ML18038B334: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:~PRIORITY 1y tACCELERATED RIDS PROCESSING)
{{#Wiki_filter:~ PRIORITY 1y tACCELERATED RIDS PROCESSING)
'REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9507170024 DOC.DATE: 95/07/11 NOTARIZED:
                    'REGULATORY INFORMATION DISTRIBUTION SYSTEM         (RIDS)
NO DOCKET g FACIL:50-296 Browns Ferry Nuclear Power Station, Unit 3, Tennessee 05000296 E AUTH.NAME AUTHOR AFFILIATION WALLACE,J.E'.
ACCESSION NBR:9507170024           DOC.DATE:   95/07/11   NOTARIZED: NO             DOCKET g FACIL:50-296 Browns Ferry Nuclear Power Station, Unit 3, Tennessee                 05000296 E AUTH. NAME           AUTHOR AFFILIATION WALLACE,J.E'.         Tennessee Valley Authority MACHON,R.D.           Tennessee Valley Authority RECIP.NAME           RECIPIENT AFFILIATION
Tennessee Valley Authority MACHON,R.D.
Tennessee Valley Authority RECIP.NAME RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 95-001-00:on 950615,under-voltage condition occurred on shutdown boards, automatically starting EDGs.Caused by loss of Athens 161 kV line.EDGs placed in standby&power restored to buses.W/950711 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES RECIPIENT ID CODE/NAME PD2-3-PD INTERNAL: ACRS AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DOPS/OECB NRR/DRCH/HICB NRR/DSSA/SPLB NRR/DSSA/SRXB RGN2 FILE 01 EXTERNAL: L ST LOBBY WARD NOAC MURPHY,G.A NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME WILLIAMS,J.
LER 95-001-00:on 950615,under-voltage         condition occurred     on shutdown boards, automatically starting EDGs.Caused by loss of Athens 161 kV line.EDGs placed in standby & power restored to buses.W/950711       ltr.
EOD~P-D/RA.B LE CE R~NRR/DE/EELB NRR/DIS P/PI PB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DSSA/SPSB/B RES/DSIR/EIB LITCO BRYCE,J H NOAC POORE,W.NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR                 ENCL     SIZE:
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN 5D8 (415-2083)
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T'NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 27 ENCL 27  
NOTES RECIPIENT           COPIES            RECIPIENT          COPIES ID CODE/NAME         LTTR ENCL        ID CODE/NAME        LTTR ENCL PD2-3-PD                 1    1      WILLIAMS,J.              1    1 INTERNAL: ACRS                       1    1        EOD~P-D/RA.B          2    2 AEOD/SPD/RRAB             1    1        LE CE      R~        1    1 NRR/DE/ECGB               1    1      NRR/DE/EELB              1    1 NRR/DE/EMEB              1    1      NRR/DIS P/PI PB          1    1 NRR/DOPS/OECB            1    1      NRR/DRCH/HHFB            1     1 NRR/DRCH/HICB            1    1      NRR/DRCH/HOLB            1    1 NRR/DSSA/SPLB            1    1      NRR/DSSA/SPSB/B         1    1 NRR/DSSA/SRXB            1    1      RES/DSIR/EIB             1    1 RGN2      FILE 01        1    1 EXTERNAL: L ST LOBBY WARD            1    1      LITCO BRYCE,J H         2    2 NOAC MURPHY,G.A          1    1      NOAC POORE,W.           1     1 NRC PDR                  1     1     NUDOCS FULL TXT          1     1 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN 5D8 (415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T 'NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR             27   ENCL     27


Te;lessee/a'eq~.."s","-"s;~"=e=".~"-="", ew:..~"a-a"=o e 2"CC R.D.iRick>Machon V e~.es"e"~"v"s=~/i"oa.-"a" July 11, 1995 U.S.Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C.20555  
Te;lessee /a'eq ~.."s", "-"s; ~" =e =".~ "-="", ew:.. ~"a-a "=o e 2 "CC R. D. iRick> Machon V e~.es "e" ~ "v   "s=~/i "oa.-"a" July 11,       1995 U.S.         Nuclear Regulatory Commission                                           10 CFR 50.73 ATTN: Document Control Desk Washington, D.C. 20555


==Dear Sir:==
==Dear       Sir:==
10 CFR 50.73 BROWNS FERRY NUCLEAR'LANT (BFN)-UNITS 1~,2I AND 3-DOCKET NOS~50 259~50 260I AND 50 296 FACILITY OPERATING LICENSE DPR-33I 52~AND 68-LICENSEE EVENT REPORT 50-296/95001 The enclosed report provides details concerning an event on June 15, 1995, in which the Unit 3 A and B diesel generators auto-started as a result of an under-voltage condition.
 
Thi.s was a direct result of an airplane severing the, Athens 161kV phase C transmission line.This report is subm'itted in accordance with 10 CFR 50.73 (a)(2).(iv) as a condition that resulted in the automatic actuation of an engineered safety feature.Sincerely, R.D.M on Site Vi e President Enclosure cc: See page 2 9507170024 9507i}PDR ADQCK 05000296 8 PAR  
BROWNS FERRY               NUCLEAR'LANT (BFN)                       - UNITS 1~,2I AND 3 - DOCKET NOS ~         50 259~         50 260I AND 50 296                       FACILITY OPERATING LICENSE DPR-33I 52~ AND 68 LICENSEE EVENT REPORT 50-296/95001 The enclosed report provides details concerning an event on June 15, 1995, in which the Unit 3 A and B diesel generators auto-started               as a result of an under-voltage condition. Thi.s was a         direct result of an airplane severing the, Athens 161kV phase C transmission line.
This report is subm'itted in accordance with 10 CFR 50.73 (a)(2).(iv) as a condition that resulted in the automatic actuation of               an engineered                 safety feature.
Sincerely, R. D.       M       on Site Vi         e   President Enclosure cc: See page                 2 9507170024 9507i}
PDR       ADQCK 05000296 8                               PAR
 
U.S. Nuclear Regulatory Commission Page  2 July 11,  1995 Enclosure cc (Enclosure):
INPO Records Center Suite    1500 1100    Circle 75 Parkway Atlanta, Georgia 30339 Paul Krippner American Nuclear Insurers Town Center, Suite 300S 29 South Main Street West    Hartford, Connecticut  06107 NRC Resident Inspector Browns Ferry Nuclear Plant Route 12, Box 637 Athens, Alabama      35611 Regional Administrator U. S. Nuclear Regulatory Commission Region 1'01 II Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 Mr. J. F. Williams, Project Manager U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland      20852
 
/
4I 0
 
U.S. Nuclear Regulatory Commission Page    3 July 11,      1995 PS SAW JEW:MTN Enclosure cc (Enclosure):
C. W. Beasley, PAB 1B-BFN P. P. Carier, BR 4G-C L. S. Clardy, CFC 1D-BFN C. T. Dexter, BFT 3A-BFN
: 0. D. Kingsley, LP 6A-C J. P. Maciejewski, LP 3B-C J. Scott Martin, PMC 1D-BFN T. J. McGrath, LP 3B-C M. 0. Medford, LP 3B-C G. D. Pierce, PEB 1B-BFN E. Preston, POB 2C-BFN C. M. Root, CFC 1D-BFN R. H. Shell, 0&PS 4C-SQN T. D. Shriver, PAB 1A-BFN H. L. Williams, EDB 1A-BFN
: 0. J. Zeringue, LP 3B-C RIMS,      WT 3B-K a:Uers5500l.jew
 
l MRC FGRM  366                                    U.S    NUCLEAR REGULATORY COMMISSION                  APPROVED BY CNB NO      3150-0104 (5-92)                                                                                                            EXPIRES  5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS IHFORMATIOH COLLECTION REQUEST: 50.0 HRS.
LZCENSEE EVENT REPORT                        (LER)                        FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH
                                                                                              <MMBB    7714),    U.ST        NUCLEAR      REGULATORY for required    nunber of  digits/characters for    each  block)        COMMISSION,    WASHINGTON, DC 20555-0001        AHD TO (See reverse                                                                              THE PAPERWORK REDUCTION PROJECT            (3130-0104),
OFFICE OF MANAGEMENT AND BUDGET, WASHINGTOH, DC 20503.
FACILITY NAME    (1)                                                                        DOCKET NQ(BER    (2)                        PAGE (3)
Browns        Ferr          Nuclear Plant                BFN      Unit      3                        05000296                        1 OF 4 TITLE  (4) Loss of    a 161Kv    line  caused the actuation of the Engineered Safety Feature (ESF) system.
EVENT DATE    (5)                  LER MIMIBER (6)                REPORT DATE  (7)                OTHER  FACILITIES INVOLVED 8)
SEQUENTIAL      REVISION                            FACILITY  NAME    HA              DOCKET NUMBER MONTH    DAY      YEAR      YEAR                                  MONTH    DAY    YEAR NUMBER        NUMBER FACILITY  NAME    NA              DOCKET NUMBER 06      15        95        95            001            00        07      11 OPERATING                  THIS REPORT IS SUBMITTED PURSUANT TO'THE REQUIREMENTS OF 10          CFR: (Check one or        mor e    11 M(X)E (9)        N          20.402(b)                          20.405(c)                          50.73(a)(2)(iv)              73.71(b) 20.405(a)(1)(i)                    50.36(c)(1)                        50.73(a)(2)(v)                73.71(c)
POWER 000                                            50.36(c)(2)                        50.73(a)(2)(vii)
LEVEL  (10)                  20.405(a)(1)(ii)                                                                                    OTHER 20.405(a)(1)(iii)                  50.73(a)(2)(i)(B)                  50 '3(a)(2)(viii)(A)      (Specify in 50.73(a)(2)(ii)                    50.73(a)(2)(vlii)(B)      Abstract below 20.405(a)(1)(iv)                                                                                and in Text, 20.405<a)(1)(v)                    50.73(a)(2)(iii)                  50.73(a)(2)(x)            NRC  Form 366A LICENSEE COHTACT FOR THIS LER      (12)
NAME                                                                                                  TELEPHOHE NUMBER    (Include Area    Code)
James      E.      Wallace, Compliance Licensing Engineer                                              (205)729-7874 C(NPLETE ONE LIME FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT              (13)
REPORTABLE                                                                      REPORTABLE CAUSE    SYSTEM        COMPONENT    MAHUFACTURER                              CAUSE      SYSTEM      COMPONENT      MANUFACTURER TO HPRDS                                                                        TO NPRDS SUPPLEMENTAL REPORT EXPECTED      (14)                                                        MOM'IH      DAY      YEAR EXPECTED YES                                                                                            SUBMISSION
                                                                      )(  NO DATE (15)
(If yes,  complete    EXPECTED SUBMISSION    DATE).
ABSTRACT    (Limit to    1400 spaces,  i.e., approximately 15 single-spaced typewritten lines) (16)
On June 15, 1995, at 1129 hours, the 3A and 3B Emergency Diesel Generators automatically started when an under-voltage condition occurred on the 3EA and 3EB 4kV shutdown boards.
This under-voltage condition caused the loss of the 3A reactor protection system further resulting in the auto-starts of the standby gas. treatment and control room emergency ventilation systems. At the time of this event, Unit 3 was defueled and inanda Unit                                                long term Main Bank transformer outage.                      Unit 2 was operating at 100 percent power,                                            1 was shutdown and defueled.                    The  event    occurred      when    an  airplane        cut    the  Athens    16lkV    phase    C transmission line. Corrective actions were taken to restore the plant systems to standby readiness'o additional corrective actionsa will,                                    be taken.        This event is reportable in condition that resulted in an automatic accordance with 10 CFR 50.73 (a)(2)(iv) as actuation of the ESF system.
NRC FORM        (      )
 
0 NRC FORll  366A        U.S    NUCLEAR REGULATORY CON(I SSI ON                      APPROVED BY (H(B MO. 3150-0104 (5-92)                                                                                        EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS ~        FORWARD COMMENTS REGARDIHG BURDEN ESTIMATE TO THE INFORMATION AHD RECORDS MANAGEMENT BRANCH (HNBB 7714),      U.S. NUCLEAR REGULATORY COMMISSION/
                'LICENSEE EVENT REPORT                              WASHINGTON, DC 20555.0001,      AND TO THE PAPERWORK REDUCTION TEXT CONTINUATION                              PROJECT  (3150-0104), OFFICE OF HANAGEHEHT AND BUDGET, WASHINGTON  DC  20503 FACILITY NAME  (1)              DOCKET NIH(BER (2)                    LER MWBER    (6)                , PAGE (3)
YEAR      SEQUENT I AL        REVISION NUMBER            NUMBER Browns Ferry          Unit    3                05000296              95            001                00                2  of 4 TEXT  If more  s ace is r uired    use additionaI co ies of    NRC  Form 366A    (17)
I ~      PLANT CONDITIONS At the time this event occurred, Unit 3 and Unit 1 were shutdown and defueled. Unit 2 was operating at 100 percent power.
DESCRIPTION OF EVENT Event On    June 15, 1995,        at  1129 hours,        Unit    3  experienced        a  loss of offsite power to common station service transformer A [EB),
which was being supplied by the Athens 161kV [FK) transmission line. This condition. occurred when an airplane severed the Athens 161kV phase          C  transmission line.
As    designed,    the start buses 1A and 2A transferred to an alternate      power source (Trinity 161kV line), and attempted to reconnect to the Athens line. However, because the fault on the Athens line had not cleared, the alternate feeder breaker [BKR) was locked out resulting in an under-voltage condition on start buses 1A and 2A.
When    the under-voltage condition occurred, the 3EA and 3EB 4kV shutdown boards [EB) de-energized.                      As a result, the 3A and 3B Emergency Diesel Generators (EDGs) [EK) started and tied to the 4kV shutdown boards.              The 3A reactor protection system (RPS)
[JC) de-energized and caused the Unit 3 reactor zone ventilation
[VB] and refueling zone ventilation [VA] systems to isolate; and the standby gas treatment (SGT) system [BH), and control room emergency ventilation (CREV)'VZ) train A to initiate. The emergency equipment cooling water [BI] pumps started to supply cooling water to the EDGs. All systems responded as expected.
At 1207 hours,        start bus 1A was manually transferred .to an alternate      power supply to re-energize the 4kV 3A unit board, which re-energized the 3EA and 3EB 4kV shutdown boards. At 1245 hours, Unit 3 EDGs were returned to standby readiness since the Trinity 16lkV transmission line,was supplying                          power to Unit 3.
At 1300 hours, SGT was secured, and at 1305 hours, CREV train A was    secured.
This event is reportable in accordance with                          10 CFR 50.73 (a)(2)(iv)    as a condition that            resulted in        an automatic actuation      of an ESF system.
B~      Ino erable Structures              Com  onents      or  S  stems    that Contributed to the Event:
None.
 
Ih NRC FORli 366A        U.S. NUCLEAR REGULATORY CCHHISSION                        APPRMD    BY NB  NO. 3150-0104 (5-92)                                                                                    EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY llITH THIS INFORHATION COLLECT IOH REQUEST: 50.0 HRS ~      FORlJARD COMMENTS REGARDING BURDEN ESTIMATE TO tHE INFORMATION AND RECORDS MANAGEMENT BRANCK (HNBB 7714),    U.S. NUCLEAR REGULATORY COMMISSION/
LICENSEE EVENT REPORT                            llASNINGTON, DC 20555-0001, AND TO THE PAPERNORK REDUCTION TEXT CONTINUATION                              PROJECT    (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, IIASHINGTON DC 20503 FACILITY NAME (1)              DOCKET NUMBER (2)                    LER NLIUIER (6)                  PAGE (3)
YEAR      SEQUENTIAL        REVISION NUMBER          NUMBER Browns    Ferry Unit      3                  05000296              95          001              00                3  of 4 TEXT  If more s ace is r uired    use  additionat co ies of  NRC  Form 366A  (17)
C~      Dates and      A    roximate Times of Ma'or Occurrences:
June 15, 1995 at 1129 hours          CDT          An    airplane severed phase            C  of the Athens 161kV transmission              line,    EDGs started and tied to boards at  1207 hours CDT                  TVA    manually transferred 1A start bus to its alternate        power supply (Trinity 161kV)      to re-energize the Unit            3  4kV 3A unit board at  1245 hours CDT                  Unit    3 EDGs    were returned        to standby readiness at  1300 hours CDT                  SGT    system secured at  1305 hours CDT                  CREV    train  A  secured at  1412 hours CDT                  TVA    provided    a 10 CFR    50.72(b)(2)(ii) notification to          NRC  Operations Center D~      Other    S  stems    or Secondar        Functions Affected:
None.
E.      Method    of Discover This condition was discovered when the control room Operations personnel [licensed, utility) received alarms and indicators that start buses 1A and 2A were de-energized and the EDGs had auto-started.
F.      0 erator Actions:
Operations personnel responded to the event in accordance with approved procedures.              Start buses 1A and 2A were repowered when they were manually placed on, their alternate feeder breakers.
G.      Safet      S  stem Res onsesl All safety        systems responded            as designed      for this type of event.
CAUSE OF THE EVENT Immediate Cause:
The immediate cause of            the event was the loss of the Athens 161kV line that created            an under-voltage condition.
 
0 NRC FORM  366A        U.S. NUCLEAR REGULATORY CQOIISSION                      APPROVED BY OMB NO. 3150-0104 (5-92)                                                                                    EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY IJITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.      FORllARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS HANAGEMENT BRANCH (MNBB 7714),    U.S. NUCLEAR REGULATORY COMMISSION, LICENSEE EVENT REPORT                            .WASHINGTON, DC 20555-0001,    AND TO THE PAPERlQRK REDUCTION TEXT CONTINUATION                              PROJECT  (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, NASHINGTOH DC 20503 FACILITY NAME  (1)              DOCKET NUMBER (2)                  LER NUMBER (6)                  PAGE (3)
YEAR      SEOUENTIAL        REVISION NUHBER          NUMBER Browns      Ferry Unit      3                05000296            95          001              00              4  of 4 TEXT  If more  s  ce is r uired    use  additional co ies  of NRC  Form 366A  (17)
B.      Root Cause:
This event occurred when the Athens 161kV line was inadvertently severed by an airplane.
IV  ~        ANALYSIS OF THE EVENT In this event, plant safety systems and associated components performed as designed.              Operations personnel immediately identified the cause of the ESF actuation and took appropriate corrective actions to restore the plant systems to standby readiness. Therefore, this event did not affect the health and safety of plant personnel and the public.
Had  Unit 3 been at full power operation providing power to the grid, these    ESF actuations would not have occurred.                      Namely, at full power operation, Unit 3 is aligned to its Unit Station Transformer, and the Athens 161kV transmission line is not aligned to supply power to the 4kV shutdown boards.
V.        CORRECTIVE ACTIONS A.      Immediate Corrective Actions:
Operations personnel restored power to the 1A and 2A start buses and subsequently placed the EDGs in standby readiness.                              A problem evaluation report (BFPER 950725) was generated to document this event.            Systems were returned to a standby readiness condition.
B.      Corrective Actions to Prevent Recurrence:
None.
VI+        ADDITIONAL INFORMATION A~      Failed    Com  onents:
None.
B~      Previous      LERs on    Similar Events:
None.
VII.        COMMITMENTS None.
Energy Industry            Identification System (EIIS) system                  and component codes are identified in the text with brackets (e.g., (XX]).


U.S.Nuclear Regulatory Commission Page 2 July 11, 1995 Enclosure cc (Enclosure):
INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 Paul Krippner American Nuclear Insurers Town Center, Suite 300S 29 South Main Street West Hartford, Connecticut 06107 NRC Resident Inspector Browns Ferry Nuclear Plant Route 12, Box 637 Athens, Alabama 35611 Regional Administrator U.S.Nuclear Regulatory Commission Region II 1'01 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 Mr.J.F.Williams, Project Manager U.S.Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852
/4I 0 U.S.Nuclear Regulatory Commission Page 3 July 11, 1995 PS SAW JEW:MTN Enclosure cc (Enclosure):
C.W.Beasley, PAB 1B-BFN P.P.Carier, BR 4G-C L.S.Clardy, CFC 1D-BFN C.T.Dexter, BFT 3A-BFN 0.D.Kingsley, LP 6A-C J.P.Maciejewski, LP 3B-C J.Scott Martin, PMC 1D-BFN T.J.McGrath, LP 3B-C M.0.Medford, LP 3B-C G.D.Pierce, PEB 1B-BFN E.Preston, POB 2C-BFN C.M.Root, CFC 1D-BFN R.H.Shell, 0&PS 4C-SQN T.D.Shriver, PAB 1A-BFN H.L.Williams, EDB 1A-BFN 0.J.Zeringue, LP 3B-C RIMS, WT 3B-K a:Uers5500l.jew l
MRC FGRM 366 (5-92)U.S NUCLEAR REGULATORY COMMISSION APPROVED BY CNB NO 3150-0104 EXPIRES 5/31/95 LZCENSEE EVENT REPORT (LER)(See reverse for required nunber of digits/characters for each block)ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS IHFORMATIOH COLLECTION REQUEST: 50.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH<MMBB 7714), U.ST NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001 AHD TO THE PAPERWORK REDUCTION PROJECT (3130-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTOH, DC 20503.FACILITY NAME (1)Browns Ferr Nuclear Plant BFN Unit 3 DOCKET NQ(BER (2)05000296 PAGE (3)1 OF 4 TITLE (4)Loss of a 161Kv line caused the actuation of the Engineered Safety Feature (ESF)system.MONTH 06 DAY YEAR 15 95 EVENT DATE (5)YEAR 95 LER MIMIBER (6)SEQUENTIAL NUMBER 001 REVISION NUMBER 00 MONTH DAY 07 11 YEAR REPORT DATE (7)FACILITY NAME HA DOCKET NUMBER FACILITY NAME NA DOCKET NUMBER OTHER FACILITIES INVOLVED 8)OPERATING M(X)E (9)POWER LEVEL (10)N 000 THIS REPORT IS SUBMITTED PURSUANT 20.402(b)20.405(a)(1)(i) 20.405(a)(1)(ii) 20.405(a)(1)(iii) 20.405(a)(1)(iv) 20.405<a)(1)(v) 20.405(c)50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(i)(B) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50'3(a)(2)(viii)(A) 50.73(a)(2)(vlii)(B) 50.73(a)(2)(x)
TO'THE REQUIREMENTS OF 10 CFR: (Check one or mor e 11 73.71(b)73.71(c)OTHER (Specify in Abstract below and in Text, NRC Form 366A LICENSEE COHTACT FOR THIS LER (12)NAME James E.Wallace, Compliance Licensing Engineer TELEPHOHE NUMBER (Include Area Code)(205)729-7874 C(NPLETE ONE LIME FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MAHUFACTURER REPORTABLE TO HPRDS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (If yes, complete EXPECTED SUBMISSION DATE).)(NO EXPECTED SUBMISSION DATE (15)MOM'IH DAY YEAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)(16)On June 15, 1995, at 1129 hours, the 3A and 3B Emergency Diesel Generators automatically started when an under-voltage condition occurred on the 3EA and 3EB 4kV shutdown boards.This under-voltage condition caused the loss of the 3A reactor protection system further resulting in the auto-starts of the standby gas.treatment and control room emergency ventilation systems.At the time of this event, Unit 3 was defueled and in a long term Main Bank transformer outage.Unit 2 was operating at 100 percent power, and Unit 1 was shutdown and defueled.The event occurred when an airplane cut the Athens 16lkV phase C transmission line.Corrective actions were taken to restore the plant systems to standby readiness'o additional corrective actions will, be taken.This event is reportable in accordance with 10 CFR 50.73 (a)(2)(iv) as a condition that resulted in an automatic actuation of the ESF system.NRC FORM ()
0 NRC FORll 366A (5-92)U.S NUCLEAR REGULATORY CON(I SSI ON'LICENSEE EVENT REPORT TEXT CONTINUATION APPROVED BY (H(B MO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS~FORWARD COMMENTS REGARDIHG BURDEN ESTIMATE TO THE INFORMATION AHD RECORDS MANAGEMENT BRANCH (HNBB 7714), U.S.NUCLEAR REGULATORY COMMISSION/
WASHINGTON, DC 20555.0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF HANAGEHEHT AND BUDGET, WASHINGTON DC 20503 FACILITY NAME (1)Browns Ferry Unit 3 DOCKET NIH(BER (2)05000296 YEAR 95 LER MWBER (6)SEQUENT I AL NUMBER 001 REVISION NUMBER 00 , PAGE (3)2 of 4 TEXT If more s ace is r uired use additionaI co ies of NRC Form 366A (17)I~PLANT CONDITIONS At the time this event occurred, Unit 3 and Unit 1 were shutdown and defueled.Unit 2 was operating at 100 percent power.DESCRIPTION OF EVENT Event On June 15, 1995, at 1129 hours, Unit 3 experienced a loss of offsite power to common station service transformer A[EB), which was being supplied by the Athens 161kV[FK)transmission line.This condition.
occurred when an airplane severed the Athens 161kV phase C transmission line.As designed, the start buses 1A and 2A transferred to an alternate power source (Trinity 161kV line), and attempted to reconnect to the Athens line.However, because the fault on the Athens line had not cleared, the alternate feeder breaker[BKR)was locked out resulting in an under-voltage condition on start buses 1A and 2A.When the under-voltage condition occurred, the 3EA and 3EB 4kV shutdown boards[EB)de-energized.
As a result, the 3A and 3B Emergency Diesel Generators (EDGs)[EK)started and tied to the 4kV shutdown boards.The 3A reactor protection system (RPS)[JC)de-energized and caused the Unit 3 reactor zone ventilation
[VB]and refueling zone ventilation
[VA]systems to isolate;and the standby gas treatment (SGT)system[BH), and control room emergency ventilation (CREV)'VZ) train A to initiate.The emergency equipment cooling water[BI]pumps started to supply cooling water to the EDGs.All systems responded as expected.At 1207 hours, start bus 1A was manually transferred.to an alternate power supply to re-energize the 4kV 3A unit board, which re-energized the 3EA and 3EB 4kV shutdown boards.At 1245 hours, Unit 3 EDGs were returned to standby readiness since the Trinity 16lkV transmission line,was supplying power to Unit 3.At 1300 hours, SGT was secured, and at 1305 hours, CREV train A was secured.B~This event is reportable in accordance with 10 CFR 50.73 (a)(2)(iv) as a condition that resulted in an automatic actuation of an ESF system.Ino erable Structures Com onents or S stems that Contributed to the Event: None.
Ih NRC FORli 366A (5-92)U.S.NUCLEAR REGULATORY CCHHISSION LICENSEE EVENT REPORT TEXT CONTINUATION APPRMD BY NB NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY llITH THIS INFORHATION COLLECT IOH REQUEST: 50.0 HRS~FORlJARD COMMENTS REGARDING BURDEN ESTIMATE TO tHE INFORMATION AND RECORDS MANAGEMENT BRANCK (HNBB 7714), U.S.NUCLEAR REGULATORY COMMISSION/
llASNINGTON, DC 20555-0001, AND TO THE PAPERNORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, IIASHINGTON DC 20503 FACILITY NAME (1)Browns Ferry Unit 3 DOCKET NUMBER (2)05000296 YEAR 95 LER NLIUIER (6)SEQUENTIAL NUMBER 001 REVISION NUMBER 00 PAGE (3)3 of 4 TEXT If more s ace is r uired use additionat co ies of NRC Form 366A (17)C~Dates and A roximate Times of Ma'or Occurrences:
June 15, 1995 at 1129 hours CDT An airplane severed phase C of the Athens 161kV transmission line, EDGs started and tied to boards at 1207 hours CDT TVA manually transferred 1A start bus to its alternate power supply (Trinity 161kV)to re-energize the Unit 3 4kV 3A unit board at 1245 hours CDT Unit 3 EDGs were returned to standby readiness at 1300 hours CDT at 1305 hours CDT at 1412 hours CDT SGT system secured CREV train A secured TVA provided a 10 CFR 50.72(b)(2)(ii) notification to NRC Operations Center D~Other S stems or Secondar Functions Affected: E.None.Method of Discover This condition was discovered when the control room Operations personnel[licensed, utility)received alarms and indicators that start buses 1A and 2A were de-energized and the EDGs had auto-started.
F.0 erator Actions: Operations personnel responded to the event in accordance with approved procedures.
Start buses 1A and 2A were repowered when they were manually placed on, their alternate feeder breakers.G.Safet S stem Res onsesl All safety systems responded as designed for this type of event.CAUSE OF THE EVENT Immediate Cause: The immediate cause of the event was the loss of the Athens 161kV line that created an under-voltage condition.
0 NRC FORM 366A (5-92)U.S.NUCLEAR REGULATORY CQOIISSION LICENSEE EVENT REPORT TEXT CONTINUATION APPROVED BY OMB NO.3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY IJITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.FORllARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS HANAGEMENT BRANCH (MNBB 7714), U.S.NUCLEAR REGULATORY COMMISSION,.WASHINGTON, DC 20555-0001, AND TO THE PAPERlQRK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, NASHINGTOH DC 20503 FACILITY NAME (1)Browns Ferry Unit 3 DOCKET NUMBER (2)05000296 LER NUMBER (6)YEAR SEOUENTIAL REVISION NUHBER NUMBER 95 001 00 PAGE (3)4 of 4 TEXT If more s ce is r uired use additional co ies of NRC Form 366A (17)B.Root Cause: This event occurred when the Athens 161kV line was inadvertently severed by an airplane.IV~ANALYSIS OF THE EVENT In this event, plant safety systems and associated components performed as designed.Operations personnel immediately identified the cause of the ESF actuation and took appropriate corrective actions to restore the plant systems to standby readiness.
Therefore, this event did not affect the health and safety of plant personnel and the public.Had Unit 3 been at full power operation providing power to the grid, these ESF actuations would not have occurred.Namely, at full power operation, Unit 3 is aligned to its Unit Station Transformer, and the Athens 161kV transmission line is not aligned to supply power to the 4kV shutdown boards.V.CORRECTIVE ACTIONS A.Immediate Corrective Actions: Operations personnel restored power to the 1A and 2A start buses and subsequently placed the EDGs in standby readiness.
A problem evaluation report (BFPER 950725)was generated to document this event.Systems were returned to a standby readiness condition.
B.Corrective Actions to Prevent Recurrence:
None.VI+ADDITIONAL INFORMATION A~Failed Com onents: B~None.Previous LERs on Similar Events: None.VII.COMMITMENTS None.Energy Industry Identification System (EIIS)system and component codes are identified in the text with brackets (e.g., (XX]).
'l}}
'l}}

Latest revision as of 23:27, 21 October 2019

LER 95-001-00:on 950615,under-voltage Condition Occurred on Shutdown Boards,Automatically Starting Edgs.Caused by Loss of Athens 161 Kv Line.Edgs Placed in Standby & Power Restored to buses.W/950711 Ltr
ML18038B334
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 07/11/1995
From: Machon R, Jay Wallace
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-95-001-03, LER-95-1-3, NUDOCS 9507170024
Download: ML18038B334 (16)


Text

~ PRIORITY 1y tACCELERATED RIDS PROCESSING)

'REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9507170024 DOC.DATE: 95/07/11 NOTARIZED: NO DOCKET g FACIL:50-296 Browns Ferry Nuclear Power Station, Unit 3, Tennessee 05000296 E AUTH. NAME AUTHOR AFFILIATION WALLACE,J.E'. Tennessee Valley Authority MACHON,R.D. Tennessee Valley Authority RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 95-001-00:on 950615,under-voltage condition occurred on shutdown boards, automatically starting EDGs.Caused by loss of Athens 161 kV line.EDGs placed in standby & power restored to buses.W/950711 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-3-PD 1 1 WILLIAMS,J. 1 1 INTERNAL: ACRS 1 1 EOD~P-D/RA.B 2 2 AEOD/SPD/RRAB 1 1 LE CE R~ 1 1 NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DIS P/PI PB 1 1 NRR/DOPS/OECB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SPSB/B 1 1 NRR/DSSA/SRXB 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 2 2 NOAC MURPHY,G.A 1 1 NOAC POORE,W. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN 5D8 (415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T 'NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 27 ENCL 27

Te;lessee /a'eq ~.."s", "-"s; ~" =e =".~ "-="", ew:.. ~"a-a "=o e 2 "CC R. D. iRick> Machon V e~.es "e" ~ "v "s=~/i "oa.-"a" July 11, 1995 U.S. Nuclear Regulatory Commission 10 CFR 50.73 ATTN: Document Control Desk Washington, D.C. 20555

Dear Sir:

BROWNS FERRY NUCLEAR'LANT (BFN) - UNITS 1~,2I AND 3 - DOCKET NOS ~ 50 259~ 50 260I AND 50 296 FACILITY OPERATING LICENSE DPR-33I 52~ AND 68 LICENSEE EVENT REPORT 50-296/95001 The enclosed report provides details concerning an event on June 15, 1995, in which the Unit 3 A and B diesel generators auto-started as a result of an under-voltage condition. Thi.s was a direct result of an airplane severing the, Athens 161kV phase C transmission line.

This report is subm'itted in accordance with 10 CFR 50.73 (a)(2).(iv) as a condition that resulted in the automatic actuation of an engineered safety feature.

Sincerely, R. D. M on Site Vi e President Enclosure cc: See page 2 9507170024 9507i}

PDR ADQCK 05000296 8 PAR

U.S. Nuclear Regulatory Commission Page 2 July 11, 1995 Enclosure cc (Enclosure):

INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 Paul Krippner American Nuclear Insurers Town Center, Suite 300S 29 South Main Street West Hartford, Connecticut 06107 NRC Resident Inspector Browns Ferry Nuclear Plant Route 12, Box 637 Athens, Alabama 35611 Regional Administrator U. S. Nuclear Regulatory Commission Region 1'01 II Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 Mr. J. F. Williams, Project Manager U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852

/

4I 0

U.S. Nuclear Regulatory Commission Page 3 July 11, 1995 PS SAW JEW:MTN Enclosure cc (Enclosure):

C. W. Beasley, PAB 1B-BFN P. P. Carier, BR 4G-C L. S. Clardy, CFC 1D-BFN C. T. Dexter, BFT 3A-BFN

0. D. Kingsley, LP 6A-C J. P. Maciejewski, LP 3B-C J. Scott Martin, PMC 1D-BFN T. J. McGrath, LP 3B-C M. 0. Medford, LP 3B-C G. D. Pierce, PEB 1B-BFN E. Preston, POB 2C-BFN C. M. Root, CFC 1D-BFN R. H. Shell, 0&PS 4C-SQN T. D. Shriver, PAB 1A-BFN H. L. Williams, EDB 1A-BFN
0. J. Zeringue, LP 3B-C RIMS, WT 3B-K a:Uers5500l.jew

l MRC FGRM 366 U.S NUCLEAR REGULATORY COMMISSION APPROVED BY CNB NO 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS IHFORMATIOH COLLECTION REQUEST: 50.0 HRS.

LZCENSEE EVENT REPORT (LER) FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH

<MMBB 7714), U.ST NUCLEAR REGULATORY for required nunber of digits/characters for each block) COMMISSION, WASHINGTON, DC 20555-0001 AHD TO (See reverse THE PAPERWORK REDUCTION PROJECT (3130-0104),

OFFICE OF MANAGEMENT AND BUDGET, WASHINGTOH, DC 20503.

FACILITY NAME (1) DOCKET NQ(BER (2) PAGE (3)

Browns Ferr Nuclear Plant BFN Unit 3 05000296 1 OF 4 TITLE (4) Loss of a 161Kv line caused the actuation of the Engineered Safety Feature (ESF) system.

EVENT DATE (5) LER MIMIBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED 8)

SEQUENTIAL REVISION FACILITY NAME HA DOCKET NUMBER MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER FACILITY NAME NA DOCKET NUMBER 06 15 95 95 001 00 07 11 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO'THE REQUIREMENTS OF 10 CFR: (Check one or mor e 11 M(X)E (9) N 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b) 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)

POWER 000 50.36(c)(2) 50.73(a)(2)(vii)

LEVEL (10) 20.405(a)(1)(ii) OTHER 20.405(a)(1)(iii) 50.73(a)(2)(i)(B) 50 '3(a)(2)(viii)(A) (Specify in 50.73(a)(2)(ii) 50.73(a)(2)(vlii)(B) Abstract below 20.405(a)(1)(iv) and in Text, 20.405<a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) NRC Form 366A LICENSEE COHTACT FOR THIS LER (12)

NAME TELEPHOHE NUMBER (Include Area Code)

James E. Wallace, Compliance Licensing Engineer (205)729-7874 C(NPLETE ONE LIME FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

REPORTABLE REPORTABLE CAUSE SYSTEM COMPONENT MAHUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER TO HPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) MOM'IH DAY YEAR EXPECTED YES SUBMISSION

)( NO DATE (15)

(If yes, complete EXPECTED SUBMISSION DATE).

ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)

On June 15, 1995, at 1129 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.295845e-4 months <br />, the 3A and 3B Emergency Diesel Generators automatically started when an under-voltage condition occurred on the 3EA and 3EB 4kV shutdown boards.

This under-voltage condition caused the loss of the 3A reactor protection system further resulting in the auto-starts of the standby gas. treatment and control room emergency ventilation systems. At the time of this event, Unit 3 was defueled and inanda Unit long term Main Bank transformer outage. Unit 2 was operating at 100 percent power, 1 was shutdown and defueled. The event occurred when an airplane cut the Athens 16lkV phase C transmission line. Corrective actions were taken to restore the plant systems to standby readiness'o additional corrective actionsa will, be taken. This event is reportable in condition that resulted in an automatic accordance with 10 CFR 50.73 (a)(2)(iv) as actuation of the ESF system.

NRC FORM ( )

0 NRC FORll 366A U.S NUCLEAR REGULATORY CON(I SSI ON APPROVED BY (H(B MO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS ~ FORWARD COMMENTS REGARDIHG BURDEN ESTIMATE TO THE INFORMATION AHD RECORDS MANAGEMENT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION/

'LICENSEE EVENT REPORT WASHINGTON, DC 20555.0001, AND TO THE PAPERWORK REDUCTION TEXT CONTINUATION PROJECT (3150-0104), OFFICE OF HANAGEHEHT AND BUDGET, WASHINGTON DC 20503 FACILITY NAME (1) DOCKET NIH(BER (2) LER MWBER (6) , PAGE (3)

YEAR SEQUENT I AL REVISION NUMBER NUMBER Browns Ferry Unit 3 05000296 95 001 00 2 of 4 TEXT If more s ace is r uired use additionaI co ies of NRC Form 366A (17)

I ~ PLANT CONDITIONS At the time this event occurred, Unit 3 and Unit 1 were shutdown and defueled. Unit 2 was operating at 100 percent power.

DESCRIPTION OF EVENT Event On June 15, 1995, at 1129 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.295845e-4 months <br />, Unit 3 experienced a loss of offsite power to common station service transformer A [EB),

which was being supplied by the Athens 161kV [FK) transmission line. This condition. occurred when an airplane severed the Athens 161kV phase C transmission line.

As designed, the start buses 1A and 2A transferred to an alternate power source (Trinity 161kV line), and attempted to reconnect to the Athens line. However, because the fault on the Athens line had not cleared, the alternate feeder breaker [BKR) was locked out resulting in an under-voltage condition on start buses 1A and 2A.

When the under-voltage condition occurred, the 3EA and 3EB 4kV shutdown boards [EB) de-energized. As a result, the 3A and 3B Emergency Diesel Generators (EDGs) [EK) started and tied to the 4kV shutdown boards. The 3A reactor protection system (RPS)

[JC) de-energized and caused the Unit 3 reactor zone ventilation

[VB] and refueling zone ventilation [VA] systems to isolate; and the standby gas treatment (SGT) system [BH), and control room emergency ventilation (CREV)'VZ) train A to initiate. The emergency equipment cooling water [BI] pumps started to supply cooling water to the EDGs. All systems responded as expected.

At 1207 hours0.014 days <br />0.335 hours <br />0.002 weeks <br />4.592635e-4 months <br />, start bus 1A was manually transferred .to an alternate power supply to re-energize the 4kV 3A unit board, which re-energized the 3EA and 3EB 4kV shutdown boards. At 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br />, Unit 3 EDGs were returned to standby readiness since the Trinity 16lkV transmission line,was supplying power to Unit 3.

At 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br />, SGT was secured, and at 1305 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.965525e-4 months <br />, CREV train A was secured.

This event is reportable in accordance with 10 CFR 50.73 (a)(2)(iv) as a condition that resulted in an automatic actuation of an ESF system.

B~ Ino erable Structures Com onents or S stems that Contributed to the Event:

None.

Ih NRC FORli 366A U.S. NUCLEAR REGULATORY CCHHISSION APPRMD BY NB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY llITH THIS INFORHATION COLLECT IOH REQUEST: 50.0 HRS ~ FORlJARD COMMENTS REGARDING BURDEN ESTIMATE TO tHE INFORMATION AND RECORDS MANAGEMENT BRANCK (HNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION/

LICENSEE EVENT REPORT llASNINGTON, DC 20555-0001, AND TO THE PAPERNORK REDUCTION TEXT CONTINUATION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, IIASHINGTON DC 20503 FACILITY NAME (1) DOCKET NUMBER (2) LER NLIUIER (6) PAGE (3)

YEAR SEQUENTIAL REVISION NUMBER NUMBER Browns Ferry Unit 3 05000296 95 001 00 3 of 4 TEXT If more s ace is r uired use additionat co ies of NRC Form 366A (17)

C~ Dates and A roximate Times of Ma'or Occurrences:

June 15, 1995 at 1129 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.295845e-4 months <br /> CDT An airplane severed phase C of the Athens 161kV transmission line, EDGs started and tied to boards at 1207 hours0.014 days <br />0.335 hours <br />0.002 weeks <br />4.592635e-4 months <br /> CDT TVA manually transferred 1A start bus to its alternate power supply (Trinity 161kV) to re-energize the Unit 3 4kV 3A unit board at 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br /> CDT Unit 3 EDGs were returned to standby readiness at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> CDT SGT system secured at 1305 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.965525e-4 months <br /> CDT CREV train A secured at 1412 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.37266e-4 months <br /> CDT TVA provided a 10 CFR 50.72(b)(2)(ii) notification to NRC Operations Center D~ Other S stems or Secondar Functions Affected:

None.

E. Method of Discover This condition was discovered when the control room Operations personnel [licensed, utility) received alarms and indicators that start buses 1A and 2A were de-energized and the EDGs had auto-started.

F. 0 erator Actions:

Operations personnel responded to the event in accordance with approved procedures. Start buses 1A and 2A were repowered when they were manually placed on, their alternate feeder breakers.

G. Safet S stem Res onsesl All safety systems responded as designed for this type of event.

CAUSE OF THE EVENT Immediate Cause:

The immediate cause of the event was the loss of the Athens 161kV line that created an under-voltage condition.

0 NRC FORM 366A U.S. NUCLEAR REGULATORY CQOIISSION APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY IJITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORllARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS HANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, LICENSEE EVENT REPORT .WASHINGTON, DC 20555-0001, AND TO THE PAPERlQRK REDUCTION TEXT CONTINUATION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, NASHINGTOH DC 20503 FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR SEOUENTIAL REVISION NUHBER NUMBER Browns Ferry Unit 3 05000296 95 001 00 4 of 4 TEXT If more s ce is r uired use additional co ies of NRC Form 366A (17)

B. Root Cause:

This event occurred when the Athens 161kV line was inadvertently severed by an airplane.

IV ~ ANALYSIS OF THE EVENT In this event, plant safety systems and associated components performed as designed. Operations personnel immediately identified the cause of the ESF actuation and took appropriate corrective actions to restore the plant systems to standby readiness. Therefore, this event did not affect the health and safety of plant personnel and the public.

Had Unit 3 been at full power operation providing power to the grid, these ESF actuations would not have occurred. Namely, at full power operation, Unit 3 is aligned to its Unit Station Transformer, and the Athens 161kV transmission line is not aligned to supply power to the 4kV shutdown boards.

V. CORRECTIVE ACTIONS A. Immediate Corrective Actions:

Operations personnel restored power to the 1A and 2A start buses and subsequently placed the EDGs in standby readiness. A problem evaluation report (BFPER 950725) was generated to document this event. Systems were returned to a standby readiness condition.

B. Corrective Actions to Prevent Recurrence:

None.

VI+ ADDITIONAL INFORMATION A~ Failed Com onents:

None.

B~ Previous LERs on Similar Events:

None.

VII. COMMITMENTS None.

Energy Industry Identification System (EIIS) system and component codes are identified in the text with brackets (e.g., (XX]).

'l