05000322/LER-1988-017: Difference between revisions

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| document report number = LER-88-017, LER-88-17, NUDOCS 9005240088
| document report number = LER-88-017, LER-88-17, NUDOCS 9005240088
| package number = ML20055C491
| package number = ML20055C491
| document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 4
| page count = 4
}}
}}

Latest revision as of 13:35, 15 March 2020

LER 88-017-01:on 881025,discovered That Seismic Monitoring Instrumentation Returned to Svc Prior to Verifying Sys Operability & Special Rept Not Written.Caused by Personnel Error.Surveillance Engineer Reassigned
ML20055C504
Person / Time
Site: Shoreham File:Long Island Lighting Company icon.png
Issue date: 05/16/1990
From: Schnaars G
LONG ISLAND LIGHTING CO.
To:
Shared Package
ML20055C491 List:
References
LER-88-017, LER-88-17, NUDOCS 9005240088
Download: ML20055C504 (4)


LER-2088-017,
Event date:
Report date:
3222088017R00 - NRC Website

text

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On October 25, 1988, it was discovered that seismic monitoring instrumentation was returned to service prior to completing all cetions necessary for verifying operability as delineated in the curveillance procedure SP 44.655.03, Seismic Monitoring Instramentation Cal, and Funct. Test'. The plant was in Operational Condition 4 with the mode switch in Shutdown and all rods inserted in the core. These instruments are required to be operable at all times per Tech Spec 3.3.7.2. When the instruments were taken out of cervice for calibration, they were required to be returned to cervice within 30 days or the Action Statement would apply. This requires the submittal of a Special Report within 10 days. These instruments were not properly returned to service due to an inadequate review of the test procedure by the surveillance engineer cnd the Action Statement was not met. This event was discovered l during an I&C review of the surveillance tests. Upon discovery, the instruments and their associated monitors were declared inoperable, cwaiting data review and completion of the surveys. Plant Management was notified of the event and the NRC was notified at 0950 on 10/26/88e per 10CFR50.72. This Supplemental Report is being submitted to inform the Commission of the status of corrective l cotions.

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IDENTIFICATION OF THE EVENT Seismic Monitoring Instrumentation (IN) was out for more than 30 days without the submittal of a Special Report violating a Tech.

L Spec. action statement due to personnel error.

Event Date: 10/25/88 Report Date: 5/16/90 l CONDITIONS PRIQB TO THE EVEHI l Operational Condition 4 (Cold Shutdown)

Mode Switch - Shutdown RPV Pressure : O psig RPV Temperature = 106 Degrees F i POWER LEVEL - 0 All rods inserted in the core.

DESCRIPTION _0E_IHE EVENI e

.On October 25, 1988, it was discovered that seismic monitoring instrumentation was returned to service prior to completing all cetions necessary for verifying operability as delineated in the curveillance procedure SP 44.655.03, Seismic Monitoring l Instrumentation Calibration and Functional Test. These instruments cre required to be operable at all times per Tech Spec. 3.3.7.2.

When-the instruments were taken out of service for calibration, they were required to be returned to service within 30 days or the Action Statement would apply. The Action Statement required the submittal of a Special Report within 10 days. These instruments were not J properly returned to service by procedure and the Action Statement was not met. This event was discovered during an I&C review of the l I

aurveillance_ tests. Upon discovery, the instruments and their associated monitors were declared inoperable, awaiting data review cnd completion of the surveys. Plant Management was notified of the cvent and the NRC was notified at 0950 on 10/26/88 per 100FR50.72.

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virr u . = w we ,.-am.u nn The following identifies the inoperable monitors and their reason for inoperability:

Date l Taken out of i instrument Eersice Beamon for Innnerabilitz 1Z94-ZR 005 BY 8/29/88 Survey not performed  ;

-ZR 005 BZ 8/31/88 Survey not performed I

-ZR 005 CX 8/19/88 Survey not performed 1

-ZR 006 C 9/03/88 Survey not performed 1

-ZR 004 X 4/22/88 Cal. data out of spec. I

-ZE 003 A 4/24/88 Survey data out of spec.

CAUSE QLIBLEYEH The root cause of the event was personnel error. The individual responsible for the review of the surveillance test did not-odequately ensure that the acceptance criteria was met prior to placing the instruments back in service. In addition, there are inadequacies in SP 44.655.03 that contributed to this event.

As part of the procedure, when the seismic instruments are calibrated and placed back in the recorder, the recorder is reinstalled from where it was removed and then surveyed to ensure it is properly positioned. The need to perform this survey before returning the recorder to service'is identified in the Discussion cection (3.2) of the procedure. Although there are procedural steps for performing the survey, the body of the procedure does not cpecifically state that this must be done prior to returning the rscorders to service. In addition, there are sign-off steps in the instrument Time Keeping Log (Appendix 12.30) to verify removal from cnd return to service of the recorders, however, the sequencing of

.the steps does not ensure that the survey is performed before being i

returned to service, l

i ANALYSIS _QE_IBE_ EYE R This event resulted in the violation of the reporting requirements specified in Technical Specification Section 3.3.7.2, Action Statement "a" and is reportable per 10CFR50.73(a)(2)(1). Technical Specifications require a Special Report to be submicted within 10 days following 30 days of seismic monitoring instrumentation inoperability. As discussed above, this reporting requirement was not met.

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mw-. - a w -on There was no safety significance to the event. All others seismic instrumentation identified in Tech. Spec. Table 3.3.7.2-1 was unaffected by the.inoperability of the subject recorders. These recorders are passive devices and do notTherefore, serve to provide their indication  :

of'a seismic event to the Control Room.

inoperability had no effect on the ability to detect a seismic cvent. They serve to provide. data for analysis following a seismic cvent. Other Control Building, Reactor Building and free field ceismic instrumentation identified in Tech. Spec. Table 3.3.7.2-1 ^

was operable to provide data for analysis and to provide Control Room indication of a seismic event.

CORRECTIVE ACTIONS H

1. . The surveillance engineer responsible for the event has been reassigned. .
2. Station Procedure SP 44.655.03 has been replaced with five smaller surveillance procedures. This will allow the testing required by Technical Specification 4.3.7.2.1 to be performed in stages and will minimize the chance of a seismic monitoring instrument being inoperable for more than 30 days. These new Procedures clearly identify that the survey requirements must j ,~

be met before returning the instruments to service. Additional reviews have also been added to the procedure.

3- An Engineering Evaluation and Assistance Request.(EEAR 89-002) has been initiated to request the installation of permanent alignment pins or mounting plates. These will eliminate the need for surveying the recorders and reduce the 3 mount of time the recorders are inoperable due to surveillance testing. Work i

on the EEAR has been deferred indefinitely due to the New York

! State - LILCO Shoreham Settlement Agreement.

ADDITIONAL INFORMATION ,

1 L a .- tianuf acturar_and_mndal_numhar_nt_f ailed _pomponent_Lal l None

b. LEB_ numbers of orevious_similar events LER 88-008 l ..e .. A usi

-