Information Notice 2016-07, Operating Experience Regarding Impacts on Site Electrical Power Distribution from Inadequate Oversight of Contractor Activities: Difference between revisions
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{{#Wiki_filter:UNITED STATES | {{#Wiki_filter:ML16057A842 | ||
UNITED STATES | |||
NUCLEAR REGULATORY COMMISSION | NUCLEAR REGULATORY COMMISSION | ||
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OFFICE OF NEW REACTORS | OFFICE OF NEW REACTORS | ||
WASHINGTON, DC 20555-0001 June 20, 2016 NRC INFORMATION NOTICE 2016-07: | WASHINGTON, DC 20555-0001 | ||
June 20, 2016 | |||
NRC INFORMATION NOTICE 2016-07: | |||
OPERATING EXPERIENCE REGARDING | |||
IMPACTS ON SITE ELECTRICAL POWER | IMPACTS ON SITE ELECTRICAL POWER | ||
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addressees of adverse effects to off-site power availability that have resulted from inadequate | addressees of adverse effects to off-site power availability that have resulted from inadequate | ||
licensee oversight of contractor activities. It is expected that recipients will review the | licensee oversight of contractor activities. It is expected that recipients will review the | ||
information for applicability to their facilities and consider actions, as appropriate, to avoid | information for applicability to their facilities and consider actions, as appropriate, to avoid | ||
similar problems. However, suggestions contained in this IN are not NRC requirements; | similar problems. However, suggestions contained in this IN are not NRC requirements; | ||
therefore, no specific action or written response is required. | therefore, no specific action or written response is required. | ||
==DESCRIPTION OF CIRCUMSTANCES== | ==DESCRIPTION OF CIRCUMSTANCES== | ||
Wolf Creek Generating Station, Unit 1 | |||
On January 13, 2012, Wolf Creek Generating Station (Wolf Creek) experienced an automatic | On January 13, 2012, Wolf Creek Generating Station (Wolf Creek) experienced an automatic | ||
reactor trip after the catastrophic failure of the main generator output breaker. The start-up | reactor trip after the catastrophic failure of the main generator output breaker. The start-up | ||
transformer assumed nonsafety-related loads, but subsequently experienced a differential relay | transformer assumed nonsafety-related loads, but subsequently experienced a differential relay | ||
actuation on its B phase. This caused a lockout of the start-up transformer and a loss of | actuation on its B phase. This caused a lockout of the start-up transformer and a loss of | ||
off-site power (LOOP). Both emergency diesel generators started and supplied power to the | off-site power (LOOP). Both emergency diesel generators started and supplied power to the | ||
safety-related 4160 volt busses as expected. | safety-related 4160 volt busses as expected. | ||
The LOOP resulted in several complications, including: | The LOOP resulted in several complications, including: | ||
* | |||
erratic source range nuclear instrumentation indications resulting from the loss of power | |||
to containment cavity cooling fans * | |||
containment sump high level alarms caused by a through-wall leak in essential service | |||
water (ESW) piping in containment resulting from a known issue with water hammer | water (ESW) piping in containment resulting from a known issue with water hammer | ||
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caused by the stop-start sequence of ESW pumps following a LOOP | caused by the stop-start sequence of ESW pumps following a LOOP | ||
* | * | ||
a loss of firefighting capability for 4 hours because of the loss of power to normal fire | |||
pumps in conjunction with the long-term inoperability of the installed diesel-powered fire | pumps in conjunction with the long-term inoperability of the installed diesel-powered fire | ||
| Line 85: | Line 94: | ||
pump and inadequacies with the procedure for starting a temporary fire pump | pump and inadequacies with the procedure for starting a temporary fire pump | ||
* | * | ||
a loss of reactor coolant pumps necessitating a natural circulation cooldown, and | |||
* | * | ||
a loss of instrument air complicating operator control of pressurizer level and pressure | |||
The cause of the LOOP was the actuation of protective relaying resulting from a short between | The cause of the LOOP was the actuation of protective relaying resulting from a short between | ||
two taps on the high side current transformers. During the previous year, the licensee had | two taps on the high side current transformers. During the previous year, the licensee had | ||
contracted with a vendor to replace electrical seal assemblies in the start-up transformer that | contracted with a vendor to replace electrical seal assemblies in the start-up transformer that | ||
experienced oil leakage. This vendor performed the majority of the work in accordance with | experienced oil leakage. This vendor performed the majority of the work in accordance with | ||
established instructions and practices, but failed to install insulating sleeves on 2 of the 37 wiring connections. These sleeves are required to prevent terminal-to-terminal contact. The | established instructions and practices, but failed to install insulating sleeves on 2 of the 37 wiring connections. These sleeves are required to prevent terminal-to-terminal contact. The | ||
investigation that followed determined that the licensee failed to satisfy the requirements of | investigation that followed determined that the licensee failed to satisfy the requirements of | ||
| Line 105: | Line 116: | ||
verification of contracted work was conducted to verify that it was performed in accordance with | verification of contracted work was conducted to verify that it was performed in accordance with | ||
applicable work orders. After the event, the licensee installed the missing insulation sleeves, and updated station procedures regarding the oversight of contractors performing work on | applicable work orders. After the event, the licensee installed the missing insulation sleeves, and updated station procedures regarding the oversight of contractors performing work on | ||
risk-significant components. | risk-significant components. | ||
This IN provides no new information on this event. The condition described was summarized | This IN provides no new information on this event. The condition described was summarized | ||
from previously-released reports prepared by an NRC Augmented Inspection Team (AIT) | from previously-released reports prepared by an NRC Augmented Inspection Team (AIT) | ||
chartered shortly after the event in 2012 to review the facts surrounding the LOOP, and the | chartered shortly after the event in 2012 to review the facts surrounding the LOOP, and the | ||
complications that resulted. Additional information can be found in Licensee Event Report | complications that resulted. Additional information can be found in Licensee Event Report | ||
05000482/2012-001, Failure of 345 kV Switchyard Breaker due to Internal Fault Resulting in | 05000482/2012-001, Failure of 345 kV Switchyard Breaker due to Internal Fault Resulting in | ||
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System (ADAMS) Accession Nos. ML12109A049, ML12095A414, and ML12227A919, respectively). | System (ADAMS) Accession Nos. ML12109A049, ML12095A414, and ML12227A919, respectively). | ||
Arkansas Nuclear One, Unit 1 and Unit 2 | |||
On March 31, 2013, at Arkansas Nuclear One (ANO) during its Unit 1 outage, an inadequately | On March 31, 2013, at Arkansas Nuclear One (ANO) during its Unit 1 outage, an inadequately | ||
designed temporary lifting rig failed while moving the Unit 1 main generator stator out of the | designed temporary lifting rig failed while moving the Unit 1 main generator stator out of the | ||
turbine building. The 525-ton stator fell onto the turbine deck and then continued falling | turbine building. The 525-ton stator fell onto the turbine deck and then continued falling | ||
approximately 30 feet into a train bay that is shared between Units 1 and 2. The collapse of the | approximately 30 feet into a train bay that is shared between Units 1 and 2. The collapse of the | ||
lifting rig resulted in one fatality and injured eight others. The impact of the dropped stator on | lifting rig resulted in one fatality and injured eight others. The impact of the dropped stator on | ||
the turbine deck damaged the Unit 1 non-vital electrical switchgear connecting plant vital busses | the turbine deck damaged the Unit 1 non-vital electrical switchgear connecting plant vital busses | ||
| Line 143: | Line 155: | ||
to off-site power, causing a LOOP to Unit 1 for six days. | to off-site power, causing a LOOP to Unit 1 for six days. | ||
At the time of the event, Unit 2 was operating at 100 percent power. Vibrations from the stator | At the time of the event, Unit 2 was operating at 100 percent power. Vibrations from the stator | ||
drop and temporary lift rig collapse caused a Unit 2 reactor coolant pump breaker to trip, resulting in an automatic reactor trip of Unit 2. Water spray from a ruptured fire water pipe migrated into the ANO-2 non-vital switchgear area located just off the train bay causing an | drop and temporary lift rig collapse caused a Unit 2 reactor coolant pump breaker to trip, resulting in an automatic reactor trip of Unit 2. Water spray from a ruptured fire water pipe migrated into the ANO-2 non-vital switchgear area located just off the train bay causing an | ||
electrical fault inside the non-vital Unit 2 electrical switchgear approximately 90 minutes after the | electrical fault inside the non-vital Unit 2 electrical switchgear approximately 90 minutes after the | ||
stator drop. This fault caused a lockout of start-up transformer 3 and a partial LOOP for Unit 2. | stator drop. This fault caused a lockout of start-up transformer 3 and a partial LOOP for Unit 2. | ||
Loss of power to all four reactor coolant pumps necessitated a natural circulation plant | Loss of power to all four reactor coolant pumps necessitated a natural circulation plant | ||
| Line 157: | Line 169: | ||
LOOP. | LOOP. | ||
The temporary lifting rig collapse resulted from errors in contractor design calculations. The | The temporary lifting rig collapse resulted from errors in contractor design calculations. The | ||
basic lifting rig design had been used by the contractor for stator lifts at other nuclear power | basic lifting rig design had been used by the contractor for stator lifts at other nuclear power | ||
plants; however, the design of the rig had been modified for use at ANO. The licensee failed to | plants; however, the design of the rig had been modified for use at ANO. The licensee failed to | ||
perform an adequate review of the contractors modified design calculations, and failed to | perform an adequate review of the contractors modified design calculations, and failed to | ||
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require the contractor to perform a load test in accordance with site procedures and applicable | require the contractor to perform a load test in accordance with site procedures and applicable | ||
regulations. These failures were the result of inadequate oversight by the licensee. The | regulations. These failures were the result of inadequate oversight by the licensee. The | ||
licensee repaired the damage to the plant and updated procedures to provide guidance on | licensee repaired the damage to the plant and updated procedures to provide guidance on | ||
| Line 179: | Line 191: | ||
Generator Stator Temporary Lift Assembly Results in a Fatality, Multiple Injuries, a Plant Scram, a Notification of Unusual Event, and Dual Unit Structural Damage, dated August 22, 2013 (ADAMS Accession No. ML12109A049). | Generator Stator Temporary Lift Assembly Results in a Fatality, Multiple Injuries, a Plant Scram, a Notification of Unusual Event, and Dual Unit Structural Damage, dated August 22, 2013 (ADAMS Accession No. ML12109A049). | ||
Comanche Peak Nuclear Power Plant, Unit 1 and Unit 2 | |||
On December 4, 2013, Comanche Peak Nuclear Power Plant (Comanche Peak) experienced a | On December 4, 2013, Comanche Peak Nuclear Power Plant (Comanche Peak) experienced a | ||
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transformer was mistakenly cut while the other start-up transformer was out of service for | transformer was mistakenly cut while the other start-up transformer was out of service for | ||
modifications. Both units remained at full power as nonsafety-related loads (including reactor | modifications. Both units remained at full power as nonsafety-related loads (including reactor | ||
coolant pumps) continued to receive power from the main generator through the unit auxiliary | coolant pumps) continued to receive power from the main generator through the unit auxiliary | ||
transformer. All four emergency diesel generators started automatically and re-energized the | transformer. All four emergency diesel generators started automatically and re-energized the | ||
safety-related busses. | safety-related busses. | ||
| Line 196: | Line 209: | ||
Comanche Peak was in the process of implementing a modification to start-up transformer | Comanche Peak was in the process of implementing a modification to start-up transformer | ||
XST-1. In preparation for the work, contract personnel had walked down the cables for XST-1 to ensure the correct cables were identified. However, an incorrect assumption about the layout | XST-1. In preparation for the work, contract personnel had walked down the cables for XST-1 to ensure the correct cables were identified. However, an incorrect assumption about the layout | ||
of the cable bus enclosure routing, combined with a failure to use design drawings to facilitate | of the cable bus enclosure routing, combined with a failure to use design drawings to facilitate | ||
| Line 202: | Line 215: | ||
the walkdown, contributed to the contractors misidentifying a feeder cable for the other start-up | the walkdown, contributed to the contractors misidentifying a feeder cable for the other start-up | ||
transformer, XST-2, rather than the cable for XST-1. The licensee did not validate the resulting | transformer, XST-2, rather than the cable for XST-1. The licensee did not validate the resulting | ||
work plan provided by the contractors. The contract electricians performing the work raised | work plan provided by the contractors. The contract electricians performing the work raised | ||
questions about the accuracy of the cable identification, but failed to pursue the issue, contrary | questions about the accuracy of the cable identification, but failed to pursue the issue, contrary | ||
to station procedures. The licensee repaired the cut cable to restore off-site power, and | to station procedures. The licensee repaired the cut cable to restore off-site power, and | ||
improved procedures regarding the design change development, review, and oversight | improved procedures regarding the design change development, review, and oversight | ||
| Line 222: | Line 235: | ||
Violation, dated August 6, 2014 (ADAMS Accession Nos. ML14043A089 and ML14218A072, respectively). | Violation, dated August 6, 2014 (ADAMS Accession Nos. ML14043A089 and ML14218A072, respectively). | ||
Joseph M. Farley Nuclear Plant, Unit 2 | |||
On October 14, 2014, a lightning strike on a 500kV line caused a partial LOOP to Joseph M. | On October 14, 2014, a lightning strike on a 500kV line caused a partial LOOP to Joseph M. | ||
Farley Nuclear Plant (Farley), Unit 2. A power circuit breaker opened to clear the fault, and | Farley Nuclear Plant (Farley), Unit 2. A power circuit breaker opened to clear the fault, and | ||
experienced an internal fault on the bus side of the main contacts. The high-fault current | experienced an internal fault on the bus side of the main contacts. The high-fault current | ||
exposed a loose connection, creating a high resistance and differential current signal that led to | exposed a loose connection, creating a high resistance and differential current signal that led to | ||
| Line 233: | Line 247: | ||
isolation of the 2B start-up auxiliary transformer (SAT), and a LOOP to its associated B train | isolation of the 2B start-up auxiliary transformer (SAT), and a LOOP to its associated B train | ||
power bus. The 2B emergency diesel generator was out of service at the time for scheduled | power bus. The 2B emergency diesel generator was out of service at the time for scheduled | ||
maintenance, and was unable to assume the B train safety-related loads. One of these loads | maintenance, and was unable to assume the B train safety-related loads. One of these loads | ||
was the B train of component cooling water, which was supplying cooling water to reactor | was the B train of component cooling water, which was supplying cooling water to reactor | ||
coolant pump oil coolers and seal coolers at the time of the event. In accordance with the | coolant pump oil coolers and seal coolers at the time of the event. In accordance with the | ||
abnormal operating procedure for loss of component cooling water, operators inserted a manual | abnormal operating procedure for loss of component cooling water, operators inserted a manual | ||
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The loose connection that caused the isolation of the 2B SAT resulted from improper wiring that | The loose connection that caused the isolation of the 2B SAT resulted from improper wiring that | ||
was introduced during installation of a power circuit breaker 18 months earlier. The breaker | was introduced during installation of a power circuit breaker 18 months earlier. The breaker | ||
installation was part of a design change package for the high-voltage switchyard implemented | installation was part of a design change package for the high-voltage switchyard implemented | ||
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by the grid operator to replace and upgrade several power circuit breakers and their control | by the grid operator to replace and upgrade several power circuit breakers and their control | ||
relay packages. Testing during the implementation verified the correct installation of the current | relay packages. Testing during the implementation verified the correct installation of the current | ||
transformers and associated wiring. However, inadequate verification practices failed to identify | transformers and associated wiring. However, inadequate verification practices failed to identify | ||
a missing nut on one of the terminals during the installation. This led to a loose connection that | a missing nut on one of the terminals during the installation. This led to a loose connection that | ||
was adequate for normal testing and operational purposes, but not for the conditions | was adequate for normal testing and operational purposes, but not for the conditions | ||
experienced during a ground fault isolation. A contributing cause of this event was the | experienced during a ground fault isolation. A contributing cause of this event was the | ||
licensees failure to fully understand the extent of differences in verification practices performed | licensees failure to fully understand the extent of differences in verification practices performed | ||
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The missing nut on the power circuit breaker current transformer was installed, and the | The missing nut on the power circuit breaker current transformer was installed, and the | ||
transformer primary and secondary protective relaying functions were tested satisfactorily. In | transformer primary and secondary protective relaying functions were tested satisfactorily. In | ||
addition, the licensee worked to strengthen the application of verification procedures used by | addition, the licensee worked to strengthen the application of verification procedures used by | ||
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==DISCUSSION== | ==DISCUSSION== | ||
Licensees often rely on contractors and supplemental personnel to perform work. This is | Licensees often rely on contractors and supplemental personnel to perform work. This is | ||
especially the case during scheduled outages. This work includes specialized, low-frequency | especially the case during scheduled outages. This work includes specialized, low-frequency | ||
tasks involving one-time modifications or the overhaul of major equipment. The NRC has | tasks involving one-time modifications or the overhaul of major equipment. The NRC has | ||
previously issued several other INs regarding contractor oversight issues, such as IN 97-74, Inadequate Oversight of Contractors During Sealant Injection Activities, and IN 00-11, Licensee Responsibility for Quality Assurance Oversight of Contractor Activities Regarding | previously issued several other INs regarding contractor oversight issues, such as IN 97-74, Inadequate Oversight of Contractors During Sealant Injection Activities, and IN 00-11, Licensee Responsibility for Quality Assurance Oversight of Contractor Activities Regarding | ||
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assurance expectations of plant process controls and, for safety-related equipment, the | assurance expectations of plant process controls and, for safety-related equipment, the | ||
requirements of the plants NRC-approved quality assurance program. While the work activities | requirements of the plants NRC-approved quality assurance program. While the work activities | ||
discussed in this IN were associated with non-safety related equipment, each event placed the | discussed in this IN were associated with non-safety related equipment, each event placed the | ||
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Industry operating experience has shown the importance of licensee programs designed to | Industry operating experience has shown the importance of licensee programs designed to | ||
ensure effective station oversight of contractor activities. Establishing clear lines of | ensure effective station oversight of contractor activities. Establishing clear lines of | ||
accountability within the licensee organization that maintains sufficient knowledge and technical | accountability within the licensee organization that maintains sufficient knowledge and technical | ||
expertise to exercise an appropriate level of oversight of the design, maintenance, modification, or refurbishment activities performed by contracted personnel is essential. This includes | expertise to exercise an appropriate level of oversight of the design, maintenance, modification, or refurbishment activities performed by contracted personnel is essential. This includes | ||
verification that procedures and work instructions contain sufficient detail, and that supplemental | verification that procedures and work instructions contain sufficient detail, and that supplemental | ||
| Line 319: | Line 333: | ||
==CONTACT== | ==CONTACT== | ||
This IN requires no specific action or written response. Please direct any questions about this | This IN requires no specific action or written response. Please direct any questions about this | ||
matter to the technical contacts listed below, or the appropriate Office of Nuclear Reactor | matter to the technical contacts listed below, or the appropriate Office of Nuclear Reactor | ||
| Line 325: | Line 339: | ||
Regulation (NRR) project manager. | Regulation (NRR) project manager. | ||
/ra/ | /ra/ | ||
Michael C. Cheok, Director | |||
/ra/ | |||
Michael C. Cheok, Director | |||
Louise Lund, Director | |||
Division of Construction Inspection | |||
Division of Policy and Rulemaking | |||
and Operational Programs | |||
Office of Nuclear Reactor Regulation | |||
Office of New Reactors | |||
Technical Contacts: Rebecca Sigmon, NRR | |||
Jesse Robles, NRR | |||
301-415-0895 | |||
301-415-2940 | |||
E-mail: Rebecca.Sigmon@nrc.gov E-mail: Jesse.Robles@nrc.gov | |||
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under NRC Library. | |||
ML16057A842 *via email | |||
TAC: MF7293 OFFICE | |||
TECH EDITOR | |||
NRR/DIRS/IOEB/TL | |||
NRR/DIRS/IOEB/TL | |||
NRR/DE/EEEB/BC | |||
NRR/DIRS/IOEB/BC | |||
NAME | |||
JDougherty* | |||
RSigmon* | |||
JRobles* | |||
JZimmerman* | |||
HChernoff* | |||
DATE | |||
03/11/2016 | |||
05/16/2016 | |||
05/18/2016 | |||
05/25/2016 | |||
05/18/2016 OFFICE | |||
NRR/DIRS/D | |||
NRR/DPR/PGCB/PM | |||
NRR/DPR/PGCB/LA | |||
NRR/DPR/PGCB/BC | |||
NRO/DCIP/D | |||
NAME | |||
SMorris* | |||
ASchwab* | |||
ELee* | |||
SStuchell* | |||
MCheok | |||
DATE | |||
05/27/2016 | |||
05/27/2016 | |||
05/31/2016 | |||
05/31/2016 | |||
06/20/2016 OFFICE | |||
NRR/DPR/D | |||
NAME | NAME | ||
LLund | |||
DATE | DATE | ||
06/20/2016}} | |||
{{Information notice-Nav}} | {{Information notice-Nav}} | ||
Latest revision as of 02:42, 10 January 2025
| ML16057A842 | |
| Person / Time | |
|---|---|
| Issue date: | 06/20/2016 |
| From: | Michael Cheok, Louise Lund Division of Construction Inspection and Operational Programs, Generic Communications Projects Branch |
| To: | |
| Schwab A | |
| References | |
| IN-16-007 | |
| Download: ML16057A842 (6) | |
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
OFFICE OF NEW REACTORS
WASHINGTON, DC 20555-0001
June 20, 2016
NRC INFORMATION NOTICE 2016-07:
OPERATING EXPERIENCE REGARDING
IMPACTS ON SITE ELECTRICAL POWER
DISTRIBUTION FROM INADEQUATE
OVERSIGHT OF CONTRACTOR ACTIVITIES
ADDRESSEES
All holders of an operating license or construction permit for a nuclear power reactor under
Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Domestic Licensing of
Production and Utilization Facilities, except those that have permanently ceased operations
and have certified that fuel has been permanently removed from the reactor vessel.
All holders of and applicants for a power reactor combined license under 10 CFR Part 52, Licenses, Certifications, and Approvals for Nuclear Power Plants.
PURPOSE
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform
addressees of adverse effects to off-site power availability that have resulted from inadequate
licensee oversight of contractor activities. It is expected that recipients will review the
information for applicability to their facilities and consider actions, as appropriate, to avoid
similar problems. However, suggestions contained in this IN are not NRC requirements;
therefore, no specific action or written response is required.
DESCRIPTION OF CIRCUMSTANCES
Wolf Creek Generating Station, Unit 1
On January 13, 2012, Wolf Creek Generating Station (Wolf Creek) experienced an automatic reactor trip after the catastrophic failure of the main generator output breaker. The start-up
transformer assumed nonsafety-related loads, but subsequently experienced a differential relay
actuation on its B phase. This caused a lockout of the start-up transformer and a loss of
off-site power (LOOP). Both emergency diesel generators started and supplied power to the
safety-related 4160 volt busses as expected.
The LOOP resulted in several complications, including:
erratic source range nuclear instrumentation indications resulting from the loss of power
to containment cavity cooling fans *
containment sump high level alarms caused by a through-wall leak in essential service
water (ESW) piping in containment resulting from a known issue with water hammer
caused by the stop-start sequence of ESW pumps following a LOOP
a loss of firefighting capability for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> because of the loss of power to normal fire
pumps in conjunction with the long-term inoperability of the installed diesel-powered fire
pump and inadequacies with the procedure for starting a temporary fire pump
a loss of reactor coolant pumps necessitating a natural circulation cooldown, and
a loss of instrument air complicating operator control of pressurizer level and pressure
The cause of the LOOP was the actuation of protective relaying resulting from a short between
two taps on the high side current transformers. During the previous year, the licensee had
contracted with a vendor to replace electrical seal assemblies in the start-up transformer that
experienced oil leakage. This vendor performed the majority of the work in accordance with
established instructions and practices, but failed to install insulating sleeves on 2 of the 37 wiring connections. These sleeves are required to prevent terminal-to-terminal contact. The
investigation that followed determined that the licensee failed to satisfy the requirements of
written procedures to ensure that (1) field activities were adequately monitored, and (2) periodic
verification of contracted work was conducted to verify that it was performed in accordance with
applicable work orders. After the event, the licensee installed the missing insulation sleeves, and updated station procedures regarding the oversight of contractors performing work on
risk-significant components.
This IN provides no new information on this event. The condition described was summarized
from previously-released reports prepared by an NRC Augmented Inspection Team (AIT)
chartered shortly after the event in 2012 to review the facts surrounding the LOOP, and the
complications that resulted. Additional information can be found in Licensee Event Report
05000482/2012-001, Failure of 345 kV Switchyard Breaker due to Internal Fault Resulting in
Reactor Trip and Coincident Loss of Offsite Power, dated April 9, 2012, in Wolf Creek Nuclear
Operating Corporation-NRC Augmented Inspection Team Report 05000482/2012008, dated
April 4, 2012, and in the NRC Augmented Inspection Team Follow-Up Report
05000482/2012009, dated August 6, 2012 (Agencywide Documents Access and Management
System (ADAMS) Accession Nos. ML12109A049, ML12095A414, and ML12227A919, respectively).
Arkansas Nuclear One, Unit 1 and Unit 2
On March 31, 2013, at Arkansas Nuclear One (ANO) during its Unit 1 outage, an inadequately
designed temporary lifting rig failed while moving the Unit 1 main generator stator out of the
turbine building. The 525-ton stator fell onto the turbine deck and then continued falling
approximately 30 feet into a train bay that is shared between Units 1 and 2. The collapse of the
lifting rig resulted in one fatality and injured eight others. The impact of the dropped stator on
the turbine deck damaged the Unit 1 non-vital electrical switchgear connecting plant vital busses
to off-site power, causing a LOOP to Unit 1 for six days.
At the time of the event, Unit 2 was operating at 100 percent power. Vibrations from the stator
drop and temporary lift rig collapse caused a Unit 2 reactor coolant pump breaker to trip, resulting in an automatic reactor trip of Unit 2. Water spray from a ruptured fire water pipe migrated into the ANO-2 non-vital switchgear area located just off the train bay causing an
electrical fault inside the non-vital Unit 2 electrical switchgear approximately 90 minutes after the
stator drop. This fault caused a lockout of start-up transformer 3 and a partial LOOP for Unit 2.
Loss of power to all four reactor coolant pumps necessitated a natural circulation plant
cooldown, which was complicated by additional equipment unavailability due to the partial
LOOP.
The temporary lifting rig collapse resulted from errors in contractor design calculations. The
basic lifting rig design had been used by the contractor for stator lifts at other nuclear power
plants; however, the design of the rig had been modified for use at ANO. The licensee failed to
perform an adequate review of the contractors modified design calculations, and failed to
require the contractor to perform a load test in accordance with site procedures and applicable
regulations. These failures were the result of inadequate oversight by the licensee. The
licensee repaired the damage to the plant and updated procedures to provide guidance on
review of calculations, quality requirements, and standards associated with third party reviews.
The NRC chartered and dispatched an AIT to review the facts of the event. Additional
information can be found in Licensee Event Report 05000313/2013-001, Collapse of a Main
Generator Stator Temporary Lift Assembly Results in a Fatality, Multiple Injuries, a Plant Scram, a Notification of Unusual Event, and Dual Unit Structural Damage, dated August 22, 2013 (ADAMS Accession No. ML12109A049).
Comanche Peak Nuclear Power Plant, Unit 1 and Unit 2
On December 4, 2013, Comanche Peak Nuclear Power Plant (Comanche Peak) experienced a
LOOP to safety-related busses when an energized cable feeding the in-service start-up
transformer was mistakenly cut while the other start-up transformer was out of service for
modifications. Both units remained at full power as nonsafety-related loads (including reactor
coolant pumps) continued to receive power from the main generator through the unit auxiliary
transformer. All four emergency diesel generators started automatically and re-energized the
safety-related busses.
Comanche Peak was in the process of implementing a modification to start-up transformer
XST-1. In preparation for the work, contract personnel had walked down the cables for XST-1 to ensure the correct cables were identified. However, an incorrect assumption about the layout
of the cable bus enclosure routing, combined with a failure to use design drawings to facilitate
the walkdown, contributed to the contractors misidentifying a feeder cable for the other start-up
transformer, XST-2, rather than the cable for XST-1. The licensee did not validate the resulting
work plan provided by the contractors. The contract electricians performing the work raised
questions about the accuracy of the cable identification, but failed to pursue the issue, contrary
to station procedures. The licensee repaired the cut cable to restore off-site power, and
improved procedures regarding the design change development, review, and oversight
processes.
Additional information can be found in Licensee Event Report 05000445/2013-003, Auto Start
of Both Units' Auxiliary Feedwater Pumps and Emergency Diesel Generators Due to a Loss of
Both Units' Safeguards Electrical Power, dated January 30, 2014 and in Comanche Peak Nuclear Power Plant-NRC Integrated Inspection Report 05000445/2014003 and Notice of
Violation, dated August 6, 2014 (ADAMS Accession Nos. ML14043A089 and ML14218A072, respectively).
Joseph M. Farley Nuclear Plant, Unit 2
On October 14, 2014, a lightning strike on a 500kV line caused a partial LOOP to Joseph M.
Farley Nuclear Plant (Farley), Unit 2. A power circuit breaker opened to clear the fault, and
experienced an internal fault on the bus side of the main contacts. The high-fault current
exposed a loose connection, creating a high resistance and differential current signal that led to
isolation of the 2B start-up auxiliary transformer (SAT), and a LOOP to its associated B train
power bus. The 2B emergency diesel generator was out of service at the time for scheduled
maintenance, and was unable to assume the B train safety-related loads. One of these loads
was the B train of component cooling water, which was supplying cooling water to reactor
coolant pump oil coolers and seal coolers at the time of the event. In accordance with the
abnormal operating procedure for loss of component cooling water, operators inserted a manual
The loose connection that caused the isolation of the 2B SAT resulted from improper wiring that
was introduced during installation of a power circuit breaker 18 months earlier. The breaker
installation was part of a design change package for the high-voltage switchyard implemented
by the grid operator to replace and upgrade several power circuit breakers and their control
relay packages. Testing during the implementation verified the correct installation of the current
transformers and associated wiring. However, inadequate verification practices failed to identify
a missing nut on one of the terminals during the installation. This led to a loose connection that
was adequate for normal testing and operational purposes, but not for the conditions
experienced during a ground fault isolation. A contributing cause of this event was the
licensees failure to fully understand the extent of differences in verification practices performed
by an outside organization.
The missing nut on the power circuit breaker current transformer was installed, and the
transformer primary and secondary protective relaying functions were tested satisfactorily. In
addition, the licensee worked to strengthen the application of verification procedures used by
the utility performing the switchyard maintenance.
Additional information can be found in Licensee Event Report 05000364/2014-002, Manual Reactor Trip due to Loss of 2B [Start-up] Auxiliary Transformer and Loss of Offsite Power, dated December 12, 2014 (ADAMS Accession No. ML14346A391).
DISCUSSION
Licensees often rely on contractors and supplemental personnel to perform work. This is
especially the case during scheduled outages. This work includes specialized, low-frequency
tasks involving one-time modifications or the overhaul of major equipment. The NRC has
previously issued several other INs regarding contractor oversight issues, such as IN 97-74, Inadequate Oversight of Contractors During Sealant Injection Activities, and IN 00-11, Licensee Responsibility for Quality Assurance Oversight of Contractor Activities Regarding
Fabrication and Use of Spent Fuel Storage Cask Systems.
Although the performance of particular tasks, including the development and execution of work
instructions and procedures, may be delegated to outside organizations, the licensee retains overall responsibility for ensuring that the procedures and their execution meet the quality
assurance expectations of plant process controls and, for safety-related equipment, the
requirements of the plants NRC-approved quality assurance program. While the work activities
discussed in this IN were associated with non-safety related equipment, each event placed the
plant in a LOOP condition and challenged the operability and reliability of safety-related
equipment.
Industry operating experience has shown the importance of licensee programs designed to
ensure effective station oversight of contractor activities. Establishing clear lines of
accountability within the licensee organization that maintains sufficient knowledge and technical
expertise to exercise an appropriate level of oversight of the design, maintenance, modification, or refurbishment activities performed by contracted personnel is essential. This includes
verification that procedures and work instructions contain sufficient detail, and that supplemental
personnel are familiar with site work control processes and expectations for procedure
adherence.
CONTACT
This IN requires no specific action or written response. Please direct any questions about this
matter to the technical contacts listed below, or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
/ra/
/ra/
Michael C. Cheok, Director
Louise Lund, Director
Division of Construction Inspection
Division of Policy and Rulemaking
and Operational Programs
Office of Nuclear Reactor Regulation
Office of New Reactors
Technical Contacts: Rebecca Sigmon, NRR
Jesse Robles, NRR
301-415-0895
301-415-2940
E-mail: Rebecca.Sigmon@nrc.gov E-mail: Jesse.Robles@nrc.gov
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under NRC Library.
ML16057A842 *via email
TAC: MF7293 OFFICE
TECH EDITOR
NRR/DIRS/IOEB/TL
NRR/DIRS/IOEB/TL
NRR/DE/EEEB/BC
NRR/DIRS/IOEB/BC
NAME
JDougherty*
RSigmon*
JRobles*
JZimmerman*
HChernoff*
DATE
03/11/2016
05/16/2016
05/18/2016
05/25/2016
05/18/2016 OFFICE
NRR/DIRS/D
NRR/DPR/PGCB/PM
NRR/DPR/PGCB/LA
NRR/DPR/PGCB/BC
NRO/DCIP/D
NAME
SMorris*
ASchwab*
ELee*
SStuchell*
MCheok
DATE
05/27/2016
05/27/2016
05/31/2016
05/31/2016
06/20/2016 OFFICE
NRR/DPR/D
NAME
LLund
DATE
06/20/2016