ML18086A293

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LER 81-029/03L-0:on 810314,diesel Generator 1A Declared Inoperable During Surveillance Test.Caused by Erratic Governor Control Preventing Generator Load from Reaching Required Level & Procedural Inadequacy.Insp Orders Issued
ML18086A293
Person / Time
Site: Salem PSEG icon.png
Issue date: 04/09/1981
From: Steele W
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18086A292 List:
References
LER-81-029-03L, NUDOCS 8104240513
Download: ML18086A293 (1)


Text

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION

... -LICENSEE EVENT REPORT CONTROL 1 6 (PLEASE PF.::\IT OR TYPE ALL REQUIRED INFORMATION) r£:El IN IJ Is I GI sl1 101 oj ol -1 ol ol ol ol ol I 1l 1l 1l 1101 I IG) 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT 58 CON'T ITEJ 7 8 UJ©I ol s I o Io I o I 2 I 1 I 2 IG)I o I 3 I 1 I 4 I s j 1 l©I o I 4 I o I 9 I a I iJ G) 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

!During normal operation while performing Surveillance Test SP(O) 4.8.1.1.2, Diesel J **.i' [£]:IJ f Generator lA was declared inoperable because erratic governor control prevented the [QJ:IJ 1raising of the generator load to > 1400 KW as required by the surveillance test. [£}]] !Investigation revealed that the governor oil system was approximately one quart low. [[I[] jOil was added and a satisfactory surveillance test completed.

Action Statement

[EJ2] 13.8.1.1.b was entered at 0210 hours0.00243 days <br />0.0583 hours <br />3.472222e-4 weeks <br />7.9905e-5 months <br /> and terminated at 1048 hours0.0121 days <br />0.291 hours <br />0.00173 weeks <br />3.98764e-4 months <br />. [TI]] I 7 8 9 80 ITTIJ 7 8 SYSTEM CODE IE IE I@ 9 10 CAUSE CAUSE CODE SUB CODE COMPONENT CODE l£...J@ UJ@ IE IN I GI I IN IE I@ 11 12 13 18 SEQUENTIAL OCCURRENCE

@ LE R RO CVENT REPORT NO. CODE I 8 I 1 I I I I 0 I 2 I 9 I I ....... , I 0 I 3 I 21 22 23 24 26 27 28 29 COMP. SUB CODE l..Ll@ 19 RE FORT TYPE 30 VALVE SUBCOOE Llj@ 20 1=J 31 ACTION FUTURE ACTION EFFECT SHUTDOWN r,;::;.. ATTACHMENT NPRD-4 ON PLANT METHOD HOURS SUBMITTED FORM ::.UB. PRIME COMP. SUPPLIER Ll..J@ I 01010101 L!J@ 33 34 35 36 37 40 41 42 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS@ 43 REVIS I Of\. NC. L£J 32 COMPOfl:Efl:T MANUFACTURER I A 11 1 s 12 I@ 44 47 IHeretofore.

no procedure existed which directed the operators to check the governor [III] loil sump level on a routine basis. Inspection Orders IO 100733 (Unit 1) and IO 100734 r::IILJ !(Unit 2) have been issued which require operator personnel to check the governor [JJ]J !oil sump levels on all diesel generators monthly. cmJ 7 8 9 FACILITY ljQ\ STATUS % POWER OTHER STATUS \:::::J [i]I) LE.j@ Ill OI Oj@._I __ N....:..../A

__ _ BO METHOD OF DISCOVERY DESCRIPTION

@ DISCOVERY l::..J@I Operator Observation 8 9 10 12 1'3 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF Em Ll.J @ W@I N/A 7 8 9 10 11 7 44 45 46 so LOCATION OF RELEASE @ N/A 44 45 80 PERSONNEL EXPOSURES r:;;:;-..

NUMBER (:;':;\TYPE DESCRIPTION IIEJ I 0 I 0 I 0 lL!.j@......_

__ ,.:.:.Nc....:A..:....-

____________________

__, 7 8 9 11 12 13 80 PERSONNEL INJURIES /;";\ NUMBER DESCRIPTION6 ol ol

____________________

__,. 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY '4J\ TYPE DESCRIPTION EEi W@ NA 1 e 9 PUBLICITY [ill] ISSUED@DESCRIPTION NRC USE ON Ly ., I ... , I I I I I I :;,._*

I I I I I I I I I .. 7 88 91 0 4 2° ( 0 5 1 3 68 69 80 ;;. NAM 0 W. J. Steele 609-935-0998 ILo E