05000298/LER-1979-020-03, /03L-0:on 790809,while Performing Surveillance Procedure on Relief Valve Bellows Monitoring Sys,Pressure Switch MS-PS-71G Failed to Actuate.Caused by Improper Assembly.Switch Was Replaced

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/03L-0:on 790809,while Performing Surveillance Procedure on Relief Valve Bellows Monitoring Sys,Pressure Switch MS-PS-71G Failed to Actuate.Caused by Improper Assembly.Switch Was Replaced
ML19208D463
Person / Time
Site: Cooper Entergy icon.png
Issue date: 09/05/1979
From: Phillips D
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19208D459 List:
References
LER-79-020-03L, LER-79-20-3L, NUDOCS 7909280455
Download: ML19208D463 (1)


LER-1979-020, /03L-0:on 790809,while Performing Surveillance Procedure on Relief Valve Bellows Monitoring Sys,Pressure Switch MS-PS-71G Failed to Actuate.Caused by Improper Assembly.Switch Was Replaced
Event date:
Report date:
2981979020R03 - NRC Website

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a NRC FQRM 366 ll U. S. NUCLEAR REGULATORY COMMISSION

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M.jCENSEE EVENT REPORT CONTROL BLOCK:

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8 60 61 DOCK ET NUVSER 68 63 EVENT DATE 74 75 REPORT CATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h o

2 l While performing Surveillance Procedure (S.P. 6.2.2.2.5) on the reifef valve bellnus I

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monitoring system as required by Tech. Spec. 4.6.D.4. pressure switch MS-PS-71G failedl o

4 l to actuate. The pressure switches on all sne other relief valves were operable. Therel o

s wer1 no significant occurrences as a result of the event.

Similar event was UE 75-1. I o

6 l There were nO adverse affects to public health and safety.

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CAUSE

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VALVE CODE CODE SUSCODE COVPONENT CODE SU8 CODE SUSCODE [o_L9_j l Il Flh Wh lB lh l I Nl S I T I R I U lh l_E_,j h (l_l h 7

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o lA pressure switch. Model A 17-1 manufactured bv Pressure Controls. Inc. f,1?oA en, r-1 i

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ltorily. The removed pressure switch was returned to the manufacturer whose analysis I

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lshOwed that it had been improperly assembled. The manufacturer stated this was a l

unique occurrence and no further action is recuir_ed.

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