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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML19338C4441980-08-11011 August 1980 Ro:On 800804,radioactivity Released in Reactor Bldg.Caused by Helium Circulator Sys Malfunction.Employee Safety Not Jeopardized,Atmospheric Release Negligible & Public Not in Danger ML19318A8991980-06-18018 June 1980 Ro:On 800501 & 0617,minute Releases of Radioactivity Occurred in Reactor Bldg.Caused by Malfunction in Helium Circulator Sys.No Radiation Was Released Into Atmosphere. Public & Personnel Health & Safety Were Not Jeopardized ML19225A2211979-07-12012 July 1979 RO 50-267/77-17(14)1,final on 770506:during Plant Startup at 15% Power,Incorrect Feedwater Flow Trip Existed in 1 of 2 Plant Protective Sys Logics.Caused by Logic Chip Failure in Circular Trip Module CT-2B2 ML19225A1181979-07-12012 July 1979 RO 50-267/76-19A on 760617:while Reactor Was in Shutdown Condition,One Steam Water Dump Valve in Each Loop Opened. Caused by Design Problem.Failure Modes & Effects Analyzed & Steam Water Dump Circuits Revised ML19224D5841979-07-0303 July 1979 RO 50-26/79-13/03-L-0 on 790412:365 Hydraulic Snubbers Found to Be Inoperable During First Functional Test,Causing Both Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Repaired ML20052F1261976-06-14014 June 1976 Ro:On 760521,discrepancies Found in Seismic Certifications for Equipment,Instruments & Components & in Application of Certain Components Required to Meet Seismic Conditions. Caused by Misinterpretation of FSAR Requirements 1980-08-11
[Table view] Category:LER)
MONTHYEARML19338C4441980-08-11011 August 1980 Ro:On 800804,radioactivity Released in Reactor Bldg.Caused by Helium Circulator Sys Malfunction.Employee Safety Not Jeopardized,Atmospheric Release Negligible & Public Not in Danger ML19318A8991980-06-18018 June 1980 Ro:On 800501 & 0617,minute Releases of Radioactivity Occurred in Reactor Bldg.Caused by Malfunction in Helium Circulator Sys.No Radiation Was Released Into Atmosphere. Public & Personnel Health & Safety Were Not Jeopardized ML19225A2211979-07-12012 July 1979 RO 50-267/77-17(14)1,final on 770506:during Plant Startup at 15% Power,Incorrect Feedwater Flow Trip Existed in 1 of 2 Plant Protective Sys Logics.Caused by Logic Chip Failure in Circular Trip Module CT-2B2 ML19225A1181979-07-12012 July 1979 RO 50-267/76-19A on 760617:while Reactor Was in Shutdown Condition,One Steam Water Dump Valve in Each Loop Opened. Caused by Design Problem.Failure Modes & Effects Analyzed & Steam Water Dump Circuits Revised ML19224D5841979-07-0303 July 1979 RO 50-26/79-13/03-L-0 on 790412:365 Hydraulic Snubbers Found to Be Inoperable During First Functional Test,Causing Both Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Repaired ML20052F1261976-06-14014 June 1976 Ro:On 760521,discrepancies Found in Seismic Certifications for Equipment,Instruments & Components & in Application of Certain Components Required to Meet Seismic Conditions. Caused by Misinterpretation of FSAR Requirements 1980-08-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
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REPORT DATE: July 3. 1979 REFORTABLE OCCURRENCE 79-13 ISSUE O OCCURRENCE DATE: April 12, 1979 Page 1 of 3 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO
'. O. B0X 361 r
PLATTEVILLE, COLORADO 80651 REPORT NO. 50-267/79-13/03-L-0 Final IDFNTIFICATION OF CCCURRENCE:
During performance of the hydraulic snubber functional test required by the Fort S t. Vrain Technical Specifications, snubbers were found to'be inoperable.
It cust be assumed that these snubbers were incperable when the plant was at power. This is contrary to LCO 4.3.10, constitutes operation it. a degraded mode, and is reportable per Section AC 7.5.2(b)2 of the Fort St. Vrain Techni-cal Specifications.
EVENT DES CRIPTION :
Specification SR 5.3.8(d) of the Fort St. Vrain Technical Specifications re-quires that a representative sa=ple of ten hydraulic snubbers be tested once each refueling cycle starting with the first refueling. The specification requires a functional test for operability including verification of proper piston =ovecent, lockup, and bleed. The specification states that for each unit and subsequent unit found inop,erable, an additional ten snubbers shall be tested until no more failures are found or all units have been tested.
The Fort St. Vrain Nuclear Generating Station began its first refueling shut-down February 1,1979, and performance of the required testing was begun on April 12, 1979. During performance of the fuutional test, snubbers were found that did not meet the acceptance criteria.
The failure of the tested snubbers to meet the acceptance criteria was both unacceptable lockup characteristics and .aacceptable bleed characteristics.
The table below shows the results of 413 snubbers tested.
Total Snubbers Tested 413 Total Found Operable 48 Total Found Ir. operable 365 Failed Piston Mo vement Test 0 Failed Lockup Test Only 16 Failed Bleed Test only 173 15 053 Failed Lockup and Bleed Test 176 79071206 %
REPORTABLE OCCURRENCE 79-13 ISSUE O Page 2 of 3 EVENT DESCRIPTION (continued):
In addition to those snubbers found to be inoperable when tested, three other items of reportability were identified during perfor=ance of the surveillance test. First, three Class 1 snubbers were found that had been installed by an approved field change in 1976 but had not been added to the list in the Technical Specifications and were not added to tha periodic surveillance in-spection program. Second, sixteen snubbers installed on another approved field change were found not to have bleed capability. Third, approximately half of the snubbers tested were found to have seal =aterial other than ethylene propylene. Technical Specification SR 5.3.8(b) requires all hydraulic snubbers whose seal materials are other than ethylene propylene or other material that has been demonstrated to be compatible with the operating environ =ent be visu-ally inspected for operability every 31 days. Contrary to this requirement the snubbers with non-ethylene propylene seals were not identified and were not inspected every 31 days.
Permission was requestcd and received from the Nuclear Regulatory Commission to delay submittal of this report until completion of the testing and repair program.
CAUS E DESCR!PTION:
The snubbers at the Fort S t. Vrain plant have been installed and in operation for several years and this is the first functional test to be performed. The exact causes of failures were found to be setpoint drif t, dirty oil, and clogged valves.
The cause of the failure to incorporate the three snubbers added in 1976 to the Technical Specification list and surveillance program was the misclassifi-cStion of the change by the originating organization as a change not requiring a Technical Specification change.
The cause of the installation of sixte n snubbers without bleed capability .
was the omission of a bleed rate from che design specification and the resul- ~
tant pu chase of snubbers without bleed capability.
The cause of the failure to perform the inspection of snubbers with non-ethylene propylene seals as required by SR 5.3.8(b) was misinformation, as *o the seal material, which led the organization responsible for surveillance test prepara-tion to believe that all snubbers had ethylene propylene seals.
CORRECTIVE ACTION:
The corrective action for snubbers that failed the functional test was to re-pair or readjust each snubber to meet acceptance criteria. All tested snubbers were reinstalled in operable condition.
415 054
REPORTA3LE OCC'JRRENCE 79-13 ISSUE O Page 3 of 3 CORRECTIVE ACTION (continued):
The failure to properly identify the three Class 1 snubbers involved in a field change was the second occurrence of this type and actually occurred prior to the first identified occurrence (Feportable Occurrence Report No.
50-267/77-41). At the time of the first occurrence a letter was sent to the prime contractor admonishing them for failure to properly review and des,. ribe a Class 1 modification. Since the error described in this report occurr J prior to the issuance of the letter no additional action will be teken. The three snubbers will be temporarily added to Technical Specification Table 4.3.10-1 until a permanent revision to Table 4.3.10-1 is issued in a subse-quent amenneent. The surveillance procedure has been revised to include the three snubbers.
Those snubbers which were found to not have bleed capability were modified by installation of a valve asse=bly providing both lockup and bleed capability.
During the functional test those snubbers that had non-ethylene propylene seals were found to have their seals in good condition. Because there was no evidence of degredation specific to non-ethylene propylene sesis, the seals in use have been deuonsertted to be co= pat.ible with the operating environment.
Therefore, there are ne snubbers at Fort St. Vrain subject to the inspection requirements of SR 5.3.8(b) and no corrective action is required.
Prepared by:
~
S + /_. , A/
Richard R. Frost Technical Services Technician Reviewed by: . / / W- _
. W 'Gahm
'T hnical Services Supervisor Reviewed by:
Frank M. Mathie Operations Manager
/ /
Approved by: 2 / /. IIl[Lw.b. -<. ~ / k //
Don Warenbourg ./ ./
Manager, Nuclear Production