ML19224D585

From kanterella
Revision as of 06:24, 5 September 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 79-013/03L-0 on 790412:during Test of Snubbers Many Found Inoperable Due to Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Snubbers Repaired & Adjusted
ML19224D585
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 07/03/1979
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19224D582 List:
References
LER-79-013-03L, LER-79-13-3L, NUDOCS 7907120663
Download: ML19224D585 (1)


Text

v c Com.i ;6 s

u. > a v u t e-n n e u u L,. i u n y cu w.w -

(7 77)LICENS,iE i"v TNT REPORT CCNTROL BLOC s l llllll(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) i e oli (_C l 0 l F l S I V l 1 Ql 0 l 0- l0 ,l010 l@l 411 l1 12 l 0 l@l ll@0 10 0 10-7 d 3 LICENSEE COCE 14 15 LICENSE NuvdER 25 26 LICENSE Tv et JO h7 Gr :8 CCN'T 0% lL @ 0l5l0l010l2l6l7 @l0lal1l2l719 @l0l7l0l317l9 @

0I'd 60 61 GCCK ET NLv6ER 68 63 EV ENT D ATE 74 75 RE8 CAT OATE 60 EVENT DESCRIPTION AND PROS A8LE CCNSECUENCES h

[TTTl l .During functional test of hvdraulic shock sucotessors ( snubbe rs).any were f ound to I a,3l be inoperable. The snubbers had not been tested since installation and nust be 1 o 64l assumed to have been inoperable while the reactor was at power contrarv to I.C0 4. 3.10 1 jnubberswere found to be inopenble due to unacceptable lockuo and/or unacceptable lo,s[ bleed characteris tics.

Reportable per Fort S t.

Vrain Technical Specification, Section t 0 is 317l AC 7.5.2(b)2.

Thr.re was o effect on pualic health and safety.

l;a, I l 7 3 3.$J SYSTEM CAUSE CAUSE CVU8 VA LV E COCE COCE S' '8 C0 0 E CC*tPONENT COCE SLSCOCE SL6COCE ( Z i Z I@ 121@ 13163) IS I" Ip 10 IR IT l@ I DI@ I Zi@

a 3 9 10 11 12 12 to 13 20'.SECUk MAL OCOLAAENCE AEPORT"EVIS3ON ,,_EVENr VEAR H E*0HT NO.

000E TYPE NO.@ .*gg a ao i7 19 l[- , lJ l1 l 3 l l/ll 0l 3llLll-ll0 lE,'y ,7_:i:::" 24 26 27:s 29:s ai 22 ACTION ruTuaE EF8ECT S a V T OCV.N ATT AC v5NT N P A O-4#AtVE CCMP COvp0NENT sLeviT to scam wS.SUP8U E A MANLFACTLAEA TAKEN A CT r C N CNPLANT VET Oc-cLpS..lDl@!Zl@l 2 l@lZ @il0 10 ullYl@lN l@l Al@lI l2l0l7l@

2;24 a,.o 3-o*i 42 43 u 47 CAUSE DESCRIPTION AND LCR AECTIVE ACTICNS h l-0l The caus:. of the failure of the snubbers to have acceotable lockuo and bleed charac-llteristics was setpoin: drift, dirty oil, and clogged valves. These snubbers sre IT7- 1

, i Grinnel snubben of various sizes and models.

All snuFbers tested were repaired /re-

], , , ,3l adjus ed p rior to reins tallation.

lla!!.'7 3 3 80-F ACILi*v v VETwCO CF STATa5 N POWE A oT*ER STATUS

>SCOVEA*Of SCOVERv OESCRIPT'CN

-.l H l@ [ 0_

0 l0 l@l N/A ll 3l { urveillance Test Results li 5 3 3 10 12 11 44 45 46 S3'ACTI V t TY CONTENT AELEASED OF AE LE ASE AVOUNT CF ACTIVITY LOCAT:CN OF AELEASE

~lsl Z l @ y@[ N/A l N/Al-3 3 10 11 44 45 60#E ASCNNEL EXPOSL AES NVY8EA TY8E O E SC Al # TIC N s 0 ] O l 0 @l Z l@l N/A l[,;'3 3 11 17 T3 30#E ASONNEL ,NJL AIES ESCAiPriCN8 415-096 yuvsEnl--0 0l0 @l N/A l7 3 3 11 12 30 LOSS OF OR C AVAC,E TO FACILITV Q

,7 9 (^J 7 ~1 Q, D,(6 Tv8E:ESCA1, cN v , T)',. , , n NRCubeCNk#

I N Gl E P i p9 0N.SSy!N/A i i i iiiiiiiiiili

o*".[/e/d'[{J. w. cahm o3) 7 ss-225 3

..e c. os,w s , ,