ML19257B938

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LER 80-001/01T-0:on 800102,during HPCI Turbine Stop Valve Monitor Test,Procedural Steps Were Improperly Completed. Caused by Personnel Error.Occurrence Discussed W/Operations & Instrument Personnel
ML19257B938
Person / Time
Site: Cooper Entergy icon.png
Issue date: 01/11/1980
From: Mike Williams
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19257B937 List:
References
LER-80-001-01T, LER-80-1-1T, NUDOCS 8001210276
Download: ML19257B938 (1)


Text

NRCg FORM 366 U.S. NUCLEAR REGULATORY COMMISSION

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LICENSEE EVENT REPORT CONTROL BLOCK: l l 1 l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

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DOCK ET NUMBER 60 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o 121 lDuring performance of surveillance procedure 6.2.2.3.12. HPCI-Turbine Stop Valve 1 o 3 l Monitor, Oil Pressure and Supervisorv Alarm Timer Calibration and Functional Test. l 0 4 lorocedural steps were not properly cornleted as reonfred. The MPPT n nvi l I nrv nil l 0I5 louco was found in the "Pul l-To-Lock" no s iti on nnn rnv4-9 e ol v % hnura afror tha enr I o 6 lun411,nco enee h2A bon e pigggg_ MPrT una_ rharafnra. innnornblo in ehe nurnaneir4 o 7 lende during Phia narind nf rimo All vamnining 1:Tr4 Cuernac upro nnavnhlp_ thne 1 o 8 Ithis event had no affect on oublic health and saferv. _.]

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7 8 9 10 II 12 IJ 1 14 19 20 SEQUENTI AL OCCUR R E NCE REFORT REVISION G ._ EVENT YEAR REPORT NO. CODE TYPE NO.

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_2t 22 23 24 26 27 23 29 30 Ji 32 ACTION FUTURE EFFECT $HUTDOWN ATT AC HY E N T N P R D-4 PRIVE COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS 22 SUBVITTED FORMhUS. SUPPLIER VANUFACTURER

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42 43 47 CAUSE DESCRIPTION AND CORREC 'lVE ACTIONS i o iThe cause of this occur rence has been attributed to cersonnel error due to instru- I liliiIment personnel's failure to cerform erocedural stens nnd onerations norsonnel f,414 l i I 'l lure to verifv HPCI system configuration uoon comoletion of surveillance orocedure.

t i IThis occurrence b,a boon discucand direct 1v vi*h norsneral invnivod nnd indi*ect1v i i 4 lwith all operations and instru~ent nersonnel. I 1 8 9 80 ST S g POWER OTHER STATUS ISCOV RY OtSCOVERY DESCRtPTION i 5 W @ l019l6I@l NA I bLjhl Onerator Observation I A TIVITY CONTENT RELEASED OF RE LE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE

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