ML18093A797

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LER 88-005-00:on 880307,identified Tech Spec Surveillance 4.7.8.1.2.a,sealed Source Leak Check Not Performed within 6 Months from Prior Surveillance.Caused by Inadequate Administrative Controls Associated W/Computer Sys
ML18093A797
Person / Time
Site: Salem PSEG icon.png
Issue date: 03/29/1988
From: Pollack M
Public Service Enterprise Group
To:
Shared Package
ML18093A794 List:
References
LER-88-005-01, LER-88-5-1, NUDOCS 8804210047
Download: ML18093A797 (4)


Text

NllC For111 . . U.1. NUCLEAll llEOULATOllY COWlllllON (9-831 APPllOVEO OM9 NO. 31ll0-0104 EXPIRES: 8/3119&

LICENSEE EVENT REPORT (LER) .

l'ACILITY NAME (11 DOCKIT NW9111 IZI I r-~~ 1:111 Salem Generatina Station - Unit 1 TITLE l*J Io 15 Io Io Io I~ 17 b 1 loF nl 4 T. S. Surveillance 4.7.S.l.2 Performed Late Due To Inadequate Administrative Control l!VINT OATI! 1111 LEA N..-Ell Ill REl'OllT OATE (7J OTHEll FACILITIEI INVOLVED Ill MONTH QAY YEAR YEAR mt SE~~~:~~.. L tr :i: MONTH DAY YEAR FACILITY NAME!I DOCKET NUMIEAISI Salem - Unit 2 0 161OI0I013 I 111 ol3 ob s s s ls- olols - olo ol3 219 s ls Ol'lllATINO THll llEl'OAT 11 IU*UTTED l'UlllUANT TO THE llEQUlllEMENTI OF 1.0 CFll §: (Ch<<k ono or man of lit* followln1J (111 MODI Ill ZO*.all(ol 10.a(11111 --- I0.7:1C.ICZIU*I I0.7Slal1Zllwl -- 7U11ltl 71.71(11 Jl llO.*lolCZI

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- l!0.73CalCZllMi l!0.73C.llillHll LICENIEE CONTACT FOii THll LEll (111 I0.71C.ICZllwlllllll I0.71C.llZll*I NAME TELEPHONE NUMllER AREA CODE M. J. Pollack - LER Coordinator 61 O 19 3 I 3 I 9 I- I 4 I O 12 I 2 COMPLETE ONE LINE FOR EACH COlll'ONENT FAILUllE DEICllllED IN THll lll!l'OllT 1131 CAUSE SYSTEM COMPONENT MANUFAC MANUFAC TUR ER TUA ER I I I I I I I I I I I I I I I I I I I I I I I I I I I I IUWLEMl!NTAL AEl'OllT l!Xl'l!CTED 1141 MONTH DAY Y&:AR EXPECTED SUllM18810.N DATE (1111 MYES flf rm. comp- EXl'ECTED SUtlMISSIDN DATEJ I I I A81TllACT (Umlr ID 1"'10 -

  • I.&, _,.,.1mor.1y 11,_, Ii,.._ ry~nen l/flll} (111 On 03/07/88 at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />,.it was identified that Technical Specification Surveillance 4.7.8.1.2.a, sealed source leak checks, was not performed within six months from the prior surve.illance. The surveillance was over~ue as of 03/01/88. The missed surveillance was identified as a result of the investigative corrective actions required by recent LERs which deal with other missed surveillance concerns (e.g., LER 272/88-004-00). *The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work acti_vity system, Managed Maintenance Information System (MMIS). The sealed source leak check surveillance was completed 03/14/88. No leaking sources were found. A manual system for tracking surveillances within the Radiation Protection Department has been implemented. This will continue until the MMIS is updated to handle this surveillance. The Radiation and Chemistry surveillance review committed to by LER 272/88-004-00 is continuing.

The PSE&G NQA evaluation of the administrative control of surveillance recurring tasks has been initiated (reference Salem Unit 2 LER 311/88-004-00).

8804210047 880413 PDR ADOCK 05000272 S DCD NllCFwm . .

(9-83)

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE -

Unit 1 5000272 88-005-00 2 of 4 PLANT AND SYSTEM IDENTIFICATION:

Westinghouse - Pressurized Water R;eactor Energy Industry Identification System (EIIS) codes are identified in the text as {xxl IDENTIFICATION OF OCCURRENCE:

Technical Specification Surveillance 4.7.8.1.2 Performed Late Due To Inadequate Administrative Control Event Date: 03/07/88 Report Date: 03/29/88 This report was initiated by Incident Report No. 88~099.

CONDITIONS PRIOR TO OCCURRENCE:

Mode 1 Reactor Power 100% - Unit Load 1160 MWe DESCRIPTION OF OCCURRENCE:

On March 07, 1988 at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, it was identified that Technical Specification Surveillance 4.7.8.1.2.a, sealed source leak checks, was not performed within six months from the prior surveillance. The surveillance was overdue as of March 01, 1988. The missed surveillance was identified as a result of the investigative corrective actions required by recent LERs which deal with other missed sµrveillance concerns (e.g., LER 272/88-004-00).

Technicai Specification 3.7.8.1 ~tates:

"Each sealed source containing radioactive material either in excess of 100 microcuries of beta and/or gamma emitting material or 5 microcuries of alpha emitting material shall be free of >

0.005 microcuries of removable contamination."

Technical Specification Surveillance 4.7.8.1.2 states:

"Test Frequencies - Each category of sealed sources shall be tested at the frequency described below."

Technical Specification Surveillances 4.7.'8.l.2.a & b state:

"a. Sources in use (excluding startup *source~ and fission detectors previously subjected to.core flux) - At least once per six months for all sealed sources containing radioactive materials. * -

1. With a half life greater than 30 days (excluding Hydrogen 3), and
2. In a*ny form other than gas.

r LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 88-005-00 3 of 4 DESCRIPTION OF OCCURRENCE (cont'd)

b. Stored sources not in use - Each sealed source and fission detector shall be tested prior to use or transfer to another licensee unless tested within the previous six months. Sealed sources and fission detectors transferred without a certificate i.ndicating *the last test date shall be tested prior to being placed int6 use."

APPARENT CAUSE OF OCCURRENCE:

The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work activity system, Managed Maintenance Information System (MMIS).

When the origianl work activity Inspection Order {IO) system data was transferred to the new MMIS in March 1987, the responsibility to ensure that the data was appropriately formatted resulting in tracking/scheduling of surveillances was not clearly defined.

Subsequently, Technical Specification 4 * .7.8.1.2.a was not formatted as required when the MMIS became effective. Additionally, the Radiation Protection Department was internally reorganized in 1987 resulting in changed assigned departmental superisory responsibilities. Sealed source inventory and control resp6nsibility was one of the re-assignments.

ANALYSIS OF OCCURRENCE:

The sealed source leak testing required by Technical Specification Surveillance 4.7.8.2.1.a ensures continued compliance with the limitations as required by Nuclear Regulatory Commission {NRC) Code of Federal Regulations. The limitation ensures leakage from byproduct, source, and special nuclear material sources will not exceed allowable intake values.

Since the Technical Specification Surveillance requirement *to leak test sealed sources every six months was notmet this event is

  • reportable in accordance with the requirements of NRC Code of Federal*

Regulations 10CFR 50.73{a) (2) {i) {B). Subsequent leak.testing of the sealed sources did* not identify any leaking sources, therefore, this event did not affect the health or safety of the public.

CORRECTIVE ACTION:

  • The sealed source leak check surveillance was completed March 14, 1988. No leaking sources were found.

A manual system for tracking surveillances within the Radiation Protection Department has been implemented. This will continue until the MMIS is updated to handle this surveillance.

The Radiation and Chemistry surveillance review committed to by LER 272/88-004-00 *is continuing. This review will resolve and clarify Radiation Protection and c*hemistry schedule requirements as well as

e e LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 88-005-00 4 of 4 CORRECTIVE ACTION: (cont'd) to identify who's responsibility it is to conduct these surveillances.

The PSE&G Nuclear Quality Assurance evaluation of the administrative control of surveillance recurring tasks has been initiated (reference Salem Unit 2 LER 311/88-004-00)

~IJA~~/1fW General Manager -

Salem Operations MJP:pc SORC Mtgo 88-025