05000293/LER-2007-003

From kanterella
Revision as of 01:35, 1 December 2017 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER-2007-003,
Docket
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
2932007003R00 - NRC Website

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

BACKGROUND

The N2K safe-end-to-nozzle weld is located at the inlet to the reactor vessel from the "B" recirculation loop. This section of the piping system supplies drive water for two jet pumps. There are 10 similar N2 safe-end-to-nozzle welds in the reactor coolant pressure boundary.

During RFO 16, a scheduled ultrasonic test (UT) was performed on the N2K safe-end-to-nozzle weld.

A weld discontinuity was recorded.

Construction records were reviewed and repairs in the area of the flaw were noted to have been performed in 1984 during the recirculation pipe replacement project. Lack of detailed documentation prevented determining the amount of grinding that was performed (e.g., depth, length). The limited documentation that is available indicates that grinding for weld repair was required and took place at most 0.75 inches from the outside diameter (OD). However, RFO 16 UT tests revealed indications were present nearer to the inside diameter (ID) of the pipe. The discrepancy between the repair records and UT test results caused elevated concern by the Level Ill inspector.

A third party review was solicited and an evaluation of construction radiographs, 1997 UT data, and 2007 UT data was performed. The detailed evaluation of the N2K flaw determined that the weld discontinuity was a subsurface planar flaw per IWB-3320. A conservative estimate concluded that the flaw was a planar-type circumferential flaw within the Alloy 82/182 weld that was inside surface connected. The review characterized a flaw depth of 1.02 inches with 0.13 inches remaining (89% through-wall flaw).

Based on the weld examinations performed, a weld repair was determined to be necessary.

EVENT DESCRIPTION

On April 26, 2007, at approximately 1930 hours0.0223 days <br />0.536 hours <br />0.00319 weeks <br />7.34365e-4 months <br /> during initial welding activities associated with installation of the full weld overlay, water seepage occurred at the outside diameter of the existing weld in the vicinity of the flaw on the N2K recirculation system inlet nozzle. The seepage confirmed that the weld flaw was inside surface connected. The crack in the weld material was peened and seal welded to stop the seepage.

The weld was subsequently repaired via the installation of a full structural weld overlay. The weld repair methodology was approved by the NRC in relief request PRR-15, Rev. 01.

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

CAUSE

The cause of leakage from the reactor coolant pressure boundary was due to welding preparation activities taken to repair the N2K safe-end-to-nozzle weld.� The cause of the almost through-wall flaw found on the N2K nozzle is a small crevice condition most likely from lack of fusion at the pipe ID, which created a crack initiation site (likely crevice corrosion) in the Inconel 182 butter. The crack propagated outward through the Inconel 182 butter and into the weld. Given the crack is entirely within the Inconel weld, the mechanism for crack propagation is Interdendritic Stress Corrosion Cracking (IDSCC).

IDSCC differs from Intergranular Stress Corrosion Cracking (IGSCC) in that the crack occurs entirely within the weld material whereas IGSCC occurs within the base metal heat affected zone. The IDSCC mechanism propagated the crack due to high residual weld stresses.

CORRECTIVE ACTION

Corrective action taken included an automated, full structural weld overlay. The weld overlay was installed with Inconel 52M weld metal, which is highly resistant to stress corrosion cracking. The weld overlay process also imparts a compressive residual stress due to the welding process, which prevents further crack growth. The weld overlay was installed under an NRC approved relief request.

After the N2K nozzle-to-safe-end weld flaw was identified, additional UT examinations were performed on an expanded scope of four Category D welds. All other Category D welds had already been examined using the EPRI Performance Demonstration Initiative (PDI) requirements during prior outages. Three of the welds in the expanded scope are N2 nozzle-to-safe-end welds. No unacceptable flaws were identified in the four expanded scope UT examinations performed in RFO 16.

An extent of condition evaluation was also performed. The evaluation assessed critical attributes related to the N2K nozzle weld flaw. The evaluation identified that 34 Category D welds at PNPS are in the BWRVIP-75 Program. Of those 34 welds, 17 are welds that contain Inconel. All 17 of the welds with Inconel were UT examined during the last two outages (RFO 15 and RFO 16). However, not all sections of each weld could be UT inspected because of transducer lift off resulting from irregular weld and pipe configurations. Best efforts have been made to contour the surface of the welds to meet EPRI PDI requirements and to maximize weld volume coverage without violating minimum wall requirements.

Ongoing corrective actions for the event includes a review of weld repair records for SSC susceptible Inconel 182 welds to determine if the repaired weld sections were fully covered by the UT examinations.

1 FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

SAFETY CONSEQUENCES

The event posed no threat to public health and safety.

The leakage from the N2K safe-end to-nozzle weld was identified while work was being performed to repair the weld. The weld repair was necessary based on the results of scheduled ultrasonic testing in accordance with the PNPS ISI Program which identified weld discontinuity in the form of a subsurface planar flaw. Only slight water seepage was reported in the area of the welding flaw. The crack was sealed by peening and seal welding before a full structural overlay was installed.

At the time that the leakage was noted, the reactor was shutdown for refueling. All required control rods were in the fully inserted position. The reactor vessel was at atmospheric pressure. The reactor vessel water temperature was less than 212 degrees Fahrenheit. Reactor water level was flooded up for refueling and being maintained at the 116' elevation.

The flaw in the N2K safe-end—to-nozzle weld was not through-wall when it was identified during a scheduled UT examination. The flaw length noted in the N2K weld is 2.87 inches wide; with an inside surface connected crack located 0.13 inches from the outside diameter. Reactor coolant leakage did not occur until weld repairs were initiated.

Since September 1991, PNPS has been operating with Hydrogen Water Chemistry (HWC). HWC arrests stress corrosion cracking initiation sites and slows existing crack growth rates. During RFO 16 the first application of Noble Metal Chemical Addition (NMCA) was completed. NMCA used in combination with Hydrogen Water Chemistry (HWC) is also effective at arresting crack initiation and slowing crack growth rates. In addition, the N2 nozzle design loads result in relatively low primary stress levels and as such fatigue is not considered to be a significant degradation factor. Therefore, if this flaw had remained in­ service slow growth crack rates would be expected during future operating cycles.

The flaw length is a small fraction of the overall pipe circumference and therefore, if the flaw had breached the outside diameter, some leakage would have occurred. This leakage would be detected by installed drywell leak detection systems. Limits on unidentified leakage in the drywell would force reactor shutdown before there is any threat of crack growth that would jeopardize the overall structural integrity of the reactor coolant boundary piping (i.e., guillotine failure).

FACILITY NAME (1)

PILGRIM NUCLEAR POWER STATION

DOCKET NUMBER (2) 05000-293 LER NUMBER (6) I REVISION

REPORTABILITY

This report was submitted in accordance with 10 CFR 50.73(a)(2)(ii)(A), because the N2K weld leak represents a condition of the nuclear power plant, including its principle safety barriers, that was seriously degraded.

SIMILARITY TO PREVIOUS EVENTS

A review was conducted of Pilgrim Station LERs submitted since 2000. The review focused on reactor coolant boundary leakage and welding flaws. The review identified that LER 03-06-00 reported a similar event which involved a nozzle-to-cap weld on the N10 nozzle.

ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for this report are as follows:

COMPONENTS CODES

Nozzle (N2K Nozzle) NZL

SYSTEMS CODES

Reactor Recirculation AD