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[Table view] Category:Licensee Response to Notice of Violation
[Table view] |
See also: IR 05000454/2008008
Text
Nuclear June 4,2008 LTR: BY RON 2008-0054
File: 2.01.0700
United States Nuclear Regulatory
Commission
Attention:
Document Control Desk Washington, DC 20555-0001
Byron Station, Unit
1 and Unit 2 Facility Operating License Nos. NPF-
37 and NPF-66 NRC Docket Nos. STN
50-454 and STN 50-455 Subject: Response to NRC Request Concerning Unresolved
Item 0500045412008008
and0500045512008008 Reference: Letter from
Ann Marie Stone (USNRC) to Charles
G. Pardee (Exelon Generation Company, LLC), "Byron Station, Units 1 and 2 Follow Up
Inspection
of an Unresolved
ltem (URI) 0500045412008008;
05000455/2008008," dated May 5,2008 In the referenced letter, the NRC requested
a response within 30 days with our
proposed actions and schedule to resolve the noncompliance
of the single failure assumptions used in
our Ultimate Heat Sink (UHS) design basis analysis.
To achieve compliance, a design basis re-analysis
of the UHS is being performed
to evaluate the impact of postulated
passive electrical single failures.
The results of this analysis will be incorporated
into the Byron Station design basis
via requirements
of 10 CFR 50.59, "Changes, tests, and experiments.'This
is expected to be completed
by December 5, 2008. We do not anticipate
any physical modifications
to the UHS will be necessary.
In the interim, we have invoked the provisions
of Administrative Letter
98-1 0, "'Dispostioning
of Technical Specifications
That are insufficient
to Assure Plant Safety.'" We have concluded
that the UHS remains operable with administrative controls
in place to ensure seven of the eight UHS cooling cells are operable to
be within the Limiting Condition
for Operations
for Technical Specifications
3.8.9, "Ultimate Heat
Sink.'" These interim controls will remain
in place until the design basis for the UHS is revised.
June 4,2008 U.S. Nuclear Regulatory Commission
Page 2 There are no regulatory commitments associated with this response. Should you have any questions about
this letter, please contact Mr. William Grundmann at (81 5) 406- 2800. Respectfully, David M. Hoots Site Vice President Byron Station
cc: Regional Administrator - NRC Region Ill NRC Senior Resident Inspector - Byron Station
Director, Office of Enforcement