ML17252A275

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Transmittal of Reportable Occurrence Report No. 50-249/1977-4
ML17252A275
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 03/23/1977
From: Stephenson B
Commonwealth Edison Co
To: James Keppler
NRC/RGN-III
References
50-249/1977-4
Download: ML17252A275 (3)


See also: IR 05000249/2019077

Text

8' Commonw.A.

Edison Dresden

Station R.R. #1 Morris, Illinois 60450 Telephone

815/942-2920

BBS Ltr. #77-239 March 23, 1977 Mr. James G. Keppler, Regional Director Directorate

of Regulatory

Operations

-Region I I I U. S. Nuclear Regulatory

Commission

799 Roosevelt

Road Glen Ellyn, Illinois 60137 (nclosed please find Reportable.

Occurrence

report number 50-249/1977-4.

This repo{t is being

to your office in

with the Dresden Nuclear Power Station Technical

Specifications, Section 6.6.B. BBS: j o Enclosure

cc: Director of Inspection

& Enforcement

Director of Management

Information

& Program Cohtrol Fi le/NRC MAR 2 5 1977

LICENSEE EVENT REPORT CONtROL BLOCK: l ,,, 1 e I I I I I.** LsE PRINT AU REQUIRED 1NFORMA.T10NJ

LICENSEE NAME . 6 LICENSE NUMBER UC EN SE TYPE ILlolRlsl3I

I o I o 1-1 o I o I o I o I ol -1 o I o I l 4 I I I 1 I 1 I 1 I 7 8 9 14 15 25 26 30 .

CATEGORY TYPE. SOURCE @mcoN'T I I . L!:J lJ:J 7 . 8 57. 58 '. _59 60 OOCKET NUMBER I o I s I o I _:_ I o 1-2 I 4 l 9 I 61 68 . EVENT OA TE . I o I 21 21 11 71 '71 69 74 EVENT DESCRIPTION

  • * -* EVENT TYPE Io I 3 I 31 REPORT DATE 1013121317171

75 80* fol2l

__

__

__ s_t_e_a_m_l_t_i_n_e

__

__ i_s_o_l_a_t_i_o_n

__ s_w_i_t_c_h

____ __JI 7 . 8 9 80 lol3I

__

__ w_a_s __ f_o_u_n_d

__

__

__

__

__

____ __JI 7 *8 9 80

10151,J I ine would have provided the required isolation

had.an _anGal high-flow

con-:-l 7* .8 (Q]§J .. ___ . _d_i_t_io_n

__ o_c_c_u_r_r_e_d_.

___ T_h_i_s __ i._s __

__ o_c_c_u_r_r_e_n_ce

__ * ___


11

7 8 9 PRIME . 80 SYSTEM CODE' @£] 1*c1 ol FACILITY STATUS fill] Ll.J 7 .8 9 FORM OF' ACTIVITY*

  • rn RELEASED LzJ 7 8 9 PERSONNEL " POWER OTHER STATUS IQ I 4 I 3 I 10 12 13 CONTENT OF RELEASE AMOUNT OF ACTIVITY W . I 10 11 EXPOSURES
  • NUMBER TYPE OESCRIPTION I ol ol ol L1J N 7 8 9 11 12 13 PERS'ONNEL

INJURIES NUMBER OESCRIPTION

COMPONENT

SUPPLIER COMPONENT

MANUFACTURER

w I BI 0 I 8 I 0 I 43 44 47 METHOD OF DISCOVERY

I I 44 45 46 NA \/10LATl)N

I tY1 I 48 * LOCATION OF RELEASE 80 I, ... 44".,,: 45

..... -* _ _,_... ___________

___,I .. w. 80 80 ITEJ lol ol ol* 7 8 9* 11 12 BO OFFSITE. CONSEQUENCES . EE NA 7 8 9 ao LOSS OR DAMAGE .. TO FACILITY . TYPE OESCRIPTION . (Ifilll.J

.,__ ___ N_A _________________________________

__,_ __________

...__....__

__ 7 8 9 10 80 PUBLICITY . EfZl *-NA 7 B 9"-------.:.:.:..:--.-...;.

____________________________

_,.. __________________________________

ADDITIONAL

FACTORS NA 7 8 9 80 ..

__ --____

_______________

PHONE: __ E_x_t_._42

........ 1. --GPO 811t*eG7

CAUSE DESCRIPTION (Continued)

It is believed that the water originated

from a leaking area cooler (Which has since been repaired)

located above the

box. The switch was cleaned and reset to trip at the correct setpoint.

In addition, the cable

the junction box was sealed. tion of the hearby switches indicated

that water

was limited to this

switch. DPIS 3-261-26 is a Barton model 278 unit with a range of 0 -200 psig.