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 Issue dateTitleTopic
05000298/LER-1982-005, Amended LER 82-005/03X-1:on 820221,surveillance Test Indicated MSIV 86A Had Closing Time Faster than Allowed by Tech Specs.Caused by Loss of Nitrogen Preload & Fluid from Hydraulic Sys Accumulator.Accumulator Recharged & Tested20 October 1982Amended LER 82-005/03X-1:on 820221,surveillance Test Indicated MSIV 86A Had Closing Time Faster than Allowed by Tech Specs.Caused by Loss of Nitrogen Preload & Fluid from Hydraulic Sys Accumulator.Accumulator Recharged & Tested
05000298/LER-1982-014, Amended LER 82-014/03X-1:on 820607,rejectable Indications Found in Heat Affected Zones of Welds BJ-13,BJ-15,BJ-20 & BJ-23.Caused by Improper Fabrication Techniques.Affected Piping & Fittings Replaced3 February 1983Amended LER 82-014/03X-1:on 820607,rejectable Indications Found in Heat Affected Zones of Welds BJ-13,BJ-15,BJ-20 & BJ-23.Caused by Improper Fabrication Techniques.Affected Piping & Fittings ReplacedAnchor Darling
Liquid penetrant
05000298/LER-1993-00118 March 1993LER 93-001-00:on 930225,several Design Discrepancies in SW & Reactor Equipment Cooling Sys Identified.Caused by Piping Configuration Error During Plant Const.Mechanical & Electrical Mods Will Be made.W/930318 Ltr
05000298/LER-1993-00722 April 1993LER 93-007-00:on 930326,determined That ECCS Pump Compartment Cooler Power Supply Design Defect Could Have Prevented Adequate Containment Heat Removal.Caused by Design Errors.Mods Planned to Provide Convection Cooling
05000298/LER-1993-00822 April 1993LER 93-008-00:on 930328,4,160-volt Breakers 1BG,1GB & 1GE Tripped Due to Actuation of 1GS Breaker Lockout Relay.Caused by Oversight in Design Change Installation Instructions. Work Stopped & Design Change Implemented
05000298/LER-1993-0296 August 1993LER 93-029-00:on 930708,partially Withdrawn Control Rod 26-31 Scrammed.Caused by RPS Scram Signal from Two of Four Reactor Pressure Scram Switches.Scram Reset & Pressure Testing completed.W/930806 Ltr
05000298/LER-1993-0309 August 1993LER 93-030-00:on 930708,discovered Inadequate Inservice Testing of Svc Water Sys Check Valves Due to Flow Instrument Calibr Error & Personnel Error in Specifying Sys Flow Requirement.Revised Calibr Factor developed.W/930809 Ltr
ML17054D24113 May 1980Annual Financial Rept 1979
ML17348B5069 October 1990Part 21 Rept Re Zener Diode VR2 on Power Supply Board 9 1682 00 106 Possibly Being Installed Backwards
ML17352A86931 May 1993Technical Rept, Assessment of Aging Degradation of Civil/ Structural Features at Selected Operating Nuclear Power Plants.Boric Acid
Coatings
Operating Basis Earthquake
Tornado Missile Protection
Earthquake
ML18024B54323 January 1980LER 79-043/03L-0:on 791228,during Normal Operation,Routine Tour Indicated through-wall Crack of Weld on Discharge of a & B Radiant Energy Conversion Pump Discharge Piping.Cause Undetermined.Temporary Soft Patch Installed
ML18038A8977 September 1994Part 21 Rept Re Defect in Latching Mechanism of Potter & Brumfield Relay on C&D High Voltage Shut Down Alarm Assembly Printed Circuit Boards.Pull Test on Relay Reset Button Incorporated Into Receiving Insp Procedures
ML18096B2421 February 1993Part 21 Rept Re Possible Matl Defect in Stainless Steel Swagelock Tube Fittings.Initially Reported on 921218.List of Part Numbers,Heat Codes & Addl Affected Customers Encl
ML19207C39520 August 1979LER 79-019/01T-0:on 790809,upon Auto Start Signal,High Pressure Coolant Injection Pump Did Not Initially Start. Caused by Deterioration of Piston Rings in Valve Actuator. Rings Replaced & Test Completed Satisfactorily
ML19208D4227 September 1979LER 79-021/03L-0:on 790811,carbon Absorber in Standby Gas Treatment Sys B Was Wetted W/Water When Control Room Received Actuation Alarm for Deluge Sys.Caused by Improper Installation of Baseplate of Fire Detection Unit
ML19208D4427 September 1979LER 79-022/03L-0:on 790812,water from Carbon Absorber Housing of Standby Gas Treatment Sys a Sprayed Carbon Absorber Trays,Rendering Trays Inoperable.Caused by Inadequate Seating Area Between Valve Clapper & Latch
ML19208D4635 September 1979LER 79-020/03L-0:on 790809,while Performing Surveillance Procedure on Relief Valve Bellows Monitoring Sys,Pressure Switch MS-PS-71G Failed to Actuate.Caused by Improper Assembly.Switch Was Replaced
ML19208D4887 September 1979LER 79-023/03L-0:on 790809,Barton Model 288 Differential Pressure Indicating Switch MS-DPIS-119B Was Found in Excess of Tech Specs Table 3.2.A.Caused by Faulty Switch. Microswitch Assembly Was Replaced
ML19209C4638 October 1979Monthly Operating Rept for Sept 1979
ML19210C3972 November 1979Revised Monthly Operating Rept for Oct 1979
ML19210C4438 November 1979Monthly Operating Rept for Oct 1979
ML19210D56725 October 1979Revised LER 79-011/03L-1:on 790424,reactor Water Cleanup Contactor CR105X Auxiliary Contacts Failed During Cold Shutdown.Caused by Failure of Auxiliary Contact Mechanism. Contactor Retrofitted
ML19210D65629 October 1979LER 79-027/03L-0:on 791001,during Routine Surveillance Procedure MS-DPIS-119B,switch Was Found W/Setpoints in Excess of Tech Specs.Caused by Setpoint Drift.Instrument Recalibr
ML19210D6999 November 1979LER 79-029/03L-0:on 791012,during Routine Plant Tour,Pinhole Leak Detected in Upstream Weld of Supply Isolation Valve. Cause Unknown.Weld Will Be Repaired During Next ShutdownFire Barrier
ML19210F01320 November 1979LER 79-030/03L-0:on 791021,while Pumping Water from Torus to radwaste,drywell-to-torus Differential Pressure Dropped Below Tech Specs.Caused by Nitrogen Pressure Forcing Water from Downcomers to Flow to Torus
ML19210F01621 November 1979LER 79-032/03L-0:on 791026,during Normal Operation,Doors to HPCI & RHR B&D Pump Rooms Left Open W/O Fire Watch.Caused by Personnel Error.Occurrence Discussed W/Personnel Involved. Fire Doors Controlled by Procedure Posted W/SignsFire Watch
ML19224D79830 May 1979LER 79-012/03L-0 on 790503:vessel Water Temp Increased to 220 F W/Primary Containment Integrity Not Established.Caused by Omission in Operating Procedures.Setpoint of Interlock Verified & Procedures Revised
ML19224D80323 June 1979LER 79-015/03L-0 on 790525:breaker 1AS Failed to Close Automatically.Caused by Improper Operation of Switch 52 in Breaker 1AN.Switch Contacts Cleaned & Tested Satisfactorily
ML19224D80830 May 1979LER 79-013/03L-0 on 790508:correct Drywell to Suppression Chamber Reading Not Established.Caused by Leaking Inlet Purge Valve.Valve Repaired & Leak Tested
ML19224D8198 June 1979LER 79-014/03L-0 on 790509:chamber Vent Valve for Torus Level Transmitter Was Left Closed.Caused by Technician Error.Vent Valve Opened & PC-LT-12 Placed Back Into Svc
ML19242A39526 June 1979LER 79-016/03L-0 on 790531:RHR Pump 1A Tripped During Start on Overcurrent in Phase C.Caused by Failure of GE Model 121AC66K8A Overcurrent Relay Operating Disc to Return to Normal Position.Relay Cleaned,Recalibr & Retested
ML19242B48819 July 1979LER 79-017/03L-0 on 790620:during Review,Observed That Surveillance Procedure 6.2.4.1 Did Not Include Daily Check of Undervoltage Relays or Monthly Functional Testing. Cause Unstated.Procedures Revised
ML19242D2633 August 1979Monthly Operating Rept for Jul 1979
ML19246B5729 July 1979Monthly Operating Rept for June 1979
ML19249C4316 September 1979Monthly Operating Rept for Aug 1979
ML19250B96628 September 1979LER 79-025/03L-0:on 790912,HPCI Turbine Stop Valve Separated from Actuator at Split Coupling.Caused by Improperly Mfg Split Coupling.Split Coupling Replaced & Installation Procedures Revised
ML19250C02428 September 1979LER 79-024/03L-0:on 790831,surveillance Testing Pressure Switch NBI-PS-55D Found W/Trip Point Below Tech Specs.Cause Not Stated.Switch Readjusted to Proper Setpoint & Then Replaced After Unsatisfactory Performance
ML19250C0349 October 1979LER 79-026/03L-0:on 790912,investigation Found Unidentified Drywell Leak on Reactor Recirculation Pump B.Caused by Failure of Pump Seal at Natural End of Life.Seal Replaced.No Further Action Planned
ML19256G5306 December 1979LER 79-033/03L-0:on 791109,surveillance Procedure Re Diesel Generator Operability Not Performed on Diesel Generator 1. Personnel Under Impression Diesel Generator 2 Would Not Be Made Operable.Test Performed Following Day
ML19256G53312 December 1979LER 79-037/03L-0:on 791113,diesel Generator 1 Failed to Start.Caused by Silencer Bypass Solenoid Stopping in mid- Position Due to Insufficient Air Supply.Valve Opened & Air Supply Capped.Sys Will Be Modified
ML19256G53710 December 1979LER 79-036/03L-0:on 791110,four Cylinder Sleeves in Diesel Generator 2 Damaged During Surveillance Test.Cause Under Investigation.Damaged Parts Replaced & Cylinders Inspected
ML19256G5466 December 1979LER 79-034/03L-0:on 791107,base for Diesel Generator 2 Lube Oil Header to Cam Chain Tensioner Broke.Caused by Hose Proximity to Cam Chain & Tensioner Sprocket.Hose Replaced & Clamped Away from Cam Chain
ML19256G5687 December 1979LER 79-035/03L-0:on 791109,during Core Spray Operability Surveillance procedure,CS-MO-12A Valve Would Not Open Electrically.Caused by Failure of Axial Movement on Worm Set Clutch Collar.Valve Repaired
ML19257B93811 January 1980LER 80-001/01T-0:on 800102,during HPCI Turbine Stop Valve Monitor Test,Procedural Steps Were Improperly Completed. Caused by Personnel Error.Occurrence Discussed W/Operations & Instrument Personnel
ML19257C5584 January 1980LER 79-041/03L-0:on 791206,during Surveillance Testing of HPCI DCIS-76 & 77,HPCI DPIS-76 Went Downscale After Being Placed Back in Svc.Caused by Technician Error.Signal Reset, Valves Opened & Technician Cautioned
ML19257C58928 December 1979LER 79-038/03L-0:on 791130,during Normal Operation, Suppression Chamber Level Instrument PC-LI-12 Failed Downscale.Caused by Failure of Power Supply.Power Supply Replaced & Proper Indication Verified
ML19257C61516 January 1980LER 79-042/03L-0:on 791223,during Routine Check,Rhr Pump 1D Breaker Found Not Charged.Rhr Pump 1D Could Not Operate. Caused by Loose Screw Holding Wire on Latch Monitoring Switch Preventing Charging Motor Operation.Tightened Screw
ML19257C62128 December 1979LER 79-039/03L-0:on 791129,suppression Chamber Inboard Vent Isolation Valve PC-230MV Not Operable W/Control Switch & No Position Indication Observed in Control Room.Caused by Random Failure.Rotor Replaced W/Qualified Part
ML19257C6402 January 1980LER 79-040/03L-0:on 791203,while Performing Maint on Backwash Line for Svc Water Pump Strainer,Execessive Erosion Noted in Pressure Boundary Piping.Caused by High Water Velocity & Solids Content of Backwash Line
ML19259A78531 December 1978Monthly Operating Rept for Dec 1978