ML18096A735

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Ro:On 920423,fire Pump 1 Declared Inoperable & Remains Inoperable Due to Broken Crankshaft.Both Fire Suppression Sys Inoperable.On 920515,fire Pump 2 Declared Inoperable Due to Severe Oil Leak.Written Rept to Be Provided in 14 Days
ML18096A735
Person / Time
Site: Salem  PSEG icon.png
Issue date: 05/15/1992
From: LABRUNA S
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NLR-N92072, NUDOCS 9205290022
Download: ML18096A735 (2)


Text

Public Service Electric and Gas Company Stanley LaBruna Public Service Electric and Gas Company P.O. Box 23.6, Hancocks Bridge, NJ 08038 609-339-1200

  • Vice President

-Nuclear Operations MAY 1 1992 NLR-N92072 united states Regtilatory**commission Document Control Desk Washington, DC 20555 Gentlemen:

CONFIRMATORY LETTER REGARDING THE INOPERABILITY OF SALEM STATION FIRE PUMPS DOCKET NOS. 50-272 AND 50-311 No. 1 Fire Pump was declared inoperable on April 23, 1992, and remains inoperable due to a broken crankshaft.

Repairs to the crankshaft are being performed at the manufac.turer' s facility.

On May 15, 1992, during performance of a surveillance test the 2 Fire Pump was declared inoperable due to a oil leak. Accordingly, consistent with the Salem Units 1 and 2 Technical .specification requirements (3.7.10.1 Action b), with both fire -suppression systems inoperable, PSE&G established a back up fire suppression system and reported the event to Nuclear Regulatory Commission in accordance with the requirements of the Emergency Classification Guide Section.18 initiating condition R. Pursuant to the requirements of Salem Technical Specification 3.7.10.1 Action b, PSE&G hereby submits this confirmatory letter documenting the Fire Pumps inoperability.

Additionally, in accordance with Salem Technical Specification requirements, a written report will be provided to the Commission within 14 days of the event outlining the cause of the inoperability, the corrective actions taken, and a schedule for restoring the system .to operable status. Should you have any questions in regard to this transmittal, do not hesitate to call. -')) _,.. .-.. .r ... ,*, d; 9205290022 920515 PDR ADOCK 05000272 S PDR I, . . / \*'- .... __ ,/

tk' lf:iVJ}J . I l '\', \J J Document Control Desk NLR-N92072 c Mr. J. c. Stone Licensing Project Manager Mr. T. Johnson Senior Resident Inspector 2 Mr. Martin, Administrator Region I Mr. Kent Tosch, Chief --New Jersey Department of Environmental

_Protection Division of Environmental Quality

  • Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625 MAY 1 5 1992