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{{#Wiki_filter:-ACCELERATED D TRIBUTION DEMONSTRATION SYSTEM DOCKET g 05000528 05000529 05000530 R D 05000528 A 05000529 05000530 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9012040223 DOC.DATE: 90/11/20 NOTARIZED:
{{#Wiki_filter:- ACCELERATED D TRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
YES FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi STN-50-529 Palo Verde Nuclear Station, Unit 2, Ariz'ona Publi ,'TN-50-530 Palo Verde Nuclear Station, Unit 3, Arizona Publi AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.
ACCESSION NBR:9012040223                 DOC.DATE:   90/11/20   NOTARIZED: YES         DOCKET g FACIL:STN-50-528 Palo Verde Nuclear Station,                 Unit 1, Arizona Publi 05000528 STN-50-529 Palo Verde Nuclear Station,             Unit 2, Ariz'ona Publi 05000529
Arizona Public Service Co.(formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
        ,'TN-50-530 Palo Verde Nuclear Station,               Unit 3, Arizona Publi 05000530 AUTH. NAME             AUTHOR AFFILIATION CONWAY,W.F.           Arizona Public Service Co.           (formerly Arizona Nuclear Power     R RECIP.NAME             RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)


==SUBJECT:==
==SUBJECT:==
Application for amends to Licenses NPF-41,NPF-51 6 NPF-74, revising TS Surveillance Requirement 4.4.1.4.1.2.
Application for amends to Licenses NPF-41,NPF-51 6 NPF-74,                         D revising   TS   Surveillance Requirement 4.4.1.4.1.2.
DISTRIBUTION CODE: A061D COPIES RECEIVED:LTR ENCL SIZE: TITLE: OR/Licensing Submittal:
DISTRIBUTION CODE: A061D             COPIES RECEIVED:LTR       ENCL       SIZE:
Loss of Residual Heat Removal (RHR)GL-87-12 NOTES: STANDARDIZED PLANT Standardized plant.Standardized plant;8 E INTERNAL: RECIPIENT ID CODE/NAME PD5 LA PETERSON,S.
TITLE: OR/Licensing Submittal: Loss               of Residual Heat   Removal (RHR) GL-87-12 NOTES: STANDARDIZED PLANT                                                             05000528 A Standardized plant.                                                         05000529 Standardized plant;                                       8                 05000530 RECIPIENT                COPIES            RECIPIENT           COPIES          D ID  CODE/NAME            LTTR ENCL        ID CODE/NAME       LTTR ENCL PD5 LA                       1    0      PD5 PD                  1    1 E
ACRS NRR TRAMMELL, C NRR/DST 8E2 OGC/HDS1 RES/DSIR/EIB COPIES LTTR ENCL 1 0 1 1 6 6 1'1 1 1 0 1 1 RECIPIENT ID CODE/NAME PD5 PD TRAMMELL,C.
PETERSON,S.                 1    1      TRAMMELL,C.              1     1 INTERNAL: ACRS                            6     6     NRR BALUKJIAN,H         2    2 NRR TRAMMELL,C              1'          NRR/DOEA/OTSB11         1     1 NRR/DST 8E2                  1     1     OC                      1   0 OGC/HDS1                    1     0       'G'F  LE            ,,"1   1 RES/DSIR/EIB                1    1 EXTERNAL: NRC PDR                         1     1     NSIC                    1   1 NOTES:                                      1     1 D
NRR BALUKJIAN,H NRR/DOEA/OTSB11 OC'G'F LE COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 0 ,,"1 1 D EXTERNAL: NRC PDR NOTES: 1 1 1 1 NSIC 1 1 D NOTE TO ALL"RIDS" RECIPIENTS:
A D
A D D PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!i T TAL NUMBER OF COPIES REQUIRED: LTTR 22 ENCL 19 Arizona Public Service Company P.O.BOX 53999~PHOENIX, ARIZONA 85072-3999 WILLIAM F.CONWAY EXECUTIVEVICEPRESIDENT NUCLEAR 161-03607-WFC/JST November 20, 1990 Docket Nos.STN 50-528/529/530 Document Control Desk U.S.Nuclear Regulatory Commission Mail Station Pl-37 Washington, D.C.20555
D NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
i T TAL NUMBER OF COPIES REQUIRED: LTTR                 22   ENCL   19


==Dear Sirs:==
Arizona Public Service Company P.O. BOX 53999 ~ PHOENIX, ARIZONA 85072-3999 WILLIAMF. CONWAY EXECUTIVEVICEPRESIDENT NUCLEAR                                                    161-03607-WFC/JST November 20, 1990 Docket Nos.       STN  50-528/529/530 Document Control Desk U. S. Nuclear Regulatory Commission Mail Station Pl-37 Washington, D. C. 20555
Sub)ect: Palo Verde Nuclear Generating Station (PVNGS)(Units 1, 2, and 3)Technical Specification Amendment Request Sections 3/4.4 and 3/4.9 File: 90-056-026 This letter requests an amendment to the PVNGS 1, 2, and 3 Technical Specification Surveillance Requirements 4.4.1.4.1.2, 4.4.1.4.2, 4.9.8.1, and 4.9.8.2.The proposed change would modify the minimum shutdown cooling flow specifications for Modes 5 and 6.The revised minimum" flow specification would meet the design requirements of the shutdown cooling system for protection against a boron dilution event and provide an increased operating margin between the minimum flow requirements and the onset of air entrainment in the shutdown cooling suction nozzles during reactor coolant system reduced inventory operation.
 
The proposed amendment is submitted in response to the"Programmed Enhancements" Section of Generic Letter No.88-17,"Loss of Decay Heat Removal." Arizona Public Service respectfully requests that this amendment be approved prior to the Unit 1 surveillance outage, scheduled to begin January 12, 1991, to support steam generator eddy current testing.Steam generator eddy current testing requires installation of the steam generator nozzle dams and lowering of reactor vessel water level to approximately mid-loop during the nozzle dams installation (approximately 2 to 3 days).If this amendment were not approved, and the additional safety margin between the onset of air entrainment and minimum Technical Specification flow requested in this amendment was not available prior to the beginning of the outage, APS would off load the core prior to mid-loop operation.
==Dear    Sirs:==
Core off load would result in'n additional 35 days being added to the outage schedule and substantial financial impact.r;r~9012040223 9'C>1100 PDR'DOCK 05000528 P PDC N 161-03607-WFC/JST November 20, 1990 Document Control Desk U.S.Nuclear Regulatory Commission Page 2 Enclosed with this amendment request are: A.Description of Amendment Request BE Purpose of the Technical Specification C.Need for the Technical Specification Change DE Basis for No Significant Hazards Consideration E.Safety Analysis of the Proposed Change Request F.Environmental Impact Consideration Determination G.Revised Technical Specification Change Pages Pursuant to 10 CFR 50.91(b)(1) a copy of this request has been forwarded to the Arizona Radiation Regulatory Agency.If there are any questions concerning this request, please contact Mr.Michael E.Powell at (602)340-4981.Sincerely, WFC/JST/jle Attachments CC: J.B.Martin (all w/a)D.H.Coe A.C.Gehr A.H.Gutterman C.F.Tedford I I 161-03607-WFC November 20, 1990 STATE OF ARIZONA))ss.COUNTY OF MARICOPA)I, WE F.Conway, represent that I am Executive Vice President Nuclear, that the foregoing document has been signed by me on behalf of Arizona Public Service Company with full authority to do so, that I have read such document and know its contents, and that to the best of my knowledge and belief, the statements made therein are true and correct.W.F.Conway Sworn To Before Me This~D Day Of 1990.Notary Public My Commission Expires ihjiy Commission Expires Apdi 6, 1991 I~,pl" g'I$1 161-03607-MFC/JST November 20, 1990 A.Descri tion of Amendment Re uest This amendment request proposes changes to Surveillance Requirements 4.4.1.4.1.2,'4.4.1.4.2, 4.9.8.1, and 4.9.8.2 for minimum shutdown cooling flow in Modes 5 and 6.The current Surveillance Requirements verify, at, least once per 12 hours, that at least one shutdown cooling loop is in operation with a flow rate of-greater.than or equal to 4000 gallons per minute (gpm).The proposed change would require this minimum flow rate to be greater than or equal to 3780 gpm (indicated).
 
C Changes to the Bases Sections 3/4.4.1 and 3/4.9.8 are also proposed to reflect the revised.flowrate..Attachment G contains the revised Technical Specification change pages., B.Pur ose of the Technical S ecification The purpose of Surveillance Requirements 4.4.1.4.1.2 and 4.4.1.4.2 (applicable in Mode 5 with and without reactor coolant loops filled)is to ensure adequate shutdown cooling loop-flow while on shutdown cooling for decay heat removal.This minimum flow requirement also provides adequate flow to ensure mixing, prevent stratification, and produce gradual reactivity changes during boron concentration reductions in the Reactor Coolant System.The purpose of Surveillance Requirements 4.9'.1 and 4.9.8.2 (applicable in Mode 6)is to ensure there is adequate shutdown cooling flow to provide (1)sufficient cooling capacity to remove decay heat and maintain the water in the reactor pressure vessel below 135 degrees Fahrenheit as required during Mode 6, (2)sufficient coolant circulation is maintained through the reactor core to minimize the effects of a boron dilution incident and prevent boron stratification, and'(3)the Temperature Differential across the core will be maintained at less than 75 degrees Fahrenheit during Mode 6.C.Need for the Technical S ecification Chan e PVNGS is proposing this amendment in accordance with the Programmed Enhancement Section of Generic Letter No.88-17 to provide additional margin between the minimum flow requirements for shutdown cooling and the onset of vortex formation in the sh'utdown cooling suction nozzles during reduced reactor coolant system inventory operation.
Sub)  ect:        Palo Verde Nuclear Generating Station (PVNGS)
The formation of vortexes in the shutdown cooling nozzles has the potential to air bind the shutdown cooling pump and heat exchanger'hus rendering the system inoperable.
(Units 1, 2, and 3) Technical Specification                    Amendment  Request Sections 3/4.4 and 3/4.9 File:    90-056-026 This    letter      requests    an    amendment    to the      PVNGS      1, 2, and  3  Technical Specification Surveillance Requirements 4.4.1.4.1.2, 4.4.1.4.2, 4.9.8.1, and 4.9.8.2. The proposed change would modify the minimum shutdown cooling flow specifications for Modes 5 and 6. The revised minimum" flow specification would meet the design requirements of the shutdown cooling system for protection against a boron dilution event and provide an increased operating margin between the minimum flow requirements and the onset of air entrainment in the shutdown cooling suction nozzles during reactor coolant system reduced inventory operation. The proposed amendment is submitted in response to the "Programmed Enhancements" Section of Generic Letter No. 88-17, "Loss of Decay Heat Removal."
The reactor coolant system is drained to mid-loop during the installation of Steam Generator nozzle dams.The installation of these dams permits work and inspections to be performed on the Steam Generators without defueling.
Arizona Public Service respectfully requests that this amendment be approved prior to the Unit 1 surveillance outage, scheduled to begin January 12, 1991, to support steam generator eddy current testing. Steam generator eddy current testing requires installation of the steam generator nozzle dams and lowering of reactor vessel water level to approximately mid-loop during the nozzle dams installation (approximately 2 to 3 days).                           If   this amendment were not approved,       and the additional safety margin between                       the onset of air entrainment and minimum Technical Specification flow requested in this amendment was not available prior to the beginning of the outage, APS would off load the core prior to mid-loop operation. Core off load would result in additional 35 days being added to the outage schedule and substantial
Entrainment of air in the shutdown cooling system has been observed at flows above 4100 gpm.The current minimum flow of 4000 gpm allows only a 100 gpm band in which to operate the shutdown cooling system between the current upper flow limit and the Technical Specification minimum flow.The minimum flow proposed by this amendment (3780 gpm indicated) would increase this-margin to 320 gpm and continue'o provide adequate mixing of boron in the RCS.This change would improve the safety of the shutdown cooling system by allowing operation substantially below the flowrate of incipient air entrainment, minimizing the possibility of air binding the shutdown cooling system (SDCS), and still providing adequate flow for decay heat removal and mixing of boron.
                                                                                                        'n financial impact.
i 161-03607-WFC/JST November 20, 1990 The proposed minimum flow of 3780 gpm (indicated) is above the region where a system flow instability has been observed.The observed phenomenon, which occurs while operating the Low Pressure Safety Injection Pump (LPSI)in the 2800 to 3400 gpm range,.is an acoustic rumble which results from recirculation flow in the-pump inlet piping.The effects of this are increased pump vibration which if allowed to occur long enough would reduce the life of pump and motor.APS is continuing to study this phenomena and methods of eliminating it." D.Basis for No Si nificant Hazards Consideration The commission has provided standards for determining whether a significant hazards consideration exists as stated in 10 CFR 50.92.A proposed amendment to an operating license for a facility involves no significant hazards consideration if operation of the facility in accordance with a proposed amendment would not: (1)Involve a signfficant increase in the probability or consequences of an accident previously evaluated:
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or (2)Create the possibility of a new or different kind of accident from any accident previously evaluated; or (3)Involve a significant reduction in a margin of safety.A discussion of these standards, as they relate to the amendment, follows: Standard 1-Involves a significant increase in the probability or consequences of an accident previously evaluated.
9012040223     9'C>1100 PDR'DOCK 05000528 P                       PDC N
The proposed change does not involve a significant increase in the probability or consequences of an accident previously evaluated but actually enhances the safety of operation of the shutdown cooling system.Lowering the shutdown cooling flow during reduced reactor coolant system inventory operation improves the margin between the required minimum flow and the formation of vortexes in the shutdown cooling suction nozzles.The formation of these vortexes has the potential of air binding the shutdown cooling heat exchanger and pumps of the operating shutdown cooling train.The boron dilution event was analyzed by ABB-Combustion Engineering to determine if the new flowrates would provide adequate time for operator recognition and correction prior to criticality.
 
The results are as follows: The limiting (most rapid)case which was analyzed for PVNGS was the case of a dilution during Beginning of Core (BOC), Mode 5 drained conditions, at the maximum charging flow rate.Based upon , the RCS volume which was assumed (including one train of SDCS)at these conditions, and the time associated with circulation of the RCS at an actual flow of 3400 gpm, the analysis shows that the mixing time is short relative to the time to criticality therefore the dilution would proceed smoothly.It is concluded that there will be sufficient time to recognize and control the dilution before the core reached critical.The case of Mode 5, RCS not drained (with"all other conditions the same)and Mode 6 cases are bounded by the limiting case of drained conditions in Mode 5.Therefore a shutdown cooling system flowrate of 3400 gpm is 161-03607-WFC/JST November 20, 1990 acceptable in Modes 5 and 6 with respect to a postulated boron dilution event.This evaluation has completed verification according to the C-E QADM.Standard 2-Create the possibility of a new or different kind of accident from any accident previously evaluated.
161-03607-WFC/JST November 20, 1990 Document Control Desk U. S. Nuclear Regulatory Commission Page 2 Enclosed with   this amendment request are:
The proposed reduced shutdown cooling flow changes the allowable flow to a value which does not affect the capability to detect and take corrective action for a boron dilution incident while on shutdown cooling.The ability of the shutdown cooling system to remove decay heat and maintain RCS temperature is controlled by operators who vary flow through the shutdown cooling heat exchanger to maintain the specified mode temperature requirements.
A. Description of Amendment Request BE Purpose of the Technical Specification C. Need for the Technical Specification Change DE Basis for No Significant Hazards Consideration E. Safety Analysis of the Proposed Change Request F. Environmental Impact Consideration Determination G. Revised Technical Specification Change Pages Pursuant to 10 CFR 50.91(b)(1) a copy of     this request has been forwarded to the Arizona Radiation Regulatory Agency.
The proposed minimum flow decreases the possibility of air binding the shutdown cooling system when at mid-loop by minimizing operation with flowrates which could induce significant air entrainment in the shutdown cooling system.The reduced flow does not affect operation of the shutdown cooling system nor involve any system configuration changes.Thus no possibility of a new or different kind of accident from any accident previously evaluated is created.Standard 3-Involve a significant reduction in a margin of safety.The reduction in the minimum flow requirements does not reduce the margin of safety associated with the operation of the shutdown cooling system.The system will still perform within its design bases.The proposed flow will increase the margin of safety by allowing operation of the system further away from the flowrates which produce significant air entrainment in the shutdown cooling system.This minimizes the possibility of rendering one train of shutdown cooling inoperable due to air binding of the pumps or heat exchanger.
If there are any questions concerning this request, please contact Mr. Michael E. Powell at (602) 340-4981.
The proposed change matches one of the examples given in 51 FR 7751 of amendments that do not involve a significant hazards consideration.
Sincerely, WFC/JST/jle Attachments CC:   J. B. Martin   (all w/a)
Specifically, the proposed amendment is a change resulting from the application of a small refinement of a previously used calculational model or design method.In this case, the lower minimum flow requirements were the result of a reanalysis of the boron dilution event by ABB-Combustion Engineering.
D. H. Coe A. C. Gehr A. H. Gutterman C. F. Tedford
This reanalysis demonstrated the proposed minimum flowrates presented in this amendment request meet the requirements of the original analysis.E.Safet Anal sis of the Pro osed Chan e Re uest The proposed Technical Specification change will not increase the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the Final Safety Analysis Report (UFSAR).The proposed amendment does not make changes to the design of the facility.The effects of the amendment are lower minimum flow requirements for shutdown cooling operation.
 
The design bases of the shutdown cooling syst: em are not affected by this change.
I I
161-03607-NFC/JST November 20, 1990 The proposed Technical Specification change will not create the possibility of an accident or malfunction of equipment of a different type than any evaluated previously in the UFSAR.This change will minimize the possibility of a loss of shutdown cooling event by increasing the margin between the onset of significant air entrained flow and the minimum required flow for shutdown cooling.There are no equipment changes proposed in thi.s amendment nor any change in the operation of shutdown cooling system other than a change to the Technical Specification minimum flowrate in Modes 5 and 6.The proposed Technical Specification change will not reduce the margin of safety as defined in the basis for any Technical Specification.
 
The bases for Surveillance Requirements 4.4.1.4.1.2, 4.4.1.4.2, 4.9.8.1, and 4.9.8.2 have been reviewed.The requirements stated in the bases sections are still met with the proposed minimum flowrates.
161-03607-WFC November 20, 1990 STATE OF ARIZONA                   )
The requirement for removal of decay heat is controlled by the operators who maintain RCS temperature by varying the amount of flow bypassing the shutdown cooling heat exchanger.
                                    ) ss.
The requirements for boron mixing are also satisfied with the proposed flowrate.Thus the proposed minimum flowrates do not reduce the margin of safety as defined in the bases for these Technical Specifications.
COUNTY OF MARICOPA                 )
The proposed amendment to reduce the minimum flow for these Surveillance Requirements has been evaluated by ABB-Combustion Engineering (NSSS vendor)to ensure adequate circulation is maintained to minimize the effects of a boron dilution event and prevent boron stratification.
I, WE F. Conway, represent that I am Executive Vice President Nuclear, that the foregoing document has been signed by me on behalf of Arizona Public Service Company with full authority to do so, that I have read such document and know its contents, and that to the best of my knowledge and belief, the statements made therein are true and correct.
The basis for the 23 minute loop circulation time criteria in the Technical Specification Bases is derived from a concern for avoiding a boron dilution event.A calculation was performed which developed acceptable accident mitigation under the following assumptions:
W. F. Conway Sworn To Before             Me   This   ~D Day Of       1990.
The SDCS operates in one RCS loop while the other RCS loop is static (i.e., only one train of the SDCS is in operation);
Notary Public My   Commission Expires ihjiy Commission Expires Apdi 6, 1991
The SDCS is in operation at 4000 gpm;The RCS is full;The fuel in the core is at beginning of core life.Inherent to the calculation are assumptions regarding fluid mixing within the RCS.At 4000 gpm a full RCS (90,000 gal)will be completely circulated within 23 minutes.This RCS circulation time was determined to be acceptable because it was significantly less than the approximately one hour minimum time for loss of shutdown margin in UFSAR Section 15.4.6.The RCS circulation time at the proposed flowrate of 3400 gpm (actual)is 27 minutes which is also significantly less than the minimum time to loss of shutdown margin.Thus the proposed flowrate of 3400 gpm (actual)would not affect the ability of an operator to recognize and curtail a boron dilution event prior to loss of shutdown margin.The requirements to remove decay heat are controlled by the operators who must ensure there is sufficient flow through the shutdown cooling heat exchanger to maintain the temperature requirements of the applicable mode.The control of RCS temperature while on shutdown cooling at Palo Verde is accomplished by controlling the amount of flow bypassing the shutdown cooling heat exchanger 161-03607-WFC/JST November 20, 1990 and not by maintaining a minimum system flowrate.Thus the requirement to maintain a minimum system flow is only for prevention of a boron dilution event and does not directly relate to decay heat removal.ABB-Combustion Engineering has performed a study to determine the minimum flows necessary to maintain RCS temperature at less than 135 degrees Fahrenheit in Mode 6 and concluded that 3400 gpm (actual)will accomplish this 12 days after shutdown with a 105 degree fahrenheit cooling water inlet temperature.
 
In Mode 5, 3400 gpm (actual)will maintain the RCS less than 200 degrees Fahrenheit 10 hours after reactor shutdown.These calculations assume worst case cooling water inlet conditions and conservative heat exchanger fouling factors, the current capability of the shutdown cooling system is in excess of these assumptions.
I ~
F.Environmental Im act Consideration Determination The proposed change request does not involve an unreviewed environmental question because operation of PVNGS Units 1, 2, and 3 in accordance with this change would not: Result in a significant increase in any adverse environmental impact previously evaluated in the Final Environmental Statement (FES)as modified by the staff's testimony to the Atomic Safety and Licensing Board, Supplements to the FES, Environmental Impact Appraisals, or in any decisions of the Atomic Safety Licensing Board: or 2.Result in a significant change in effluents or power levels;or 3.Result in matters not previously reviewed in the licensing basis for PVNGS which may have a significant environmental impact.G.Revised Technical S ecification Chan e Pa es See attached pages as typical for each unit.Deletions are noted by strikeout and additions are highlighted and in bold italic print.}}
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161-03607-MFC/JST November 20, 1990 A. Descri   tion of Amendment Re       uest This   amendment   request     proposes     changes     to   Surveillance       Requirements 4.4.1.4.1.2, '4.4.1.4.2, 4.9.8.1, and 4.9.8.2 for minimum shutdown cooling flow in Modes 5 and 6. The current Surveillance Requirements verify, at, least once per 12 hours, that at least one shutdown cooling loop is in operation with a flow rate of- greater .than or equal to 4000 gallons per minute (gpm). The proposed change would require this minimum flow rate to be greater than or equal to 3780 gpm (indicated).
to the Bases Sections 3/4.4.1 and 3/4.9.8 are also proposed to reflect C
Changes the revised. flowrate. .             Attachment G contains           the revised Technical Specification change pages.,
B. Pur ose   of the Technical       S ecification The purpose of Surveillance Requirements 4.4.1.4.1.2 and 4.4.1.4.2 (applicable in Mode 5 with and without reactor coolant loops               filled)   is to ensure adequate shutdown cooling loop-flow while on shutdown cooling for decay heat removal.
This minimum flow requirement also provides adequate flow to ensure mixing, prevent stratification, and produce gradual reactivity changes during boron concentration reductions in the Reactor Coolant System.
The purpose   of Surveillance Requirements 4.9 '.1 and 4.9.8.2 (applicable in Mode 6) is to ensure there is adequate shutdown cooling flow to provide (1) sufficient cooling capacity to remove decay heat and maintain the water in the reactor pressure vessel below 135 degrees Fahrenheit as required during Mode 6, (2) sufficient coolant circulation is maintained through the reactor core to minimize the effects of a boron dilution incident and prevent boron stratification,   and '(3) the Temperature         Differential     across   the core   will be maintained at less than     75 degrees     Fahrenheit during     Mode 6.
C. Need   for the Technical     S   ecification   Chan e PVNGS   is proposing     this amendment in accordance with the Programmed Enhancement   Section of Generic Letter No. 88-17 to provide additional margin between the minimum flow requirements for shutdown cooling and the onset of vortex formation in the sh'utdown cooling suction nozzles during reduced reactor coolant system inventory operation. The formation of vortexes in the shutdown cooling nozzles has the potential to air bind the shutdown cooling pump and heat exchanger'hus             rendering the system inoperable.             The reactor coolant system is drained to mid-loop during the installation of Steam Generator nozzle dams.           The installation of these dams permits work and inspections     to be   performed       on the Steam Generators             without defueling.
Entrainment of air     in the   shutdown   cooling   system   has   been   observed at flows above 4100 gpm.     The current     minimum   flow of 4000   gpm   allows   only a 100 gpm band in which to operate the shutdown cooling system               between   the current upper flow limit and the Technical Specification               minimum     flow. The   minimum flow proposed by this amendment (3780 gpm indicated)               would   increase   this- margin to 320 gpm and     continue'o     provide adequate mixing of           boron   in the RCS. This change would improve the safety of the               shutdown   cooling system by allowing operation substantially below the flowrate of incipient air entrainment, minimizing the possibility of air binding the shutdown cooling system (SDCS),
and still providing adequate flow for decay heat removal and mixing of boron.
 
i 161-03607-WFC/JST November 20, 1990 The proposed minimum         flow of 3780 gpm (indicated) is above the region where a system flow       instability     has been observed.         The observed phenomenon, which occurs while operating the Low Pressure Safety Injection Pump (LPSI) in the 2800 to 3400 gpm range, .is an acoustic rumble which results from recirculation flow in the- pump inlet piping.               The effects of this are increased pump vibration which       if allowed to occur long enough would reduce the life of pump and motor.           APS is continuing to study this phenomena               and methods of eliminating     it."
D. Basis   for No   Si nificant Hazards Consideration The commission has provided standards             for determining whether a significant hazards consideration exists as stated             in 10 CFR 50.92. A proposed amendment to an operating license for a facility involves no significant hazards consideration if operation of the facility in accordance with a proposed amendment would not: (1) Involve a signfficant increase in the probability or consequences         of an accident previously evaluated: or (2) Create the possibility of a new or different kind of accident from any accident previously evaluated; or (3) Involve a significant reduction in a margin of safety.
A discussion of these standards,         as they   relate to the   amendment,   follows:
Standard     1   -   Involves   a   significant     increase   in the     probability or consequences     of   an accident   previously evaluated.
The proposed change does not involve a significant increase in the probability or consequences of an accident previously evaluated but actually enhances the safety of operation of the shutdown cooling system.                   Lowering the shutdown cooling flow during reduced reactor coolant system inventory operation improves the margin between the required minimum flow and the formation of vortexes in the shutdown cooling suction nozzles. The formation of these vortexes has the potential of air binding the shutdown cooling heat exchanger and pumps of the operating shutdown cooling train.
The   boron     dilution       event was analyzed by ABB-Combustion Engineering to determine     if   the new flowrates would provide adequate time for operator recognition and correction prior to criticality. The results are as follows:
The limiting (most rapid) case which was analyzed for PVNGS was the case of a dilution during Beginning of Core (BOC), Mode 5 drained conditions, at the maximum charging flow rate. Based upon
      , the RCS volume which was assumed         (including one train of SDCS) at these conditions, and the time associated with circulation of the RCS at an actual flow of 3400 gpm, the analysis               shows that the mixing time is short relative to the time to criticality therefore the dilution would proceed smoothly.             It is concluded that there will be sufficient time to recognize and control the dilution before the core reached critical. The case of Mode 5, RCS not drained (with "all other conditions the same) and Mode 6 cases are bounded by the limiting case of drained conditions in Mode 5.
Therefore a shutdown cooling system flowrate of 3400 gpm is
 
161-03607-WFC/JST November 20, 1990 acceptable     in Modes 5     and 6   with respect to a postulated boron dilution event. This             evaluation has completed verification according to the C-E       QADM.
Standard 2 - Create the possibility of a new or                 different kind of accident from any accident previously evaluated.
The proposed     reduced     shutdown cooling flow changes         the allowable flow to a value which does not affect the capability to detect and take corrective action for a boron dilution incident while on shutdown cooling. The ability of the shutdown cooling system to remove decay heat and maintain RCS temperature is controlled by operators who vary flow through the shutdown cooling heat exchanger               to maintain the specified mode temperature requirements. The proposed minimum flow decreases the possibility of air binding the shutdown cooling system when at mid-loop by minimizing operation with flowrates which could induce significant air entrainment in the shutdown cooling system. The reduced flow does not affect operation of the shutdown cooling system nor involve any system configuration changes. Thus no possibility of a new or different kind of accident from any accident previously evaluated is created.
Standard   3 -   Involve   a significant reduction in       a margin of safety.
The   reduction in the minimum flow requirements does not reduce the margin of safety associated with the operation of the shutdown cooling system. The system will still perform within its design bases. The proposed flow will increase the margin of safety by allowing operation of the system further away from the flowrates which produce significant air entrainment in the shutdown cooling system. This minimizes the possibility of rendering one train of shutdown cooling inoperable due to air binding of the pumps or heat exchanger.
The proposed       change   matches     one of the     examples given in 51 FR 7751 of amendments     that     do   not   involve     a   significant hazards consideration.
Specifically,       the proposed amendment             is a change resulting from the application of     a small refinement of a         previously used calculational model or design method.       In this case, the lower minimum flow requirements were the result of     a   reanalysis of the boron dilution event by ABB-Combustion Engineering.     This reanalysis demonstrated the proposed minimum flowrates presented in this amendment             request meet the requirements       of the original analysis.
E. Safet   Anal sis of the Pro osed Chan           e Re   uest The proposed     Technical Specification change will not increase the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the Final Safety Analysis Report (UFSAR). The proposed amendment does not make changes to the design of the facility. The effects of the amendment are lower minimum flow requirements for shutdown cooling operation. The design bases of the shutdown cooling syst: em are not affected by this change.
 
161-03607-NFC/JST November 20, 1990 The proposed   Technical Specification change will not create the possibility of an accident   or malfunction of equipment of a different type than any evaluated previously in the UFSAR. This change will minimize the possibility of a loss of shutdown cooling event by increasing the margin between the onset of significant air entrained flow and the minimum required flow for shutdown cooling. There are no equipment changes proposed in thi.s amendment nor any change in the operation of shutdown cooling system other than a change to the Technical Specification minimum flowrate in Modes 5 and 6.
The proposed Technical         Specification     change will not reduce the margin of safety as defined in the       basis for any Technical Specification. The bases for Surveillance Requirements 4.4.1.4. 1. 2, 4 .4 .1.4. 2, 4.9 . 8 . 1, and 4. 9 . 8 . 2 have been reviewed. The requirements stated in the bases sections are still met with the proposed minimum flowrates. The requirement for removal of decay heat is controlled by the operators who maintain RCS temperature by varying the amount of flow bypassing the shutdown cooling heat exchanger.                       The requirements for     boron mixing   are also satisfied   with the proposed   flowrate.
Thus the proposed minimum flowrates do not reduce the margin of safety as defined in the bases for these Technical Specifications.
The proposed amendment to reduce the minimum flow for these Surveillance Requirements has been evaluated by ABB-Combustion Engineering (NSSS vendor) to ensure adequate circulation is maintained to minimize the effects of a boron dilution event and prevent boron stratification. The basis for the 23 minute loop circulation time criteria in the Technical Specification Bases is derived from a concern for avoiding a boron dilution event. A calculation was performed which developed acceptable accident mitigation under the following assumptions:
The SDCS     operates in one RCS loop while the other RCS loop is static (i.e., only one train of the SDCS is in operation);
The SDCS is in operation at 4000 gpm; The RCS is   full; The fuel in the core is at beginning of core         life.
Inherent to the calculation are assumptions regarding fluid mixing within the RCS. At 4000 gpm a     full RCS (90,000 gal) will be completely circulated within 23 minutes. This RCS   circulation time was determined to be acceptable because it was significantly less than the approximately one hour minimum time for loss of shutdown margin in UFSAR Section 15.4.6. The RCS circulation time at the proposed flowrate of 3400 gpm (actual) is 27 minutes which is also significantly less than the minimum time to loss of shutdown margin. Thus the proposed flowrate of 3400 gpm (actual) would not affect the ability of an operator to recognize and curtail a boron dilution event prior to loss of shutdown margin.
The requirements     to remove decay heat are controlled by the operators who must ensure there   is sufficient     flow through the shutdown cooling heat exchanger to maintain   the temperature     requirements   of the applicable mode. The control of RCS temperature     while   on   shutdown   cooling   at Palo Verde is accomplished by controlling   the   amount   of flow   bypassing   the shutdown cooling heat exchanger
 
161-03607-WFC/JST November 20, 1990 and not by maintaining a minimum system flowrate.         Thus the requirement to maintain a minimum system flow is only for prevention of a boron dilution event and does not directly relate to decay heat removal.
ABB-Combustion Engineering     has performed a study to determine the minimum flows necessary to maintain RCS temperature at less than 135 degrees Fahrenheit in Mode 6 and concluded that 3400 gpm (actual) will accomplish this 12 days after shutdown with a 105 degree fahrenheit cooling water inlet temperature. In Mode 5, 3400 gpm (actual) will maintain the RCS less than 200 degrees Fahrenheit 10 hours after reactor shutdown. These calculations assume worst case cooling water inlet conditions and conservative heat exchanger fouling factors, the current capability of the shutdown cooling system is in excess   of these assumptions.
F. Environmental Im act Consideration Determination The   proposed change request does not involve an unreviewed environmental question because operation of PVNGS Units 1, 2, and 3 in accordance with this change would not:
Result in a significant increase in any adverse environmental impact previously evaluated in the Final Environmental Statement (FES) as modified by the staff's testimony to the Atomic Safety and Licensing Board, Supplements to the FES, Environmental Impact Appraisals, or in any decisions of the Atomic Safety Licensing Board: or
: 2. Result in a significant change in effluents or power levels; or
: 3. Result in matters     not previously   reviewed in the licensing basis for   PVNGS which may have a significant environmental impact.
G. Revised Technical S ecification Chan e Pa es See attached pages as typical for each unit. Deletions are noted by strikeout and additions are highlighted and in bold   italic print.}}

Revision as of 10:24, 29 October 2019

Application for Amends to Licenses NPF-41,NPF-51 & NPF-74, Revising TS Surveillance Requirements 4.4.1.4.1.2, 4.4.1.4.2,4.9.8.1 & 4.9.8.2 to Modify Min Shutdown Cooling Sys for Protection Against Boron Dilution Event
ML17305B211
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 11/20/1990
From: Conway W
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML17305B212 List:
References
161-03607-WFC-J, 161-3607-WFC-J, GL-88-17, NUDOCS 9012040223
Download: ML17305B211 (12)


Text

- ACCELERATED D TRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9012040223 DOC.DATE: 90/11/20 NOTARIZED: YES DOCKET g FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 STN-50-529 Palo Verde Nuclear Station, Unit 2, Ariz'ona Publi 05000529

,'TN-50-530 Palo Verde Nuclear Station, Unit 3, Arizona Publi 05000530 AUTH. NAME AUTHOR AFFILIATION CONWAY,W.F. Arizona Public Service Co. (formerly Arizona Nuclear Power R RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Application for amends to Licenses NPF-41,NPF-51 6 NPF-74, D revising TS Surveillance Requirement 4.4.1.4.1.2.

DISTRIBUTION CODE: A061D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: OR/Licensing Submittal: Loss of Residual Heat Removal (RHR) GL-87-12 NOTES: STANDARDIZED PLANT 05000528 A Standardized plant. 05000529 Standardized plant; 8 05000530 RECIPIENT COPIES RECIPIENT COPIES D ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 0 PD5 PD 1 1 E

PETERSON,S. 1 1 TRAMMELL,C. 1 1 INTERNAL: ACRS 6 6 NRR BALUKJIAN,H 2 2 NRR TRAMMELL,C 1' NRR/DOEA/OTSB11 1 1 NRR/DST 8E2 1 1 OC 1 0 OGC/HDS1 1 0 'G'F LE ,,"1 1 RES/DSIR/EIB 1 1 EXTERNAL: NRC PDR 1 1 NSIC 1 1 NOTES: 1 1 D

A D

D NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

i T TAL NUMBER OF COPIES REQUIRED: LTTR 22 ENCL 19

Arizona Public Service Company P.O. BOX 53999 ~ PHOENIX, ARIZONA 85072-3999 WILLIAMF. CONWAY EXECUTIVEVICEPRESIDENT NUCLEAR 161-03607-WFC/JST November 20, 1990 Docket Nos. STN 50-528/529/530 Document Control Desk U. S. Nuclear Regulatory Commission Mail Station Pl-37 Washington, D. C. 20555

Dear Sirs:

Sub) ect: Palo Verde Nuclear Generating Station (PVNGS)

(Units 1, 2, and 3) Technical Specification Amendment Request Sections 3/4.4 and 3/4.9 File: 90-056-026 This letter requests an amendment to the PVNGS 1, 2, and 3 Technical Specification Surveillance Requirements 4.4.1.4.1.2, 4.4.1.4.2, 4.9.8.1, and 4.9.8.2. The proposed change would modify the minimum shutdown cooling flow specifications for Modes 5 and 6. The revised minimum" flow specification would meet the design requirements of the shutdown cooling system for protection against a boron dilution event and provide an increased operating margin between the minimum flow requirements and the onset of air entrainment in the shutdown cooling suction nozzles during reactor coolant system reduced inventory operation. The proposed amendment is submitted in response to the "Programmed Enhancements" Section of Generic Letter No. 88-17, "Loss of Decay Heat Removal."

Arizona Public Service respectfully requests that this amendment be approved prior to the Unit 1 surveillance outage, scheduled to begin January 12, 1991, to support steam generator eddy current testing. Steam generator eddy current testing requires installation of the steam generator nozzle dams and lowering of reactor vessel water level to approximately mid-loop during the nozzle dams installation (approximately 2 to 3 days). If this amendment were not approved, and the additional safety margin between the onset of air entrainment and minimum Technical Specification flow requested in this amendment was not available prior to the beginning of the outage, APS would off load the core prior to mid-loop operation. Core off load would result in additional 35 days being added to the outage schedule and substantial

'n financial impact.

r; r~

9012040223 9'C>1100 PDR'DOCK 05000528 P PDC N

161-03607-WFC/JST November 20, 1990 Document Control Desk U. S. Nuclear Regulatory Commission Page 2 Enclosed with this amendment request are:

A. Description of Amendment Request BE Purpose of the Technical Specification C. Need for the Technical Specification Change DE Basis for No Significant Hazards Consideration E. Safety Analysis of the Proposed Change Request F. Environmental Impact Consideration Determination G. Revised Technical Specification Change Pages Pursuant to 10 CFR 50.91(b)(1) a copy of this request has been forwarded to the Arizona Radiation Regulatory Agency.

If there are any questions concerning this request, please contact Mr. Michael E. Powell at (602) 340-4981.

Sincerely, WFC/JST/jle Attachments CC: J. B. Martin (all w/a)

D. H. Coe A. C. Gehr A. H. Gutterman C. F. Tedford

I I

161-03607-WFC November 20, 1990 STATE OF ARIZONA )

) ss.

COUNTY OF MARICOPA )

I, WE F. Conway, represent that I am Executive Vice President Nuclear, that the foregoing document has been signed by me on behalf of Arizona Public Service Company with full authority to do so, that I have read such document and know its contents, and that to the best of my knowledge and belief, the statements made therein are true and correct.

W. F. Conway Sworn To Before Me This ~D Day Of 1990.

Notary Public My Commission Expires ihjiy Commission Expires Apdi 6, 1991

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161-03607-MFC/JST November 20, 1990 A. Descri tion of Amendment Re uest This amendment request proposes changes to Surveillance Requirements 4.4.1.4.1.2, '4.4.1.4.2, 4.9.8.1, and 4.9.8.2 for minimum shutdown cooling flow in Modes 5 and 6. The current Surveillance Requirements verify, at, least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, that at least one shutdown cooling loop is in operation with a flow rate of- greater .than or equal to 4000 gallons per minute (gpm). The proposed change would require this minimum flow rate to be greater than or equal to 3780 gpm (indicated).

to the Bases Sections 3/4.4.1 and 3/4.9.8 are also proposed to reflect C

Changes the revised. flowrate. . Attachment G contains the revised Technical Specification change pages.,

B. Pur ose of the Technical S ecification The purpose of Surveillance Requirements 4.4.1.4.1.2 and 4.4.1.4.2 (applicable in Mode 5 with and without reactor coolant loops filled) is to ensure adequate shutdown cooling loop-flow while on shutdown cooling for decay heat removal.

This minimum flow requirement also provides adequate flow to ensure mixing, prevent stratification, and produce gradual reactivity changes during boron concentration reductions in the Reactor Coolant System.

The purpose of Surveillance Requirements 4.9 '.1 and 4.9.8.2 (applicable in Mode 6) is to ensure there is adequate shutdown cooling flow to provide (1) sufficient cooling capacity to remove decay heat and maintain the water in the reactor pressure vessel below 135 degrees Fahrenheit as required during Mode 6, (2) sufficient coolant circulation is maintained through the reactor core to minimize the effects of a boron dilution incident and prevent boron stratification, and '(3) the Temperature Differential across the core will be maintained at less than 75 degrees Fahrenheit during Mode 6.

C. Need for the Technical S ecification Chan e PVNGS is proposing this amendment in accordance with the Programmed Enhancement Section of Generic Letter No. 88-17 to provide additional margin between the minimum flow requirements for shutdown cooling and the onset of vortex formation in the sh'utdown cooling suction nozzles during reduced reactor coolant system inventory operation. The formation of vortexes in the shutdown cooling nozzles has the potential to air bind the shutdown cooling pump and heat exchanger'hus rendering the system inoperable. The reactor coolant system is drained to mid-loop during the installation of Steam Generator nozzle dams. The installation of these dams permits work and inspections to be performed on the Steam Generators without defueling.

Entrainment of air in the shutdown cooling system has been observed at flows above 4100 gpm. The current minimum flow of 4000 gpm allows only a 100 gpm band in which to operate the shutdown cooling system between the current upper flow limit and the Technical Specification minimum flow. The minimum flow proposed by this amendment (3780 gpm indicated) would increase this- margin to 320 gpm and continue'o provide adequate mixing of boron in the RCS. This change would improve the safety of the shutdown cooling system by allowing operation substantially below the flowrate of incipient air entrainment, minimizing the possibility of air binding the shutdown cooling system (SDCS),

and still providing adequate flow for decay heat removal and mixing of boron.

i 161-03607-WFC/JST November 20, 1990 The proposed minimum flow of 3780 gpm (indicated) is above the region where a system flow instability has been observed. The observed phenomenon, which occurs while operating the Low Pressure Safety Injection Pump (LPSI) in the 2800 to 3400 gpm range, .is an acoustic rumble which results from recirculation flow in the- pump inlet piping. The effects of this are increased pump vibration which if allowed to occur long enough would reduce the life of pump and motor. APS is continuing to study this phenomena and methods of eliminating it."

D. Basis for No Si nificant Hazards Consideration The commission has provided standards for determining whether a significant hazards consideration exists as stated in 10 CFR 50.92. A proposed amendment to an operating license for a facility involves no significant hazards consideration if operation of the facility in accordance with a proposed amendment would not: (1) Involve a signfficant increase in the probability or consequences of an accident previously evaluated: or (2) Create the possibility of a new or different kind of accident from any accident previously evaluated; or (3) Involve a significant reduction in a margin of safety.

A discussion of these standards, as they relate to the amendment, follows:

Standard 1 - Involves a significant increase in the probability or consequences of an accident previously evaluated.

The proposed change does not involve a significant increase in the probability or consequences of an accident previously evaluated but actually enhances the safety of operation of the shutdown cooling system. Lowering the shutdown cooling flow during reduced reactor coolant system inventory operation improves the margin between the required minimum flow and the formation of vortexes in the shutdown cooling suction nozzles. The formation of these vortexes has the potential of air binding the shutdown cooling heat exchanger and pumps of the operating shutdown cooling train.

The boron dilution event was analyzed by ABB-Combustion Engineering to determine if the new flowrates would provide adequate time for operator recognition and correction prior to criticality. The results are as follows:

The limiting (most rapid) case which was analyzed for PVNGS was the case of a dilution during Beginning of Core (BOC), Mode 5 drained conditions, at the maximum charging flow rate. Based upon

, the RCS volume which was assumed (including one train of SDCS) at these conditions, and the time associated with circulation of the RCS at an actual flow of 3400 gpm, the analysis shows that the mixing time is short relative to the time to criticality therefore the dilution would proceed smoothly. It is concluded that there will be sufficient time to recognize and control the dilution before the core reached critical. The case of Mode 5, RCS not drained (with "all other conditions the same) and Mode 6 cases are bounded by the limiting case of drained conditions in Mode 5.

Therefore a shutdown cooling system flowrate of 3400 gpm is

161-03607-WFC/JST November 20, 1990 acceptable in Modes 5 and 6 with respect to a postulated boron dilution event. This evaluation has completed verification according to the C-E QADM.

Standard 2 - Create the possibility of a new or different kind of accident from any accident previously evaluated.

The proposed reduced shutdown cooling flow changes the allowable flow to a value which does not affect the capability to detect and take corrective action for a boron dilution incident while on shutdown cooling. The ability of the shutdown cooling system to remove decay heat and maintain RCS temperature is controlled by operators who vary flow through the shutdown cooling heat exchanger to maintain the specified mode temperature requirements. The proposed minimum flow decreases the possibility of air binding the shutdown cooling system when at mid-loop by minimizing operation with flowrates which could induce significant air entrainment in the shutdown cooling system. The reduced flow does not affect operation of the shutdown cooling system nor involve any system configuration changes. Thus no possibility of a new or different kind of accident from any accident previously evaluated is created.

Standard 3 - Involve a significant reduction in a margin of safety.

The reduction in the minimum flow requirements does not reduce the margin of safety associated with the operation of the shutdown cooling system. The system will still perform within its design bases. The proposed flow will increase the margin of safety by allowing operation of the system further away from the flowrates which produce significant air entrainment in the shutdown cooling system. This minimizes the possibility of rendering one train of shutdown cooling inoperable due to air binding of the pumps or heat exchanger.

The proposed change matches one of the examples given in 51 FR 7751 of amendments that do not involve a significant hazards consideration.

Specifically, the proposed amendment is a change resulting from the application of a small refinement of a previously used calculational model or design method. In this case, the lower minimum flow requirements were the result of a reanalysis of the boron dilution event by ABB-Combustion Engineering. This reanalysis demonstrated the proposed minimum flowrates presented in this amendment request meet the requirements of the original analysis.

E. Safet Anal sis of the Pro osed Chan e Re uest The proposed Technical Specification change will not increase the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the Final Safety Analysis Report (UFSAR). The proposed amendment does not make changes to the design of the facility. The effects of the amendment are lower minimum flow requirements for shutdown cooling operation. The design bases of the shutdown cooling syst: em are not affected by this change.

161-03607-NFC/JST November 20, 1990 The proposed Technical Specification change will not create the possibility of an accident or malfunction of equipment of a different type than any evaluated previously in the UFSAR. This change will minimize the possibility of a loss of shutdown cooling event by increasing the margin between the onset of significant air entrained flow and the minimum required flow for shutdown cooling. There are no equipment changes proposed in thi.s amendment nor any change in the operation of shutdown cooling system other than a change to the Technical Specification minimum flowrate in Modes 5 and 6.

The proposed Technical Specification change will not reduce the margin of safety as defined in the basis for any Technical Specification. The bases for Surveillance Requirements 4.4.1.4. 1. 2, 4 .4 .1.4. 2, 4.9 . 8 . 1, and 4. 9 . 8 . 2 have been reviewed. The requirements stated in the bases sections are still met with the proposed minimum flowrates. The requirement for removal of decay heat is controlled by the operators who maintain RCS temperature by varying the amount of flow bypassing the shutdown cooling heat exchanger. The requirements for boron mixing are also satisfied with the proposed flowrate.

Thus the proposed minimum flowrates do not reduce the margin of safety as defined in the bases for these Technical Specifications.

The proposed amendment to reduce the minimum flow for these Surveillance Requirements has been evaluated by ABB-Combustion Engineering (NSSS vendor) to ensure adequate circulation is maintained to minimize the effects of a boron dilution event and prevent boron stratification. The basis for the 23 minute loop circulation time criteria in the Technical Specification Bases is derived from a concern for avoiding a boron dilution event. A calculation was performed which developed acceptable accident mitigation under the following assumptions:

The SDCS operates in one RCS loop while the other RCS loop is static (i.e., only one train of the SDCS is in operation);

The SDCS is in operation at 4000 gpm; The RCS is full; The fuel in the core is at beginning of core life.

Inherent to the calculation are assumptions regarding fluid mixing within the RCS. At 4000 gpm a full RCS (90,000 gal) will be completely circulated within 23 minutes. This RCS circulation time was determined to be acceptable because it was significantly less than the approximately one hour minimum time for loss of shutdown margin in UFSAR Section 15.4.6. The RCS circulation time at the proposed flowrate of 3400 gpm (actual) is 27 minutes which is also significantly less than the minimum time to loss of shutdown margin. Thus the proposed flowrate of 3400 gpm (actual) would not affect the ability of an operator to recognize and curtail a boron dilution event prior to loss of shutdown margin.

The requirements to remove decay heat are controlled by the operators who must ensure there is sufficient flow through the shutdown cooling heat exchanger to maintain the temperature requirements of the applicable mode. The control of RCS temperature while on shutdown cooling at Palo Verde is accomplished by controlling the amount of flow bypassing the shutdown cooling heat exchanger

161-03607-WFC/JST November 20, 1990 and not by maintaining a minimum system flowrate. Thus the requirement to maintain a minimum system flow is only for prevention of a boron dilution event and does not directly relate to decay heat removal.

ABB-Combustion Engineering has performed a study to determine the minimum flows necessary to maintain RCS temperature at less than 135 degrees Fahrenheit in Mode 6 and concluded that 3400 gpm (actual) will accomplish this 12 days after shutdown with a 105 degree fahrenheit cooling water inlet temperature. In Mode 5, 3400 gpm (actual) will maintain the RCS less than 200 degrees Fahrenheit 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> after reactor shutdown. These calculations assume worst case cooling water inlet conditions and conservative heat exchanger fouling factors, the current capability of the shutdown cooling system is in excess of these assumptions.

F. Environmental Im act Consideration Determination The proposed change request does not involve an unreviewed environmental question because operation of PVNGS Units 1, 2, and 3 in accordance with this change would not:

Result in a significant increase in any adverse environmental impact previously evaluated in the Final Environmental Statement (FES) as modified by the staff's testimony to the Atomic Safety and Licensing Board, Supplements to the FES, Environmental Impact Appraisals, or in any decisions of the Atomic Safety Licensing Board: or

2. Result in a significant change in effluents or power levels; or
3. Result in matters not previously reviewed in the licensing basis for PVNGS which may have a significant environmental impact.

G. Revised Technical S ecification Chan e Pa es See attached pages as typical for each unit. Deletions are noted by strikeout and additions are highlighted and in bold italic print.