ML18086A322

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LER 81-004/04T-0:on 810407,containment Fan Cooling Unit 24 Found Leaking Svc Water.Caused by Vent Valve 24SW63 Not Fully Closed.Valve Closed
ML18086A322
Person / Time
Site: Salem PSEG icon.png
Issue date: 04/21/1981
From: STEELE W J
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18086A319 List:
References
LER-81-004-04T, LER-81-4-4T, NUDOCS 8104280654
Download: ML18086A322 (1)


Text

' . NRt..fORM 3-136 (7'.7.71 e LICENSEE EVENT REPORT e NUCLEAR REGULATORY COMMISSION CONTROL BLOCK: I f G) (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 rIIIJ l N I J I s I G I s I 2 101 0 I 0 I -I 0 I 0 I 0 I 0 I 0 I -I 0 I 0 101 4 I 1 I 1 I l I i 101 I I 0 7 8 g LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT SB CON'T CIT!] 7 B LJJ©I ol sl ol ol ol 31 ii iK?)l...2.L4l ol 11 al i@I Ol 4 12-1110 11 IG) 60 61 DOCKET NUMBER 68 69 .OVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@ I While performing routine shift rounds at 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> on 4/7/81, an Equipment

[]JI] Operator discovered a Service Water leak emanating from the No. 24 Containment Fan I Cooling Unit. In accordance with NRC IE Bulletin 80-24, the NRC was notified by [QJ}] I telephone at 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br /> with written confirmation transmitted later in the day. Investigation revealed that a vent valve on the Fan Cooling Unit was not fully [§JI] closed. [ill] 7 B 9 80 [TI!] 7 0 SYSTEM CODE lw IA I@ 9 10 CAUSE CAUSE COMP. CODE SUBCODE COMPONENT CODE SUBCODE l!..J@) lvlAILlvlElxl@ (LI@) 11 12 13 18 19 SEQUENTIAL OCCURRENCE REPORT VALVE SUB CODE 1£..J@ 20 LER'RO LVENTYEAA REPORT NO. CODE TYPE REPORT 1 a 11 1 1 1 1 o r o 1 4 1 1 ....... 1 1 a 1 4 1 l.'!J 1 1 NUMBER 21 22 23 24 26 27 28 29 30 31 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. REVISION NO. w 32 COMPONENT MANUFACTURER TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FOAM liUB. SUPPLIER W@W@ W@ W lolololo!

W@ W@ W@ 33 34 35 36 37 . 40 41 42 43 IR j 3 I 4 I 0 I@ CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @ "" 47 IJlI] I A vent valve (24SW63) was found not p1lly closed. The valve was closed stopping the leak: No explanation for the valve not being fully closed can be found. r::mJ o:rn o::m 7 B 9 FACILITY tJ()\ STATUS % POWER OTHER STATUS v:::;:/ [ill] l£.J@ I 0 I 0 I 0 l@)I NA I 1 0 e 10 12 13 "" ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY IIill W @) L!J@"-1 ....;N=A'"--------.11 1 0 9 10 11 "" . PERSONNEL EXPOSURES t::::\_ METHOD OF DISCOVERY L!..J{§)I Operator 45 46 I NA DISCOVERY DESCRIPTION Observation LOCATION OF RELEASE @ 80 80 80 NUMBER A TYPE DESCRIPTION Em I ol al 1 .0 9 11 12 13 80 PERSONNEL INJURIES NUMBER EE] I cl al 1 0 e 11 12 00 LOSS OF OR DAMAGE TO FACILITY 143\ TYPE DESCRIPTION E1IJ 7 B 9 10 80 PUBLICITY C\ NRC USE ONLY .. ISSUEDt,;:;\

IIIIJ I I I I I I I I I I I I I! 7 8 9 10 6B 69 80 ; 0 a. w. J. Steele NAME OF

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