|
---|
Category:Letter
MONTHYEARML24303A0902024-10-29029 October 2024 Operator Licensing Examination Approval IR 05000352/20240122024-10-17017 October 2024 Commercial Grade Dedication Inspection Report 05000352/2024012 and 05000353/2024012 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24274A2372024-10-0707 October 2024 – Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding Primary Containment Leakage Technical Specifications ML24278A3022024-10-0404 October 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10 CFR 50.62 ATWS Rule to Support the Digital Modernization Project Installation - Rev Unit 2 Technical Spec ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24263A0032024-09-27027 September 2024 Generation Station, Units 1 and 2 – Regulatory Audit Plan Supporting Review of the Component Interface Module System of the Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) (Redacted) ML24243A0482024-09-19019 September 2024 Generation Station, Unit Nos. 1 and 2 - Schedule Update for License Amendment Request to Replace Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System ML24215A4042024-09-18018 September 2024 Request for Withholding Information from Public Disclosure IR 05000352/20244202024-09-16016 September 2024 – Security Baseline Inspection Report 05000352/2024420 and 05000353/2024420 RS-24-090, Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-09-12012 September 2024 Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds IR 05000352/20250102024-09-10010 September 2024 Information Request for Quadrennial Baseline Comprehensive Engineering Team Inspection; Notification to Perform Inspection 05000352/2025010 and 05000353/2025010 ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification IR 05000352/20230022024-09-0404 September 2024 Reissued Integrated Inspection Report 05000352/2023002 and 05000353/2023002 IR 05000352/20240052024-08-29029 August 2024 Updated Inspection Plan for Limerick Generating Station, Units 1 and 2 (Report 05000352/2024005 and 05000353/2024005) ML24241A1952024-08-28028 August 2024 License Amendment Request for Modification to Technical Specification 3.6.1.2 and Main Steam Isolation Valve Leakage Rate Requirements ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24163A3902024-08-14014 August 2024 Request for Withholding Information from Public Disclosure IR 05000352/20240022024-08-12012 August 2024 Integrated Inspection Report 05000352/2024002 and 05000353/2024002 ML24220A2392024-08-12012 August 2024 Correction to Technical Specification Page 3/4 3-11 in Amendment No. 225 ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24204A0712024-07-29029 July 2024 Issuance of Amendment Nos. 263 and 225 Technical Specifications for Main Steam Line Tunnel Temperature ML24208A1592024-07-25025 July 2024 Regulatory Audit Plan Supporting Review of the System Development Portion of Limerick Digital Instrumentation and Controls License Amendment Request (EPID L-2022-LLA-0140) - Non-Proprietary ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24201A1662024-07-19019 July 2024 Response to Request for Additional Information for License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam L ML24199A1842024-07-15015 July 2024 RAI-LAR for Limerick EPID: L-2024-LLA-0079- Use This Version RS-24-070, Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions2024-07-12012 July 2024 Independent Spent Fuel Storage Installation, Nine Mile Point, Units 1 and 2, Quad Cities, Units 1 and 2, R. E. Ginna - Nuclear Radiological Emergency Plan Document Revisions ML24180A1572024-06-28028 June 2024 Request to Return and Replace WEC Documents (EQ-EV-386-GLIM, EQ-QR- 433-GLIM, and APP-GW-GLR-611), to Meet 10CFR2.390 Request to Withdraw from Public Disclosure Requirements ML24170A7702024-06-20020 June 2024 Individual Notice of Consideration of Issuance of Amendments to Renewed Facility Operating Licenses, Proposed No Significant Hazards Consideration Determination, Opportunity for Hearing(Epid L-2024-LLA-0079) LTR 05000352/LER-2024-003, Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK1232024-06-18018 June 2024 Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK123 ML24166A1142024-06-14014 June 2024 Response to Requests for Additional Information (RAIs 15 Through 23) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24165A2642024-06-13013 June 2024 License Amendment Request for Proposed Changes to the Technical Specification Isolation Actuation Instrumentation Tables and New Turbine Enclosure Main Steam Line Tunnel Temperature TS 3/4.7.9 05000352/LER-2024-001, Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit2024-06-10010 June 2024 Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit 05000352/LER-2024-002, Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker2024-06-10010 June 2024 Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker ML24151A2012024-06-10010 June 2024 Request for Withholding Information from Public Disclosure ML24151A2882024-06-10010 June 2024 Request for Withholding Information from Public Disclosure ML24150A0242024-05-29029 May 2024 Notification of Commercial Grade Dedication Inspection (05000352/2024012 and 05000353/2024012) and Request for Information ML24149A2112024-05-28028 May 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFR50.62 ATWS Rule to Support the Digital Modernization Project Installation ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 IR 05000352/20243022024-05-20020 May 2024 Revised Initial Operator Licensing Examination Report 05000352/2024302 and 05000353/2024302 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000352/20240012024-05-0707 May 2024 Integrated Inspection Report 05000352/2024001 and 05000353/2024001 ML24124A0432024-05-0303 May 2024 Response to Requests for Additional Information (RAIs 9 Through 14) for License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with RS-24-038, Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-05-0202 May 2024 Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24114A3222024-04-23023 April 2024 Supplement to License Amendment Request to Revise the Licensing and Design Basis to Incorporate the Replacement of Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System (PPS) - Pivot to Unit ML24109A0702024-04-18018 April 2024 Supplement to License Amendment Request to Revise Technical Specifications and Exemption Request from Requirements of 10CFRC50.52 ATWS Rule to Support the Digital Modernization Project Installation . ML24093A0912024-04-17017 April 2024 Revised Estimated Review Completion Date Concerning License Amendment Request to Replace Existing Safety-Related Analog Control Systems with a Single Digital Plant Protection System ML24106A1832024-04-15015 April 2024 Submittal of Changes to Technical Specifications Bases 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000352/LER-2024-003, Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK1232024-06-18018 June 2024 Core Operating Limits Report Thermal Limit Exceeded for Unit 1 Fuel Bundle GGK123 05000352/LER-2024-002, Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker2024-06-10010 June 2024 Invalid Actuation Due to a Trip of 1B Reactor Protection System Circuit Breaker 05000352/LER-2024-001, Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit2024-06-10010 June 2024 Leakage for the Unit 1 `B Outboard Main Steam Isolation Valve Exceeded Technical Specification Limit 05000352/LER-2017-0012017-01-27027 January 2017 Condition Prohibited by TS due to Parts Quality Issue, LER 17-001-00 for Limerick Generating Station, Units 1 and 2 Regarding Condition Prohibited by TS due to Parts Quality Issue 05000353/LER-2016-0012016-07-27027 July 2016 Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error, LER 16-001-00 for Limerick, Unit 2 Regarding Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error 05000352/LER-2016-0032016-05-18018 May 2016 Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak, LER 16-003-00 for Limerick, Unit 1, Regarding Plant Shutdown Required by Technical Specification Due to a Pressure Boundary Leak 05000352/LER-2016-0022016-04-11011 April 2016 Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements, LER 16-002-00 for Limerick, Unit 1 & 2, Regarding Condition Prohibited by Technical Specifications Due to Inoperable Safeguard Batteries During Cell Replacements 05000352/LER-2016-0012016-03-23023 March 2016 Inoperable Reactor Enclosure Secondary Containment Integrity Due to Open Airlock, LER 16-001-00 for Limerick, Unit 1, Regarding Condition That Could Have Prevented Fulfillment of the Reactor Enclosure Secondary Containment Integrity Safety Function 2024-06-18
[Table view] |
Text
Exelon Generation
.. LG-16-083 July 27, 2016 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Limerick Generating Station, Unit 2 Renewed Facility Operating License No. NPF-85 NRC Docket No. 50-353 10CFR50.73
Subject:
LEA 2016-001-00, Manual Actuation of the Reactor Protection System This Licensee Event Report (LEA) addresses a manual actuation of the reactor protection system (RPS) following a trip of both reactor recirculation pumps. The pump trips occurred during testing of a modification to the Plant Process Computer (PPC). The manual scram was directed by the unexpected/unexplained change in core flow procedure (OT-112) due to the tripping of the reactor recirculation pumps at power. An error in the modification wiring design caused an actuation of the reactor recirculation pump trip relays. This LEA is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(iv)(A).
There are no commitments contained in this letter. If you have any questions, please contact Robert 8. Dickinson at (610) 718-3400.
Respectfully, '"
Richard W. Libra Site Vice President
-Limerick Generating Station Exelon Generation Company, LLC cc: Administrator Region I, USNRC USNRC Senior Resident Inspector, LGS NRC FORM 366 (01-2014) NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION(01-2014)
LICENSEE EVENT REPORT (LER) (See Page 2 for required number of digits/characters for each block)
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 01/31/2017 Estimated burden per response to comply with this mandatory collection request: 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME Limerick Generating Station, Unit 2 2. DOCKET NUMBER 05000353 3. PAGE 1 OF 3 4. TITLE Manual Actuation of the Reactor Protection System When Critical Due to Wiring Design Error 5. EVENT DATE 6. LER NUMBER 7. REPORT DATE 8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL NUMBER REV NO. MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 05000 06 01 2016 2016 - 001 - 00 07 27 2016 FACILITY NAME DOCKET NUMBER 05000 9. OPERATING MODE 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 1 20.2201(b) 20.2203(a)(3)(i) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii) 20.2201(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(2)(i) 50.36(c)(1)(i)(A) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A)
- 10. POWER LEVEL 20.2203(a)(2)(ii) 50.36(c)(1)(ii)(A) 50.73(a)(2)(iv)(A) 50.73(a)(2)(x) 100 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(v)(A) 73.71(a)(4) 20.2203(a)(2)(iv) 50.46(a)(3)(ii) 50.73(a)(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(C)
OTHER 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(v)(D)
Specify in Abstract below or in NRC Form 366A
- 12. LICENSEE CONTACT FOR THIS LER FACILITY NAME Robert B. Dickinson, Manager - Regulatory Assurance TELEPHONE NUMBER (Include Area Code) 610-718-3400 13. COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT CAUSE SYSTEM COMPONENT MANU-FACTURER REPORTABLETO EPIX CAUSE SYSTEM COMPONENT MANU-FACTURER REPORTABLE TO EPIX B AD P G080 Y 14. SUPPLEMENTAL REPORT EXPECTED YES (If yes, complete 15. EXPECTED SUBMISSION DATE)
NO 15. EXPECTED SUBMISSION DATE MONTH DAY YEAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)
A manual actuation of the reactor protection system (RPS) when the reactor was critical was initiated during Plant Process Computer (PPC) modification testing at power. A modification wiring design error caused an actuation of both reactor recirculation pump (RRP) trip relays when a circuit isolation switch was closed. The direct cause of the event was a circuit wiring design error implemented in the field that caused energization of the RRP adjustable speed drive (ASD) trip coils. The root cause of the event was a failure of station personnel to appropriately apply Technical Human Performance (THU) error prevention techniques to identify the design error and prevent its installation and testing as part of the modification. The isolation switch for the mis-wired circuit was opened to enable reset of the ASD trip coils. The 2A and 2B ASDs were returned to service. The corrective actions are to change the circuit design to correct the design error. The human performance aspects of the event will be addressed through several management actions that include reinforcement of proper standards and behaviors related to THU error techniques with station personnel.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION(01-2014)
LICENSEE EVENT REPORT (LER) CONTINUATION SHEET APPROVED BY OMB: NO. 3150-0104 EXPIRES: 01/31/2017 Estimated burden per response to comply with this mandatory collection request: 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME 2. DOCKET 6. LER NUMBER 3. PAGELimerick Generating Station, Unit 2 05000353 YEAR SEQUENTIAL NUMBER REV NO. 2 OF 3 2016 - 001 -00 NARRATIVE NRC FORM 366A (01-2014)
Unit Conditions Prior to the Event
Unit 2 was in Operational Condition (OPCON) 1 (Run) at approximately 100 percent power with PPC modification testing in progress. There were no structures, systems or components out of service that contributed to this event.
Description of the Event
On Wednesday, June 1, 2016, Limerick Unit 2 was operating at 100 percent power with PPC (EIIS:CPU) modification testing in progress. The modification testing directed closure of a circuit isolation switch which resulted in the trip of both RRPs (EIIS:P) due to an error in the modification wiring design. The control room supervisor (CRS) entered the procedure for an unexpected/unexplained change in core flow (OT-112) due to the trip of both RRPs. The procedure directed a manual actuation of RPS.
All control rods inserted and safety significant systems functioned as expected. Reactor level initially increased then decreased to approximately +0 inches which is less than the
+12.5 inch low level setpoint for RPS. Level then stabilized at normal level. Nuclear Steam Supply Shutoff System Groups IIA and IIB isolations actuated on low level at +12.5 inches. The digital feedwater level control system functioned as designed. Reactor pressure vessel pressure was controlled by the main steam bypass valves.
The investigation of the event identified that a wiring design error caused an unplanned actuation of both RRP trip relays when a circuit isolation switch was closed as directed by the modification acceptance test procedure.
A four-hour ENS notification (#51968) was completed on Wednesday, June 1, 2016, at 1041 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.961005e-4 months <br /> as required by 10CFR50.72(b)(2)(iv)(B) for an actuation of RPS when the reactor is critical. This LER is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(iv)(A) for a manual actuation of RPS.
Analysis of the Event
There was no actual safety consequence associated with this event. The potential safety consequences of this event were minimal. All control rods were verified to be fully inserted following the RPS actuation. The 2A RRP was restarted at 1548 hours0.0179 days <br />0.43 hours <br />0.00256 weeks <br />5.89014e-4 months <br /> on June 1, 2016 and the 2B RRP was restarted at 0326 hours0.00377 days <br />0.0906 hours <br />5.390212e-4 weeks <br />1.24043e-4 months <br /> on June 2, 2016.
The PPC replacement modification was in progress and computer input points were being transferred from the original computer to the new computer. When the second RRP related computer point was placed in service by closure of a circuit isolation switch both 2A and 2B RRP trip relays were energized due to an error in the wiring design.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION(01-2014)
- 1. FACILITY NAME 2. DOCKET 6. LER NUMBER 3. PAGELimerick Generating Station, Unit 2 05000353 YEAR SEQUENTIAL NUMBER REV NO. 3 OF 3 2016 - 001 - 00 NARRATIVE NRC FORM 366A (01-2014) LICENSEE EVENT REPORT (LER) CONTINUATION SHEET Cause of the Event
The direct cause of the event was a circuit wiring design error that was implemented in the field and caused energization of the RRP ASD trip coils.
The root cause of the event was a failure of station personnel to appropriately apply THU error prevention techniques to identify the design error and prevent its installation and testing as part of the modification.
Corrective Actions Completed The isolation switch for the mis-wired circuit was opened to enable reset of the ASD trip coils.
The 2A and 2B ASDs were returned to service.
Corrective Actions Planned
The wiring design error will be corrected and the Modification Acceptance Test will be revised to ensure the change is correctly tested per the requirements of the Acceptance Test Criteria.
The human performance aspects of the event will be addressed through several management actions that include reinforcement of proper standards and behaviors related to THU error techniques with station personnel.
Previous Similar Occurrences
There was no previous RPS actuation in the past five years due to modification testing.
Component data
System: AD Reactor Recirculation System Component: P Pump Component number: 2A-P201-DR Component name: Reactor Recirculation Pump Manufacturer: G080 General Electric Company Model number: 5K46385AA1