Shaft Seal 9321-F-27453, Rev 30. Flow Diagram - Sampling System (valve 953) 9321-F-27383, Rev 27. Flow Diagram RC System (valve 514A) 322097-00, Rev 2, Replacement of Removed Liner Insulation (U2)
21-F-1280-15, A200 168, Containment Liner Details (U2) Pressurizer Drawing
- BMI [[]]
- NDE [[Calibration Sample Tube Condition Reports (IP3-2009) 00898 01335 01242 01103 01097 01097 00779 00898 01016 00739 00805 Work Packages]]
- NDE [[]]
- PDI [[]]
- XI [[]]
XI, Sub-Section IWE Section 1R12: Maintenance Effectiveness
Procedures 3-PT-Q83,
ES-1.3, Transfer to Cold Leg Recirculation Condition Reports (CR-IP3-) 2008-01027 2008-01080 2008-01088 2008-01139 2008-01264 2008-01327 2008-01340 2008-01490 2008-01520 2008-01554 2008-01566 2008-01577 2008-01594 2008-01599 2008-01601 2008-01602 2008-01670 2008-01723 2008-01828 2008-01849 2008-01870 2008-01873 2008-01878 2006-01671 2007-01179 2007-03884 2007-04038 2007-04352 2007-04409 2007-03155
2008-00726 2008-01844 2008-02211 2008-02875 2008-03019 2009-00348
Attachment
SED-AD-22, "Condition Monitoring of Maintenance Rule Structures," Rev. 4 Miscellaneous Maintenance Rule Basis Document Residual Heat Removal System, dated 5/23/05 Work Orders 51667042 51802297 51797562 51694152 51688955 51679627 52024026 00176792
Section 1R13: Maintenance Risk Assessment and Emergent Work Control Procedures
- SMM -WM-101, "On-Line Risk Assessment," Rev. 3 Work Week Managers Operator's Risk Report, Work Weeks 0905, 0906 and 0908 3R15 Refueling Outage Schedule Risk Assessment Report, Jan. 2009, Amended Feb.
SMM-OU-104, Attachment 9.1, "Shiftly Outage Shutdown Safety Assessment," Rev. 5
Section 1R15: Operability Evaluations
Procedures
OP-104, "Operability Determinations," Rev. 3
Indian Point Unit 3 Updated Final Safety Analysis Report, Rev. 2
- AL [[]]
CO Genset Operation with Injection Pumps 3R and 4R Locked Out, Rev. 0
Attachment
MA-133, Attachment 9.1, Scaffold approval forms for Scaffolds #212 and 214
Section 1R18: Plant Modifications
Procedures 3-TAP-001-EDG, "Removal and Installation of Service Water Drain Line on Emergency Diesel Generator Jacket Water Heat Exchangers," Rev. 0 3-OSP-EL-001, "Emergency Diesel Generator Operation with Temporary Service Water Return Lines," Rev. 3 Miscellaneous
Section 1R19: Post-Maintenance Testing
Procedures
WM-105, "Planning," Rev. 4 and 5 3-PT-R032A, "Fuel Storage Building Filtration System," Rev. 18 0-GNR-410-ELC, "Emergency Diesel Generator 8-Year Inspection," Rev. 3 3-GNR-026-ELC, "Emergency Diesel Generator 16-Year Inspection," Rev. 4
3-PT-R160B, "32
- VLV -404-AOV, "Use of Air Operated Valve Diagnostics," Rev. 5 3-PT-OL3B15, "Residual Heat Removal Pump #31 Load Sequencer Calibration," Rev. 2 3-PT-Q134, "31
RHR Cooling Not In Service)," Rev. 4 3-PT-Q126, "Fan Cooler Unit Operational Test," Rev. 0
3-PT-R007A, "31 & 33 Auxiliary Boiler Feedwater Pumps Full Flow test," Rev. 16 Condition Reports (CR-IP3-) 2009-00012 2009-00013 2009-00138 2009-01200 2009-01222 2009-00149 2008-03053 2008-03074 2008-03165 2008-03240
Work Orders 00162194 51548354 51558427 00165576 00153367 51483691 51672208 51698102 00177619 00163178
Misc
MS-S-009-IP3, "IP3 System Safety Function Sheets," Rev. 1 Section 1R20: Refueling and Outage Activities Procedures 3-POP-3.3, Plant Cooldown - Hot To Cold Shutdown 3-POP-4.1, Operation at Cold Shutdown 3-SOP-RHR-001, Residual Heat Removal System Operation 3-SOP-NI-003, Setting of the High Flux at Shutdown Alarm 3-SOP-RP-021, Filling the RCS/Refueling Cavity
3-SOP-CVCS-003, Reactor Coolant System Boron Concentration Control
Attachment 3-POP-3.2, Plant Recovery From Trip, Hot Standby Condition Reports (IP3-2009-) 00681 01242 01178 00963 2008-00440 Section 1R22: Surveillance Activities
Procedures 0-SOP-LEAKRATE-001, "RCS Leakrate Surveillance, Evaluation and Leak Identification," Rev. 1 3-PT-Q-116C, 33 Safety Injection Pump Functional Test," Rev. 13
3-PT-R003B, "Safety Injection System Test Breaker Sequencing/Bus Stripping," Rev. 26 Work Orders 51695634 51796922 Condition Reports (CR-IP3-2009) 00111 00321 00463 00711 00715 00716 00773
Section
RP-208, Rev. 02, Whole Body Counting and In-Vitro Bioassay
Condition Reports
- TEDE [[]]
- ALA [[]]
RA Committee Reviews
Attachment
- RWP 's: 2009-002, 2009-003, 2009-2021, 2009-3001, , 2009-3002, 2009-3056, 2009-3501, 2009-3504, 2009-3515, 2009-3529 Section 4
OA1: Performance Indicator Verification
Procedures
- LI -114, Attachment 2, "NRC Performance Indicator Technique Sheet," Rev. 2, for First Quarter 2008 thru Fourth Quarter 2008 for selected Performance Indicators
LI-106, Attachment 9.4, "NRC Submittal Review," Rev. 3 NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Rev. 5
Section 4OA5: Other Activities
EnergySolutions Procedure
- FO -WI-001, Rev. 0, Spent Fuel Pool Cleaning at Indian Point Unit 1 Entergy Procedure 1-RP-RWM-913, Rev. 1, Unit 1 Fuel Handling Building West Pool 24/7 Demineralizer System Entergy Work Order 00123484 10, Modifications to the
- EDG s 31, 32 & 33 Accident Loading Other Documents Indian Point Nuclear Generating Unit No. 3, Updated Final Safety Analysis report, Chapter 8, Rev. 02, 2007
FM/ALCO Indian Point Nuclear Generating Unit No. 3 Technical Specifications, Section 3.8, Electrical Power Systems, through Amendment 226 Indian Point Nuclear Generating Unit No. 3 Technical Specifications Bases, Section 3.8, Electrical Power Systems, Rev. 3
Attachment
- LIST [[]]
- OF [[]]
- ACRONY [[]]
- MS [[]]
- AMSAC [[]]
- SCRAM [[]]
- CE [[]]
- EC [[]]
- EP [[]]
- GL [[]]
- LH [[]]
- PA [[]]
PM Preventive Maintenance PRA Probabilistic Risk Assessments
PWR Pressurized-Water Reactor
Attachment
- TE [[]]