ML19209B775

From kanterella
Revision as of 12:15, 15 August 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 79-060/03L-0:on 790916,differential Pressure Transmitter Failed to Respond to Test Signal.Caused by Transmitter Capsule Failure.New Transmitter Ordered
ML19209B775
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 10/02/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19209B773 List:
References
LER-79-060-03L-01, LER-79-60-3L-1, NUDOCS 7910100433
Download: ML19209B775 (1)


Text

. ._mm LICENSEE EVENT REPORT CONTROL BLOCK: l llllllh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 foT-'I I N i c 81EIP 1 1 @ 150101-!01010 0101-10101@l411 111111@l ll@7 8 9* UCENSEE CODE 14 UCENSE NUMBER 25 26 UCENSE TYPE JO 57 CAT 58 CON'T$"p"C Ll@l0l5 0l-l0l3l2l5 @l0l9l1 6l7l9l@l1l0 0l2l7 9 lg , T 10 1 7__8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h FITl lWhile performing PT 55.9 PC, Shutdown Panel RHR Service Water D/P calibration, differ- l fOTil lential pressure transmitter 1 Ell-PDT-N002BX failed to respond to a test signal.

l-@ Irechnical Specifications 3.3.5.2, 6.9.1.9b l1.9.1.5.J l I O 16lITTG I I.0 8ll7 8 9 80 E OE SU C E COMPONENT CODE SUB D'E SU E gl Wl Al@ g@ l G l@ lI iN lS lT lR lU @ ]@

z[@7 8 9 10 11 12 13 18 19 20_SEQUENTIAL OCCUR R ENCE REPORT REVISION LE R/RO EVENT YEAR REPORT NO.

CODE TYPE N O.@ REl7 9 gl0 l6 l0 l yl0 3 llLlgl0 l21 22 23 24 26 27 28 29 30 31 32 N CT T METH HOURS 22 SUB I FOR B.Su L*MANUF LEJ@lC J@zl@W@llll'I 6@l@W@l R l 3 l7RERl 9lg

" 33 34_35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h

[rhe transmitter capsule failed causing no output signal for the indicator. A new li O g Itransmitter has been ordered and'is to arrive by October 10, 1979. When the transmitter l s received, it will be installed, calibrated, and returned to service. As this is g i i 2 g lthe first failure of this instrument, this is considered an isolated event.

li 4 I l 7 8 9 80 STA% POWER OTHER STATUS De O RY CISCOVERY DESCRimON y @ l0l0 0 [@l NAlg gl Periodic Test l5 7 8 g 12 13 44 46 46 80 RELEASED OF RELEASE AMOUNTOF ACTIVITY LOCATION OF' RELEASE t.!.tu [z )@ LzJ@SES l NAlNAl * .PE son ~R expos

          • DESCRmriOu @

NUM8ER TvPE 10 lo 0 i@lz l@lNA li >'*' PERSONNEt = U L S DESCRenON@

NuM8ER 0 0 10 l@l NA

} } }9. Mli a 7 8 9 11 12 80 LOSS OF oR DAMAGE TO FACluTY TYPE DESCRIPTION l NAl9 7 8 9 10]80'"'"L'?CR,TiOu @

7 910100 / W NRC uSe ONov IS[SU@l NA llllllllllllll$

.2 o 7 8 9 IO 68 69 80 g on, R.--PHONE: ,.NAME OF PREPARER