05000247/FIN-2009002-04
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Finding | |
|---|---|
| Title | Inadequate Maintenance Procedure for EDG Ventilation Motor Control Center #2 |
| Description | The inspectors identified a NCV of very low safety significance related to TS5.4.1, Administrative Controls: Procedures, because Entergy did not maintain an adequate maintenance procedure for a safety-related electrical motor control center (MCC). Specifically, the eight-year maintenance procedure for the affected EDG ventilation MCC did not contain an adequate method to identify high resistance connections within the cubicle as was expected in the applicable preventative maintenance industry template. Subsequently, a high resistance connection within the MCC developed into a phase-to-phase electrical fault on January 28, 2009. Entergy entered the issue into the corrective action program, scoped the affected MCC and 21additional MCCs into the sites thermography program, and planned to revise the maintenance procedure. This issue was more than minor because the finding was associated with the external factors attribute of the Initiating Events cornerstone and impacted the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety systems during shutdown as well as power operations. Specifically, the high resistance connection degraded into a phase-to-phase fault and increased the likelihood of a fire in the EDG building. The condition was evaluated by a Senior Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection Significance Determination Process. It was determined that in the event of a fire consuming the MCC, no transient would be placed on the plant and no components required to safely shutdown the plant would be impacted. As a result, in accordance with task 2.3.5 of Appendix F, the issue was screened to Green. The inspectors determined that the finding had a cross-cutting aspect associated with the area of problem identification and resolution related to the use of operating experience (OE). Specifically, Entergy personnel did not implement industry recommended practices, or an alternate equivalent method, for identifying high resistance connections in electrical switchgear. (P.2(b) per IMC 0305 |
| Site: | Indian Point |
|---|---|
| Report | IR 05000247/2009002 Section 1R12 |
| Date counted | Mar 31, 2009 (2009Q1) |
| Type: | NCV: Green |
| cornerstone | Initiating Events |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71111.12 |
| Inspectors (proximate) | C Hott G Malone J Commiskey M Gray |
| CCA | P.5, Operating Experience |
| INPO aspect | CL.1 |
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Finding - Indian Point - IR 05000247/2009002 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Indian Point) @ 2009Q1
Self-Identified List (Indian Point)
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