ML18038B386

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LER 95-002-00:on 950710,DG 3D Auto Started Due to Personnel Error.Work Was Stopped & DGs Shut Down
ML18038B386
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 08/04/1995
From: JONES W C
TENNESSEE VALLEY AUTHORITY
To:
Shared Package
ML18038B385 List:
References
LER-95-002-03, LER-95-2-3, NUDOCS 9508100319
Download: ML18038B386 (10)


Text

NRC FORH 366 (5-92).S.NUCLEAR REGULATORY C(sall SSION ROVED BY (NB NO.3150-0104 EXPIRES 5/31/95 LICENSEE EVENT REPORT (LER)'(See reverse for required nutter of digits/characters for each block)ESTIHATED BURDEN PER RESPONSE.TO COMPLY HITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS~FORNARD COMHEHTS REGARDING BURDEN ESTIHATE TO THE IMFORHATIOH AMD RECORDS MAMAGEHEHT BRANCH (MMBB 7714)~U.ST NUCLEAR REGULATORY COHHISSIOH, NASHIHGTOH, DC 20555 0001 AMD TO THE PAPERMORK REDUCTION PROJECT (3140 0104), OFFICE OF HAMAGEHEMT AMD BUDGET UASHIMGTOM DC 20503.FACILITY NAHE (1)Browns Ferry Nuclear Plant (BFN)Unit 3 DOCKET INNER (2)05000296 PAGE (3)1OFS TITLE (4)DIESEL GENERATOR AUTO START DUE TO PERSONNEL ERROR EVENT DATE 5 LER IRNBER 6 REP(NIT DATE 7 OTHER FACILITIES INVOLVED 8 HOMTH 07 DAY 10 YEAR 95 YEAR.95 SEQUENT I AL HUHBER 002 REVISION MUHBER 00 HOMTH DAY 08 04 FACILITY NAHE YEAR NA FACILITY MAHE NA DOCKET HUHBER DOCKET MUHBER OPERATING M(X)E (9)N THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR: Check.one or more 11 20.405(c)X 50.73(a)(2)(iv) 20.402(b)73.71(b)POMER LEVEL (10)000 20.405(a)(1)(i) 20.405(a)(1)(ii) 20.405(a)(1)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii)

LICEMSEE C(NITACT FOR THIS LER 12 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x) 73.71 (c)OTHER (Specify in Abstract below and in Text, MRC Form 366A NAHE William C.Jones, Compliance Licensing Engineer TELEPHONE MUHBER (Include Area Code)(205)729-7857 DNPLETE ONE LINE FOR EACH CXNPONENT FAILURE DESCRIBED IN THIS REP(NIT 13 CAUSE SYS TEH COMPONENT HAMUFACTURER REPORTABLE TO NPRDS CAUSE SYSTEH COMPONENT MANUFACTURER REPORTABLE TO MPRDS SUPPLHKNTAL REPORT EXPECTED 14 YES (If yes, complete EXPECTED SUBHISSIOH DATE).<XV<p~ig.'.

EXPECTED SUBMISSION DATE (15)HOMTH DAY'EAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)(16)On July 10, 1995, at 1446 hours0.0167 days <br />0.402 hours <br />0.00239 weeks <br />5.50203e-4 months <br />, diesel generator (DG)3D auto started, and at approximately 1447 hours0.0167 days <br />0.402 hours <br />0.00239 weeks <br />5.505835e-4 months <br />, DGs 3A, 3B, and 3C auto started during the performance of wire lifts conducted to facilitate testing of the Emergency Core Cooling System logic.During the wire lifts, an electri.cian shorted two relay terminals with a pair of pliers.At the time of this event, Unit 3 was defueled and in a long-term outage.Unit 2 was operating at 100 percent power, and Unit 1 was shutdown and defueled.This event was caused by personnel error due to inattention to detail.The electrician performing the wire lift failed to take proper precautions while working on energized equipment (e.g.,tape ad)acent terminals, tape tools).Subsequent to the event the DGs were shutdown and returned to standby readiness.

This report is submitted in accordance with 10 CFR 50.73 (a)(2)(iv) as a condition that resulted in automatic actuation of an Engineered Safety Feature (ESF).MRC FORM ()'P508100319 95080J)PDR ADOCK 05000296 8 PDR 4l NRC FORII 366A (5-92)U.S.NUCLEAR REGULATORY COMMISSI OH LICENSEE EVENT REPORT TEXT CONTINUATION APPROVED BY QGI NO.3150-0104.EXP I RES-5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0'RS.FORWARD COMMENTS REGARDING BURDEH ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S.NUCLEAR REGULATORY COMMISSION,'WASHINGTON, DC 20555-0001, AHD TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGENENT AHD BUDGET, WASHINGTON DC 20503 FACILITY NAME (1)DOCKET NUMBER (2)LER NINIBER (6)YEAR SEQUENTIAL REVISION NUHBER NUMBER PAGE (3)Browns Ferry Unit 3 05000296 95 002 00 2 of 5 TEX'I If more s ce is r uired use additional co ies of NRC Form 366A (17)I~PLANT CONDITIONS At the time this event occurred, Unit 3 and Unit 1 were shutdown and defueled.Unit 2 was at 100 percent power.DESCRIPTION OF EVENT A.Event At 1446 hours0.0167 days <br />0.402 hours <br />0.00239 weeks <br />5.50203e-4 months <br /> Central Standard Time (CST)on July 10, 1995/diesel'enerator (DG)3D (EK)auto started during the performance of wire lifts conducted to facilitate testing of the Emergency Core Cooling System Logic[JE).The event occurred when an electrician (contractor, non-licensed) was performing a wire lift on a relay[RLY)terminal and the electrician's pliers came in contact with an adjacent terminal.The initial contact caused partial closure of the relay contacts resulting in the auto start of the 3D DG.At 1447 hours0.0167 days <br />0.402 hours <br />0.00239 weeks <br />5.505835e-4 months <br /> CST, the pliers again contacted the adjacent terminal causing complete closure of the relay contacts resulting in the auto start of the 3A, 3B, and 3C DGs.The Assistant Shift Operations Supervisor (ASOS)(utility, licensed)immediately notified personnel in the Auxiliary Instrument Room to stop activities associated with the wire lifts.At 1523 hours0.0176 days <br />0.423 hours <br />0.00252 weeks <br />5.795015e-4 months <br /> the DGs were shutdown and returned to standby readiness.

This event is reportable in accordance with 10 CFR 50.73 (a)(2)(iv) as a condition that resulted in an automatic actuation of an ESF.B.Co Ino erable Structures Com onents or S stems that Contributed to the Event: None.Dates and A roximate Times of Ma or Occurrences:

July 10, 1995 at 1446 hours0.0167 days <br />0.402 hours <br />0.00239 weeks <br />5.50203e-4 months <br /> CST at 1447 hours0.0167 days <br />0.402 hours <br />0.00239 weeks <br />5.505835e-4 months <br /> CST at 1523 hours0.0176 days <br />0.423 hours <br />0.00252 weeks <br />5.795015e-4 months <br /> CST 3D DG auto started 3A, 3B,&3C DG auto started Unit 3 DGs shutdown and returned to standby readiness

NRC FORM 366A (5-92)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT TEXT'ONTINUATION APPROVED BY (His NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTIOH REQUEST: 50.0 HRS~FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S.NUCLEAR REGULATORY COMMISSION/

WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTIOH PROJECT (3150-0104), OFFICE OF MANAGEMENT AHD BUDGETS WASHINGTON DC 20503 FACILITY NAME (1)DOCKET NIH(BER (2)LER NQ(BER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER PAGE (3)Browns Ferry Unit 3 05000296 95 002 00 3 of 5 TEXT lf more s ce is re uired use additional co ies of NRC Form 366A (17)at 1607 hours0.0186 days <br />0.446 hours <br />0.00266 weeks <br />6.114635e-4 months <br /> CST TVA provided a 10 CFR 50.72 (b)(2)(ii) notification to NRC Operations Center D~E~Other S stems or Secondar Functions Af fected: None.Method of Discover F~'Thi's condition was discovered when the Unit Operator (UO)(utility, licensed]received alarms (ALM)and indicators that the 3A, 3B, 3C, and 3D DGs had auto started.0 erator Actions: When the UO observed the alarms, the ASOS immediately notified personnel in the Auxiliary Instrument'oom to stop activities associated with the wire lift.G~Safet S stem Res onses: The safety systems responded as designed for this type of event.CAUSE OF THE EVENT A.Immediate Cause: The immediate cause of the event was the inadvertent contact of pliers between two relay terminals.

This short simulated an accident signal resulting in the auto start of the Unit 3 DGs.B~Root Cause: C~The cause of this event was personnel error due to inattention to detail.During the performance of a wire lift on a relay in an electrical panel, the electrician's pliers inadvertently contacted an adjacent terminal.Although the area inside the electrical panel was cramped, the electrician should have taken additional precautions while working on energized equipment (e.g., tape adjacent terminals, tape tools): Contributin Factors: None.

0 NRC FORH 366A (5-92)LICENSEE EVENT REPORT TEXT CONTINUATION FACILITY NAHE (1)DOCKET N(MBER (2)U.S.NUCLEAR REGULATORY COMHISSIOH APPROVED BY (NQ NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEH PER RESPONSE TO COHPLY WITH THIS INFORHATIOH COLLECTION REOUEST: 50.0 HRS.FORWARD CONHENTS REGARDIHG BURDEN EST IHATE TO THE INFORHAT I ON AND RECORDS NANAGEHEHT BRANCH (MNBB 7714), U.S.NUCLEAR REGULATORY CONHISSION

~WASHINGTON, DC 20555-0001, AND TO,THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF HANAGENENT AND BUDGETS'WASHINGTON DC 20503 PAGE (3)LER NQIBER (6)Browns Ferry Unit 3 05000296'YEAR 95 SEQUENTIAL NUHBER 002 REVISION NUHBER 00 4 of 5 TEXT If more s ace is r uired use additional co ies of'NRC Form 366A (17)IV.ANALYSIS OF THE EVENT The DGs are designed to auto start when an accident signal is received.In"this event, the auto start of the DGs was a successful completion of the designed function.Operations personnel immediately identified the cause of the ESF actuation and took appropriate corrective actions to restore the DGs to standby readiness.

Therefore, this event did not affect the health and safety of plant ,personnel or the public.V~CORRECTIVE ACTIONS A~Immediate Corrective Actions: B~The work was stopped and the DGs were shutdown.Corrective Actions to Prevent Recurrence:

The electrician was counseled to further emphasize the need to take necessary precautions when working on energized equipment and to develop a questioning attitude prior to performing work.VI., ADDITIONAL INFORMATION A.Failed Com onents: B.None.Previous LERs on Similar Events: There have been several LERs written to document unplanned DG autostarts.

Three of these LERs (i.e., 259/89014, 259/91004/

and 296/91003) occurred as a result of personnel error.In LER 259/89014, the individual allowed a wire to contact another energized, terminal during performance of an SI.The corrective action was to revise the SI to include a precautionary note to insulate adjacent terminals prior to lifting wires.

4l I NRC FORM 366A (5-92)U.S NUCLEAR REGULATORY COIOIISSIOH LICENSEE EVENT REPORT TEXT CONTINUATION APPROVED BY CKB NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS IHFORHATION, COLLECTION REQUEST: 50.0 MRS'ORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 771C), U.S.NUCLEAR REGULATORY COMMISSIOH, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150 0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON DC 20503 FACILITY NAME (1)DOCKET NINBER'(2)LER NWER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER PAGE (3)Browns Ferry'Unit 3 05000296 95 002 00 5 of 5 TEXT If more s ace is re ired use additionaI co ies of HRC Form 366A (17)In LER 259/91004, the individual placed the wrong keylock switch in the test position.The corrective actions were to install larger identification labels to assist individuals in identifying the correct component.

In LER 296/91003, the individual did not properly install an inhibiting boot during the performance of an SI.The corrective actions were to train.maintenance personnel on the proper installation of boots.Only LER 296/91003 is similar to this event.However, the previous corrective actions for this LER would not have precluded this event.VI I~COMMITMENTS None.Energy Industry Identification System (EIIS)system and component codes are identified in the text with brackets (e.g.,[XX].

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